ML20034H800

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Insp Repts 50-254/93-04 & 50-265/93-04 on 930112-0222. Violations Noted.Major Areas Inspected:Operational Safety Verification,Engineered Safety Feature Sys,Monthly Maint Observation & Monthly Surveillance Observation
ML20034H800
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 03/11/1993
From: Hiland P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20034H787 List:
References
50-254-93-04, 50-254-93-4, 50-265-93-04, 50-265-93-4, NUDOCS 9303220090
Download: ML20034H800 (11)


See also: IR 05000254/1993004

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U.S. NUCLEAR REGULATORY COMMISSION

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REGION III

Reports No. 50-254/93004(DRP); 50-265/93004(DRP)

Docket Nos. 50-254; 50-265

License Nos. DPR-29; DPR-30

Licensee:

Commonwealth Edison Company

Executive Towers West III

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1400 Opus Place Suite 300

Downers Grove, IL

60515

Facility Name: Quad Cities Nuclear Power Station, Units I and 2

Inspection At: Quad Cities Site, Cordova, Illinois

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Inspection Conducted:

January 12 through February 22, 1993

Inspectors:

T. E. Taylor

J. M. Shine

P. F. Prescott

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Approved By:

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Pat Hilfnd, Chief-

Dat'e .

Reactor Projects Section IB

Inspection Summary

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Inspection from January 12 through February 22, 1993 (Report Nos. 50-

254/93004(DRP): 50-265/93004(DRP))

Areas Inspected:

Routine, unannounced safety inspection by the resident

inspectors of licensee action concerningi operational safety verification;

engineered safety feature systems; monthly maintenance observation; monthly.

surveillance observation; report review; and events.

Results: Of the areas inspected, one violation regarding inadequate logic

system functional testing was identified in paragraph 7.

In the remaining

areas, two non-cited violations discussed in paragraph 2.a. and 2.c. were~

identified.

9303220090 930312

'gDR

ADOCK 05000254-

PDR

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EXECUTIVE SUMMARY

Plant Operation

Operations performance was mixed. Operator response'to events (2' Unit 2

scrams) was very good. Two non-cited violations were identified; one for new

fuel misplacement and the other was a missed Technical Specification

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surveillance. Also, two instances of control rod errors occurred. Operations

involvement for the March 1993 Unit 2 refuel outage on March 7,1993, was :

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considered good.

Radiological Controls

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Performance was steady.

Maintenance and Surveillance

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Performance in this area was mixed.

Preparations for the upcoming refuel

outage have been good. One unresolved item was identified concerning

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calibration of flow indicators for IST and surveillance testing.

Engineerino and Technical Support

Performance in this area was weak. Durii.g the inspection period, one

violation for inadequate functional testing was identified. This item was the

result of the inspectors- review of the HPCI and RCIC dual inoperability on

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February 4, 1993.

Region-based inspectors identified three additional

violations concerning.the HPCI torus suction check valve. This was part of

the dual inoperability evaluation. The Regional inspectors' results were

documented in' Inspection Report 254/265-93005.

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DETAILS

11.

Persons Contacted

Commonwealth Edison Company (CECO)

  • R. L. Bax, Station Manager
  • B. Strub, Assistant Superintendent - Operations

D. Gibson, Master Mechanic

  • B. Moravec,' Engineering and Nuclear Construction Site Manager-

D. Craddick, Assistant. Superintendent - Maintenance

G. Klone, Operating Engineer - Unit 1

J. Kopacz, Operatina Engineer-- Unit 2

D. Bucknell, Assistant Technical Staff Supervisor

A. Hisak, Regulatory Assurance Supervisor

  • R. Walsh, Technical Staff Supervisor

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J. Burkhead, Quality Verification Program Supervisor

K. Leech, Security Administrator

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B. McGaffigan, Assistant Superintendent - Work Planning

J. Hoeller, Training Supervisor

  • D. Kanakares. NRC Coordinator - Regulatory Assurance

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  • J. Neal, Quality Verification
  • A. Pedersen,-Operations Consultant
  • Denotes those attending the_ exit interview conducted on. February 22,

1993, or contacted at other times during the. inspection period.

The inspectors also talked with and interviewed several other' licensee

employees, . including members. of the technical and engineering staffs;

reactor and equipment operators; shift engineers and foremen;

electrical, mechanical, and instrument maintenance personnel; and

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contract s'ecurity personnel.

2.

Operational Safety Verification' (71707).

The inspectors observed control room operation, reviewed applicable

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logs, and conducted discussions with control room operators. The

inspectors verified the operability of selected emergency systems',

reviewed tag out records, and verified the proper return to service of

affected components.

