ML20029D112

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Insp Rept 50-298/94-03 on 940102-0212.Violations Noted.Major Areas Inspected:Onsite Response to Events,Operational Safety Verification,Maintenance Observations & Surveillance Observations & Followup on CA for Violations
ML20029D112
Person / Time
Site: Cooper Entergy icon.png
Issue date: 04/29/1994
From: Gagliardo J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20029D109 List:
References
50-298-94-03, 50-298-94-3, NUDOCS 9405040046
Download: ML20029D112 (17)


See also: IR 05000298/1994003

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APPENDIX B

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection Report:

50-298/94-03

License: DPR-46

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Licensee: Nebraska Public Power District

P.O. Box 499

Columbus, Nebraska

Facility Name: Cooper Nuclear Station (CNS)

Inspection.At:

Brownville, Nebraska

Inspection Conducted: January 2 through' February'12, 1994,

Inspectors:

R. A. Kopriva, Senior Resident Inspector

W. C. Walker, Resident Inspector

E. E. Collins, Project Engineer

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Approved-

. E.

agliardo, Chief, Project Section C

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Inspection Summar_Y

Areas Inspected:

Routine, unannounced inspection of onsite response to

events, operational safety verification, maintenance observations and

surveillance observations, followup on corrective' actions for violations, and

onsite review of licensee event reports.

Results:

An unexpected actuation of an engineered safety feature during the high

pressure core injection (HPCI) surveillance-indicated procedure problems

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which were not identified as discrepancies-in previous surveillances.

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The recently developed questioning attitude by operators resulted in the

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concern finally being identified (Section 2.1).

The review of several maintenance procedures indicated a lack of

recognition by maintenance personnel concerning procedural requirements

and inadequate implementation of a procedure (Section 3.2.1).

The efforts of maintenance personnel to evaluate alternatives and prejob

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planning for repair of a reactor equipment cooling valve were a noted

strength (Section 4.1).

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Surveillance activities identified a discrepancy in a procedure which

was a strength, but the surveillance should have been stopped and

reviewed when the discrepancy was first observed (Section 5).

The licensee had identified that manual primary containment isolation

valves were not uniquely identified and controlled as a result of the

event documented in Licensee Event Report (LER)93-012, but the licensee

had not yet implemented, at the time of the inspection, the corrective

action to address this issue.

Inspectors identified additional examples

of manual primary containment isolation valves that were not being

controlled by approved station procedures (Section 7.2).

The use of a single, unlocked, manual valve for the containment function

is an unresolved item. Two examples of single valves that did not meet

the design intent were identified.

'ieveral examples where a single,

unlocked valve was used for the containment function were identified

(Section 7.2).

Summary of Inspection Findings:

Unresolved Item 298/9403-01 was opened (Section 7.2).

Violation 298/9403-02 was opened (Section 7.2).

Violation 298/9325-01 was closed (Section 6.1).

Violation 298/9219-03 was closed (Section 6.2).

LER 298/93-016 was closed (Section 7.1).

LER 298/93-012 was closed (Section 7.2).

LER 298/93-011 was closed (Section 7.3).

Attachments:

Persons Contacted and Exit Meeting

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DETAILS

1 PLANT STATUS

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At the beginning of the inspection period, the plant was operating at

100 percent power.

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On January 21, 1994, the licensee initiated a load reduction to approximately

69 percent power as part of the licensee's efforts for fuel conservation.

During the power reduction, the licensee was able to complete its scheduled

turbine testing and to complete maintenance on the Condensate Booster Pump B

oil system.

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Contrcl rod adjustments were also performed prior to increasing power.

Full

power operation was restored on January 24.

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2 ONSITE RESPONSE TO EVENTS (93702)

2.1 HPCI Valve Operability

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On January 19, 1994, during the performance of Surveillance Procedure 6.3.3.2,

"High Pressure Core Injection Valve Operability Test," the pump's minimum flow

Valve HPCI-M0V-M025 unexpectedly stroked open. The control room operators

were stroking open and closed the pump's Valves HPCI-M0V-M019 and -M020, which

are injection valves, when Valve -M025 opened.