Tours of accessible areas of the plant were conducted to observe plant

equipment conditions including potential fire hazards, fluid leaks and-

excessive vibration,.and to verify that' equipment discrepancies were

noted and being resolved by the licensee.

The inspectors observed plant housekeeping and cleanliness conditions-

and verified implementation of radiation protection and physical

security plant controls.

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Inspector observations were:

a.

Recombiner Temperature Surveillance Error

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On-January 14, 1993, the shift control room engineer (SCRE)

noticed that four previous shifts of surveillance readings for

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explosive gas mixture were not initialed as required. During the

verification of recombiner temperatures, the operators were

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required to interpolate the existing graph parameters to determine

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whether the recombiner temperatures were within the required'

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temperature band. However, of the five operators involved, four

noted power <30% instead of interpolating graph parameters as -

required. Areas of weekness identified by the inspector included:

the failure of the SCREs and shift engineers to identify the

anomaly during shift surveillance log reviews and use of a graph

for verifying recombiner temperature that did not include

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operation below 25% power.

This required the operators to

interpolate the existing graph parameters to perform the

surveillance.

The graph was being revised and individuals

involved were counseled on proper surveillance performance and

documentation.

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The missed surveillance for one shift was a violation of the

requirements of the Technical Specifications; however, no Hotice

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of Violation will be issued because the criteria of 10 CFR Part 2,

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Appendix C, paragraph Vll.B.2 were met. This item is considered

closed.

b.

Control Rod Positionino Error

On January 31, 1993, during rod pulls for reactor'startup, two

errors in rod positioning occurred. During initial rod pulls

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prior to criticality, the nuclear station operator (NS0) selected

the H3 instead of the H4 rod and pulled it from 00 to 02. The NSO

identified the error to the nuclear engineer and the shift

management. Subsequently, the control rod was reinserted. The

NS0 was then counseled on use of the' rod worth minimizer and self

check. Later in the startup after criticality, a test of the RCIC

system was needed.. The NSO was directed to insert-rods to set up-

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for the test activity. The HSO had been withdrawing a " group" of

control rods from position 8 to 12 then 12 to 48. Two of the rods

had been pulled to 48 and the third selected.

In error, the NSO

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started to insert the third rod already selected instead of the

two at position 48. Again:the operator identified the error and

notified shift management and the nuclear engineer.

The NSO was removed from the unit and reassigned to the center

desk position. The operator was again counseled on proper rod

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manipulations and attention to detail. Although the HSO committed-

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two rod manipulation errors, the prompt identification and

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notification of management was appropriate and in accordance with

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station procedures. The licensee's response and operator reaction

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to this event was considered adequate. The inspectors had no

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further concerns.

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c.

New fuel Mispositioning

During new fuel receipt and storage activities for the upcoming

Unit 2 outage, a mispositioning of a new fuel assembly occurred.

The fuel handling foreman failed to note the predetermined fuel

location on the nuclear component transfer list (NCTL). After

discovering the error the NCTL was corrected.

The cause of the

event was a failure by the fuel. handling foreman to notice the

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storage of new fuel had been predetermined. On previous shipments

the NCIL was filled in as new fuel was placed in the vaults. A

contributing factor was the lack of communication between the

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nuclear engineer and fuel handling foreman regarding pre-selecting

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new fuel storage locations. The significance of the event was

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considered minimal. The fuel position error did not have any

safety impact. The failure to position fuel in the new fuel vault

per the NC1L was a violation of 10 CFR 50 Appendix B Criteria V;

however, no Notice of Violation will be issued because the

criteria of 10 CFR Part 2, Appendix C, paragraph VII.B.2 were met.

This issue is considered closed.

Two non-cited violations were identified.

3.

Engineered Safety Feature (ESF) 5_ystems (71710)

During the inspection, the inspectors selected accessible portions of

the Unit 1/2 emergency diesel generator to verify its operability

status.

Consideration was given to the plant mode, applicable Technical.

Specifications, limiting conditions for operation action, and other

%,.dicable requirements.

Various observations, where applicable, were

made of: hangers and supports; housekeeping; valve positions and

conditions; potential ignition sources; major component labeling,

lubrication, cooling, etc.;-interior conditions of electrical breakers

and control panels; whether instrumentation was properly installed and

functioning and whether significant process parameter values were

consistent with expected values; whether instrumentation was calibrated;

whether necessary support systems were operational; and whether locally

and renotely indicated breaker and valve positions agreed.

Previous

work requests and outstanding work requests were reviewed.