Valve -M025 is designed to

open on pump low flow of less than or equal to 400 gpm and a pump discharge

pressure of greater than or equal to 125 psig. Valve -M025 was not expected

to move during the surveillance test.

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The resident inspectors became aware of the concern on January 20, when the

licensee was preparing to make an Emergency Notifications System telephone

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call to the NRC inspectors informing them of the valve actuation, which was

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classified as an unexpected actuation of an Engineered Safety Features

component.

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The inspectors discussed the event with plant management and the system

engineers to obtain an understanding of the valve actuation.

Initially, the

engineers were uncertain as to the root cause of the problem. Maintenance

Work Request (MWR) 94-0289 and special instructions were generated to

troubleshoot the discrepancy.

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The inspectors followed the licensee's actions on determining the cause of the

actuation. The licensee installed a pressure gauge on a test connection for

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the HPCI system and noted a stagnant system pressure of 70 psig which is as

expected by the keep-fill system. The operators closed Valve -M020 and

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recorded a pressure of 100 psig.

Pump Valve -M019 was then opened and a

system pressure of 140 psig was noted. When Valve -M019 was again closed, the

pressure increased to 150 psig. At this point Valve -M020 was reopened, which

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caused Valve -H025 to open, and pressure dropped to essentially 0 psig,

initiating the start of the auxiliary condensate (keep-fill) pump.

The system engineers explained the results of the test.

During the sequence

of events, the pipe section between Valves -M019 and -M020 became pressurized

to 150 psig from the normal system pressure of the keep-fill pump.and the

valve stroking. When Valve -M020 was then opened, a pressure wave propagated

down the line and was picked up by the pressure sensor for Valve -M025. The

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minimum flow valve logic sensed a no-flow condition with a discharge pipe

pressure of more than 125 psig, which satisfied the opening logic for

Valve -M025, which then opened.

The inspectors had originally questioned the engineers concerning the

potential for back leakage from Control Valve CV-29CV, which could have caused

the increased pressure. The engineers responded that the pressure recorded

while performing the special instructions was not leakage by Valve CV-29CV and

the check valve. The pressure present in the pipe between Valves -M019'and

-M020 when they were both closed was not abnormal and, when the valves were

placed in.this configuration per Surveillance Procedure (SP) 6.3.3.2, the

normal _and expected response of Valve -M025 would be to open. A Temporary.

Procedure Change Notice and Procedure Change Notice to.SP 6.3.3.2 were issued

which caution operators to expect Valve -M025 to open and, if it does open, to

proceed with closing it, thereby preventing the recording of this normal

response as a discrepant condition.

The inspectors questioned the licensee about system configurations which could

cause similar occurrences. The licensee indicated that the valve operability

procedure for residual heat removal (6.3.5.2), reactor core isolation

cooling (RCIC) (6.3.6.2), and core spray (CS) systems (6.3.4.2) have been

reviewed for similar configuration. The RCIC system logic and valve operating

procedure is similar to the HPCI system in that the minimum flow valve is

controlled by flow and pressure inputs. A caution for possible minimum flow

valve operation should be considered for SP 6.3.4.2 for the RCIC system.

Minimum flow valve operation during CS and residual heat removal motor-

operated valve (MOV) surveillance testing is not expected because their

respective minimum flow valves are not controlled by pump discharge pressure',

they are controlled by flow rate logic only.

The licensee appeared to have investigated the'cause for the engineered safety

features actuation adequately. There were two concerns identified with the

event. The first was, why had this expected condition not been addressed in

the procedure, and why had the operators not questioned it during past

surveillances.

Licensee representatives indicated that this was identified at

this time because of the new questioning attitude of the employees.