Discrepancies identified included two valve identification tags missing-

and a terminal strip cover out of position. The noted discrepancies did

not effect the system operability.

The technical staff engineer has

resolved the discrepancies. A sample of system operating, surveillance,

and instrument procedures was reviewed for adequacy and accuracy.

The

inspectors had no further concerns.

No violations and deviations were identified in this area.

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Mont'ly Maintenance Observation ~(62703)-

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Station' maintenance activities _ for both safety relatedLand non-safety-

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related systems were observed and/or. reviewed to-ascertain that'

activities were conducted:in accordance~with approved procedures, . .

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regulatory guides, industry codes or standards,: and in conformance with '

technical specifications.

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The following maintenance activities were observed and/or_ reviewed:

Unit 1/2-B HVAC Pressure Transmitter Replacement

Q05814 Unit 1/2 Diesel Generator Heat Exchanger Inspe'ction -

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Q05735 Unit 1 HPCI System (2301-39) Check Valve Repair

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Unit 1 Reactor protection system (RPS) reserve? electrical

protective assemblies (EPA) troubleshooting and diagnosis

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Q05233 Unit 2 Correct Cocked Saddle Blocks on Fuse Holder Terminal.

Block EE in 902-39 Panel

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Unit 2 New Fuel- Receipt and Inspection

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Q05736 Unit 2 HPCI System (2301-39) Check Valve Repai_r

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Observations:

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a.

RPS Reserve Electrical Protective Assemblies

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The inspectors _ monitored portions of activities associated with

the Unit 1 RPS reserve EPA. The breaker' opened on'two occasions

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with no apparent cause. Management and electrical, maintenance

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(EM)' personnel demonstrated good support ~ for root ~ cause. analysis;

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EM personnel coordinated well with the operational' analysis group

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in tracking the problem upstream to the voltag'e spiking problem of

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the.' voltage regulating transformer. The licensee , subsequently -

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replaced the transformer. The system engineer made the finding.

and was involved.in the process.

b.

HPCI System Control Power

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On January:11, 1993, the Unit '2 NSO, .during a panel' walkdown,

discovered no light indication existed for the HPCI. motor gear

unit (MGU), motor speed changer-(MSC), and stop valve.

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maintenance (EM) determined the loss of power was.due to a cocked:

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electrical termination saddle on a terminal block to a' fuse in the

125 VDC main fuse wire lug which resulted in a loss of electrical'

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continuity..

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The loss of power affected MSC and MGU motors and light

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indications, stop valve light indication, reset solenoid valve

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-(SV-8), trip solenoid valve. (SV-12), thrust bearing: alarm testing'

solenoid valves- (SV-9 and 11), and the' solenoid valves:for the air

operated (AO) steam trap bypass (2-2301-31) and exhaust; drain-pot:

_(2-2301-32) valves.

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'Previously, an LER was submitted by the licensee for a similar

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problem in.the off-gas system caused by a cocked saddle block.

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Corrective actions taken discovered six other cocked saddle blocks

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(including the-one for HPCI). The repairs were: scheduled for the-

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next refuel outage for both units. -The licensee's. work planning -

process failed to consider these items for any short~ outages prior-

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to the' refuel outages. .This weakness in the work planning process,

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resulted in missed opportunities to correct the identified ~

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deficiencies prior to the failure which occurred on January 11'

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1993. Subsequent to the HPCI event all but one'of the original

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six were repaired.' The one remaining item will be worked during

~the March 1993 Unit 2 refuel outage. ' A caution: tag was-placed on

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the affected panel to identify to personnel working'in the area of.

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the wiring. sensitivity. This condition appeared to be an original-

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construction installation problem. The inspectors have no.further

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concerns'with this item,

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No violations or deviations were identified,

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5.

Monthly Surveillance Observation (61726)

The inspectors observed surveillance testing and verified one or more of

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the following: testing was performed in accordance with adequate

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procedures; test equipment was properly calibrated; test results

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conformed with technical specification and procedure requirements, and'

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were properly reviewed; and deficiencies . identified during the test'

activities were resolved by the appropriate personnel.

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The inspectors witnessed or reviewed portions of the following test

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activities:

QCOS 300-4 Unit 1 Control Rod Coupling Integrity--Neutron

Instrumentation Response

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QCIS 1000-2 Unit 1 Monthly High Drywell Pressure Scram Functional-

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Test

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QTS 1311-1,3 Unit 1.' Full Core.LPRM Calibration

Unit 2 Differential Pressure Test of (2)-1402-38B '_ .