The second concern is that the resident inspectors were not informed of the

engineered safety features actuation until the licensee was about to make an

emergency notification system call. There were no log book entries

identifying a surveillance concern or discrepancy. This concern was discussed

with the licensee.

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2.2 10 CFR Part 21 Reportable Condition

During the report period, the resident inspectors reviewed a 10 CFR Part 21

Reportable Condition which had been issued from General Electric Company on

December 3, 1993.

In 1975, General Electric Company had installed reactor protection system

scram status indicating lights on a BWR/4 control room panel to show when

power was available to scram pilot valve solenoids.

To protect against a hot

short condition, the current limiting isolation resistors for the status

indicating lights were to have been enclosed inside of their respective scram

contractor boxes.

In 1993, it had been discovered that the current limiting isolation resistors

were not located in their respective scram contractor b

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or any separation

enclosure, as required by the plant design. The 10 CFR Part 21 report

indicated that, if a hot short across the terminals of the isolation resistors

were to occur, in conjunction with a transient event, the resulting condition

would not jeopardize the safe shutdown of the plant, but it could be expected

that the minimum critical power ratio safety limit might be exceeded.

The inspectors discussed the concern with licensee management and engineers.

The engineers indicated that they had previous knowledge of the concern

identified in 10 CFR Part 21 report and had investigated the concern.

Their

conclusions were that CNS did not have the particular concern pertaining to a

hot short condition of the current limiting isolation resistors.

The inspectors were shown the style of isolation resistor used at CNS and

inspected the scram indicating lights installed at the plant. The isolation

(current limiting) resistor used at CNS is an integral part of the reactor

protection system scram status light, greatly reducing the potential of a hot

short condition. Also, the scram indicator lights were enclosed within a

protective box, further reducing the potential for an accidental hot short.

2.3 CS Minimum Flow Valve Actuation

The inspectors were informed that on February 1, 1994, during the performance

of SP 6.3.4.2, " Core Spray M0V Valve Operability," while stroking open

Valve M026B which is the Test Loop B return valve, Valve CS-M0V-M05B, the

Pump B minimum flow valve, stroked closed and immediately reopened.

It was

noted from the plant management information system data that when Valve M026B

was stroked open, the pump discharge line pressure decreased and the discharge

line flow as read by PMIS Point N001, indicated a flow rate of approximately

1461 gpm, although Core Spray Pump B was not operating. Valve -M058 is a

normally open valve with position logic controlled by the Core Spray Pump B

discharge flow rate. The logic is designed to have the valve close on a

sensed flow rate greater than 1200 gpm.

The licensee performed portions of the surveillance test in an attempt to

recreate the actuation of Valve -M05B.

Valve -M0268 was stroked again,

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and Valve -M05B did not close on this attempt. Core Spray Loop B was declared

inoperable. The inspectors questioned the licensee as to whether this

actuation had been identified during past performances of the surveillance.

The licensee indicated that this was not expected nor did they recall any

previous actuations.

The licensee pursued the cause of the valve actuation

and their investigation revealed that the Core Spray Loop B flow

instrumentation had been calibrated per SP 6.2.2.4.1 earlier in the day on

February 1.

Further troubleshooting, including stroking of Valve -M0268,

could not recreate the actuation of Valve -M05B.

Review of the work item

history revealed numerous problems attributed to air in the flow indication

instruments and sensing lines.

Review of the electrical circuitry indicated

no factors that would produce this type of indication.

The licensee continued searching for resolution of the valve actuation.

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licensee proceeded to back-flush the flow instrumentation after the event.

The licensee was unable to recreate the scenario nor were they able to

specifically identify a root cause.

On February 11, Valve -M026 was again stroked, with no resulting actuation of

Valve -M05B. The licensee concluded that, since the flow instrumentation

which provides the initiation logic for Valve CS-M0V-M058 had been calibrated

just prior to performing SP 6.3.4.2, and the fact that the problem could not

be recreated, indicated that the unexpected initiation of Valve -M05B was

caused by spurious operation of the flow sensor.

Licensee representatives

stated that a small air-bubble introduced or removed in the instrument sensing

lines during calibration could have produced the type of flow indication

identified when the discharge line was rapidly depressurized to initiate

Valve -M05B closure.

2.4 Conclusions

Operator performance during plant events was good.

However, the failure to

inform the resident inspectors in a timely manner of ongoing events and the

failure to log surveillance discrepancies indicates that continued improvement

is needed in this area.

The licensee had knowledge of a Part 21 concern applicable to the control

panel and had aggressively inrpected the configuration at CNS which confirmed

the fact that the Part 21 concern was not applicable to CNS.

The licensee had

concluded their investigation prior to the inspectors' inquiring about the

concern.

3 OPERATIONAL SAFETY VERIFICATION (71707)

The objectives of this inspection were to ensure that the CNS facility was

being operated safely and in conformance with regulatory requirements and to

ensure that the licensee's management controls were effectively discharging

the licensee's responsibilities for continued safe operation.

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3.1 Control Room Observations

The inspectors observed operations in the control room during normal and

backshift hours on a sampling basis.

The inspectors noted that the shift

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supervisors have taken a more active, aggressive role in controlling and

managing the control room and plant work activities.

Communications and repeat backs in the control room and throughout the plant

continued to improve.

The licensee indicated that they were continuing their

efforts in this area.

3.2 Plant Tours

The licensee was continuing their efforts to improve the housekeeping

condition of the plant, and the overall appearance of the plant was good.

3.2.1 Review of Maintenance Procedures

On January 11, 1994, the inspectors observed work which was in progress under

MWR 94-0094 to repair leaking Service Water Valves SW-A0V-851AV and SW-A0V-

853AV. The inspectors noted that maintenance personnel had used a 1/4-inch

nylon rope to tie off two pieces of equipment.

The nylon rope was draped over

a 3-inch reactor equipment cooling pipe and tied off on the yoke of a reactor

equipment cooling valve.

The inspector questioned the maintenance supervisor

concerning the acceptability of this practice and whether a rigging / loading

analysis had been performed. The licensee had not performed an analysis to

verify that the equipment supported by the nylon rope and piping would have no

adverse impact on the pipe and valve. Maintenance Procedure (MP) 7.0.3.1,

" Control of Lift: Less Than or Equal to 1000 Pounds," Revision 0, provides

guidance on this type of rigging.

Based on the inspectors' review of the

procedure, it appeared that the licensee should have completed Step 7.7.2,

which would have provided a justification for not implementing rigging

controls. This justification was to be signed by an engineer and a

supervisor.

The inspectors also noted that Section 8.10.1.3 of MP 7.0.4, " Conduct of

Maintenance," Revision 0, states, in part, "a review group shall be

established to periodically field observe the implementation of MWRs." The

group is to be composed of one representative from the mechanical, electrical,

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instrument and control (I&C), and weld shops. The procedure specifies that

the maintenance supervisor shall select one corrective maintenance and one

preventive maintenance activity for each shop representative to field observe

for each shop. The inspectors requested a summary of the observations

performed by the maintenance group and received four observations for 1993.

It appears that this program is not being properly implemented.

The

inspectors discussed the two examples above with the maintenance manager and

the engineering manager.

Based on the discussions, it appeared that an error

in judgement was made by the maintenance supervisor and mechanics in not

recognizing that any rigging activity being performed in the reactor building

requires a rigging analysis.

The rigging procedure was reviewed and the

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inspectors discussed the adequacy of the procedure with the maintenance

engineer.

The procedure appeared to be acceptable as written, but indicates

lack of recognition by maintenance personnel of requirements in a maintenance

procedure.