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QCOS 6600-1 Unit 1/2 Emergency Diesel Generator Monthly Load Test-

Unit 1/2 Diesel Generato'r Cooling Water Flow Calibration

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Observations:

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Unit 1/2 Diesel Generator Water Flow Calibration'

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On february ll,1993, the 1/2 diesel generator was declared

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inoperable because. diesel generator' cooling water flow for- ECCS.

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room coolers and 1/2 diesel generator was less than required.

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This condition was discovered during performance of a routine

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inservice test activity. Review of the circumstances for the low-

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flow showed no apparent reason- for the decreased flow other than

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potential inconsistencies in the calibration process. Calibration

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of the flow' indication instruments was performed as a skill of the

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craft activity. The inspector's initial review identified the

following concerns:

1)

Training did not specifically address calibration of

the Barton flow indicators,

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Instructions for the calibration were not clearly

documented, and

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Technicians performing the calibration did not refer

to the vendor manual for the calibration activities.

This issue was considered an Unresolved Item pending further

evaluation by the inspectors (254/265 93004-01(DRP)).

b.

Safety Related Contact Test Program

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The inspectors reviewed portions of the Commonwealth Edison safety.

related contact testing program at the Quad Cities station. The

program commitment resulted from issues identified at the Zion

station. The resident and Region-based inspectors discussed the

program status with the station staff and concluded the program

was proceeding adequately.

Review of plant systems covered under

the technical specification was to be completed by January 1994.

The inspectors.will track completion of the program as an Open

Item (254/93004-02(DRS)).

No violations or deviations were identified; .however, one unresolved

item regarding instrument calibration, and one open item regarding

contact testing were identified.

6.

Report Review

During the inspection period, the inspector reviewed the licensee's

Monthly Performance Report for January 1993. The inspector confirmed

that the information provided met the requirements of Technical Specification 6.9.1.8 and Regulatory Guide 1.16.

The inspector also reviewed the licensee's Station Monthly Performance

Update Report for December 1992.

No violations or deviations were identified.

7.

Dual Unit HPCI and RCIC Inocerability (93702)

On February 4,1993, the licensee identified that- the automatic pump

suction transfer circuits for the high pressure coolant. injection (HPCI)-

and reactor core isolation cooling (RCIC) systems were not adequately.

tested. Since the technical specification-(TS) surveillance

requirements were not met for HPCI and RCIC, the licensee entered a 24

hour limiting condition for operation (LCO) and attempted to manually

align the suction paths to the suppression pools (SP). The RCIC systems

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were aligned, filled, vented, and declared operable. However, the-

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licensee was unable to establish " water fill" in the HPCI discharge

piping for either unit. With RCIC operable, the licensee exited .the

associated 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> LCO and entered 14 day LCOs on both units due to

continued HPCI inoperability.

Leaking SP suction check valves allowed a

flow path from the HPCI. discharge piping to the SP. The leakage through

the check valves surpassed jockey fill pump capacity. The licensee

successfully tested the transfer circuits on February 5.

The HPCI check

valves were repaired and tested. The system was declared operable on

February 6, 1993.

The TS required that a logic system functional test be performed for the

HPCI and RCIC systems each refueling outage. The 15 definition of a

logic system functional test required that All relays .and contacts of a

logic circuit be tested from sensor to activated device to ensure all

components are operable in accordance with the design intent. The'

licensee determined the 151CN relay in the SP high water level portion

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of the automatic transfer circuitry was not verified electrh; ally

energized during prior functional tests. Coatequently, the testing

failed to demonstrate functionality of the relay contacts per the intent

of the TS logic system functional test.

Failure to perform adequate

logic system functional testing for the 151CN relay contacts in the HPCI

and RCIC automatic suction transfer circuit is considered a Violation of

Technical Specifications 4.5.C.5 and 4.5.E.5. (254/265 93004-03(DRP))

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On April 9,1990, the licensee's procedure rewrite group identified that

calibration of the low level switches automatic transfer function from

the contaminated condensate storage tank was not performed. After being

informed, electrical and instrument maintenance personnel confirmed the

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finding. Maintenance personnel took no further action. The procedure

group verified that a " functional" test of the automatic suction

transfer was performed. The " functional" test confirmed the appropriate

valves repositioned; however, the test did not demonstrate energization

of all relay contacts.

The procedure rewrite group incorporated

development of the calibration procedures into the procedure rewrite

program. No further corrective action was taken.

"PRC" Engineering Systems performed a review of the HPCI system to

assess overall status of the HPCI preventive maintenance (PM) program.