The example of the field observation program not being properly implemented

appeared to result from a breakdown in management direction and poor

communication of expectations for performance, requiring accountability of

assigned activities as they relate to periodic review of maintenance

activities. The inspectors discussed this with the maintenance manager and

were informed that these activities would begin to take place immediately as

specified in the procedure.

3.2.2

Fuel Pool Activities

On February 1, the inspectors observed the receipt of a transportation cask

for removal of two control blades. The cask, which weighed approximately

45,000 pounds, was transferred by crane from the first floor 903-foot

elevation of the reactor building to the refueling floor 1001-foot elevation.

The licensee personnel demonstrated good work practices during the lifting of

the cask. The crane operator was in constant communication with the

maintenance technician on the first floor during the lifting operation. After

the cask was placed on the 1001-foot level, it was washed off in preparation

for lowering into the spent fuel pcol for loading of the two control rod

blades. The licensee's health physics personnel were present at all times

during performance of activities on the refuel floor. The licensee was using

Special Work Permit (SWP)94-118 for entrance into and out of the work area.

Inside the SWP area the health physics staff had established another roped-off

area with step-off pad.

The inspectors questioned the health physics

technician concerning this additional area which was inside the contaminated

area but did not have an SWP.

The area inside the SWP area was roped-off as a

prudent measure to try to limit the spread of contamination on the refuel

floor. However, during the inspectors' observation, one contract individual

crossed through the additional roped-off area and then exited with potentially

contaminated boots. The additional controlled area appeared to be a good

radiological practice to reduce spread of contamination, but it appeared that

the contractors performing the work were somewhat confused on how to perform

work inside this additional roped-off area.

3.2.3

Reactor Eauipment Cooli_nq Heat Exchanger Cleaning

On February 1, the inspectors observed the outlet water box of the Reactor

Equipment Cooling (REC) B Heat Exchanger. The licensee determined that some

pitting existed and several areas were below minimal wall thickness and

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required weld buildup. The inspectors reviewed MWR 94-0438 under which the

ultrasonic testing, weld buildup, and radiographing of the weld areas was

performed.

The inspectors discussed and reviewed the radiographs with the

licensee, and no abnormalities were found.

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During the next scheduled refueling or maintenance outage, the licensee plans

to sandblast the heat exchanger, ultrasonic-test areas for minimum wall

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thickness, perform weld buildup if necessary, and coat the inner surface of

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the heat exchangers with epoxy, to decrease the potential for pitting and

erosion / corrosion.

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3.2.4 High Vibration on CS System

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On February 10, the inspectors observed the performance of SP 6.3.4.1, "CS

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Test Mode Surveillance Operation." A fastener from the flange on Core Spray -

Restricting Orifice - 29A located on the CS test return line had vibrated

loose from the flange and was found on the floor.

The licensee initiated

Deficiency Report 94-048 to document this discovery. After discovery of the

fastener which had vibrated loose, the licensee reviewed potential actions

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which could be initiated for systems with high vibration. Maintenance Work

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Requests 94-0460 and 94-0516 were initiated with special instructions to

increase the torquing on the flange fasteners on both CS Systems A and B.

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licensee also decided to run CS Systems A and B to obtain additional vibration

readings which could be used by the engineering design group to determine if

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additional pipe supports were needed on the CS system.

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During observation of the CS B run, the inspectors noted a loose conduit

connection on Valve CS-MOV-26.

A Deficiency Report 94-118 was initiated by

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the licensee to document this discovery. The inspectors noted that CS

System B was on an increased inservice test frequency for vibration.

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inspectors observed the maintenance technicians collecting vibration readings

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for the piping downstream of Valve CS-M0V-26.

It appeared that vibration was

highest downstream of CS-MOV-?6.

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3.4 Security Observations

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The inspectors observed various aspects of the licensee's security program.

Personnel and packages entering the protected area were observed to be

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properly searched. Vehicles were properly controlled or escorted within the

protected area. Designated vehicles parked and unattended within the

protected area were found to be locked and their keys removed.