PRC issued a draft report to the licensee about February 7, 1992.

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executive summary of that report indicated certain calibration and

functional tasks were not performed. The PM coordinator, maintenance

staff supervisor, and HPCI system engineer reviewed the information.

The PM coordinator initiated documentation to add the contacts to the 15

surveillance data base.

In January 1993 the quality verification (QV)

group discovered the discrepancy while reviewing the PRC report, and

informed station management. Technical staff management reviewed the

finding and concluded the TS surveillance was inadequate.

In summary,

information surfaced on two previous occasions which should have

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resulted in resolution of the testing discrepancy prior to the event

date. The inspectors concluded, based on the above, that resolution of

the testing deficiency was untimely.

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Personnel handling the noted findings failed to: apply the proper TS testi

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criteria when-assessing the adequacy of functional testing. The

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inspectors identified a lack of understanding of TS requirements ~ and:a?

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failurt to' inform appropriate managementElevelstof testing deficiencies

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as causal factors of;the event. Through recent experience withithe

safety-related contact testing program the technicalf st'aff personnel who(

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reviewed the QV finding were able to discern the_ operability issue.-

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failure' to promptly-recognize and resolve emergent operability concerns"

was considered a management weakness.

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Maintenance and testing of. the HPCI torus suction check valves appeared

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inadequate, and not commensurate with the: safety. function'of the valve.

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NRC Region III, Division'of Reactor Safety inspectors reviewed the check:

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valve issue discussed above. The results of that' review were documented-

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in Inspection Report 254/265-93005.

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One violation regarding logic system functional testing:was identified.-

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Unit 2 Reactor Scram

On January 29, 1993, Unit 2 scrammed due to a high reactor pressure.

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signal. The licensee's immediate investigation ofLthe scram identified

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that " contractors" working in the area'of the high reactorLpressurez

sensing lines was the probable cause. Operator action.in response to

the event was considered prompt and appropriate. .The inspectors review:

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of the scram and discussion with contractors and operations personne1'

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identified that-

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The cause of the scram appeared to be an individual bumping

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or in some manner causing a vibration on the highLreactor~-

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pressure sensing line. No dirtet action by .an _ individual-

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contractor was identified to have-caused the. scram.

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b.

The licensee's contractor overview-program implementation'

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had weaknesses:

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Theoperationsshiftforemanperforminglthepre-job _

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walkdown did not' identify any specific areas of s

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concern other than to say;that all sensing-lines were.

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sensitive. The sensing line physical arrangement on-

the scaffolding was: configured such that it would be

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easy to inadvertently bump theilines-

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(2)

The operations shift foremen interviewed were not-

aware of management expectations ~for contractor

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overview;

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(3)

Engineering.and construction (ENC) management'

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. expectations were that the assigned ENC engineer.

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should spend.at least-two to three-hoursiduringial

shift at the work area. The ENC engineerLassigned to-

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oversee the work activity didcnot spendia. sufficient'

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amount of time at the job site. ' Unless interested -in

a specific job activity the ENC engineer spent about

30 minutes at the work area during a shift; and

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The contractor foreman directly supervising the

activity had been on the job for the three of the last_'

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five weeks the job was in progress. :The foreman had

not received a walkdown by ENC or operations personnel

of the job site to identify _ sensitive areas. The.

foreman received verbal cautions from the operation _

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shift engineer as-to the sensitivity of the activity.

The licensee's contractor overview program appeared adequate except for

the program implementation weaknesses noted above. -Contractor-

activities will be monitored by inspectors during the March.1993 Unit 2-

refuel outage.

This is considered an Open item pending further review

(254/265-93004-04(DRP)).

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No violations or deviations were identified; however, one open item

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regarding the licensee's contractor overview program was identified.

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Unresolved Items

Unresolved items are matters which require more information in order _to~

ascertain whether _it is an acceptable item, an open. item, a deviation or.

a violation. An unresolved item disclosed during this inspection is

discussed in paragraph 5.

10.

Open item

Open items are matters which: have been discussed with the licensee;

will be further reviewed by the inspector; and involved some actions on

the part of the NRC, licensee, or both. Open items disclosed during the

inspection are discussed in paragraphs 5 and 8.

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11.

Exit Interview

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The_ inspectors met with the licensee representatives denoted in

Paragraph I during the inspection period and at-the conclusion of the-

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inspection on February 22, 1993. The inspectors summarized the scope

and results of the inspection and discussed the likely content of-this -

inspection report. The licensee acknowledged the information'and did

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not indicate that any of the information disclosed during the inspection >

could be considered proprietary in~ nature.

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