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routinely toured the protected area perimeter and found it to be maintained at

an excellent level.

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3.5 Radiation Protection Activities

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The inspectors verified that selected activities of the licensee's

radiological protection program were properly implemented.

Radiation and

contaminated areas were properly posted and generally well controlled.

Health

physics personnel were observed routinely touring the controlled areas.

3.6 Conclusions

Maintenance personnel and procedures continue to need management's attention

to assure that the procedures are being implemented adequately and personnel

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are following the procedures.

Failure to control two manual containment

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valves indicated the need for more positive controls on manual valves designed

for containment isolation purposes.

4 MAINTENANCE OBSERVATIONS (62703)

4.1 Replacement of Reactor Eauipment Cooling Valve

On January 14, 1994, the inspectors observed maintenance troubleshooting of

reactor equipment cooling valve (REC-A0V-TCV-451) under MWR 93-4128. The

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system engineer was also present during the troubleshooting activities. .The

valve was cycled five times and it appeared that the valve was binding in the

valve seat. After discussions with the engineering supervisor and. maintenance

supervisor, a decision was reached by licensee personnel.to replace the valve.

On January 26, the inspectors observed reinstallation of Service Water Inlet

Valve SW-A0V-TCV-4518. The maintenance mechanics were authorized to perform

work under MWR 94-0180 which was at the job site.

The mechanics also had a

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copy of the vendor manual and referred to it when clarification was required,

concerning the crushing of the newly installed flexitallic gaskets. All

signatures were present as required on the MWR and the inspectors reviewed the

comments concerning the as-found condition of the valve. During the removal

of the valve, which was located on top of the torus, a rigging evaluation was

required. This evaluation was present at the work site and attached to the

work package.

In the process of removing the valve, it was necessary to

provide additional rigging pick points prior to proceeding with the. valve

removal. Design Engineering was consulted to provide approval for the

additional rigging. The inspectors discussed with the mechanics the torquing

requirements that were contained in the vendor manual for compressing of the

flexitallic gaskets since no requirements were specific in the work package.

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The mechanics had reviewed the vendor manual and determined that no vendor

requirements were specified for torquing and compressing of. the flexitallic

gaskets.

The inspectors questioned the maintenance mechanics concerning radiological

hazards in the area. The mechanics were aware of the dose rates in the area,

and specific areas which had elevated dose rates were labeled. A radiological

survey was performed prior to the work effort by a health physics technician.

The inspectors also discussed the training requirements for the mechanics

performing the work and verified their qualifications through review of

mechanical maintenance training records.

The inspectors observed that the

maintenance mechanics were working on the top of the torus without.any type of

safety harness to prevent falling off the side of the torus. The MP did not

require the use of a safety harness, however, it appeared that some type of

safety restraint would have been prudent.

The inspectors observed the

satisfactory postmaintenance testing of the valve.

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4.2 Conclusion

The workmanship involved in the replacement of Reactor Equipment Cooling

Valve SW-A0V-TCV-451B was good. The licensee evaluated the alternatives for

repairing the valve and exercised good prejob planning to schedule the

cleaning of the REC B heat exchanger concurrent with the replacement of the

valve.

5 SURVEILLANCE OBSERVATIONS (61726)

5.1 CS Surveillance

On January 11, 1994, the licensee performed SP 6.2.2.4.2, "CS Loops A

and B Pump Time Delay Calibration and Functional / Functional Test,"

Revision 27. The purpose of this surveillance is to verify the operability of

the CS pumps' time delay logic which allows for sequential loading of the

diesel generators when normal station power is unavailable.

During

performance of the surveillance at Step 8.1.13, the control room operator was

uncertain of the status of Indicator Light 14A-DS20A on Panel 9-3 which

verifies the CS pump stop signal is sealed in (illuminated). At the time of

the surveillance, the control room operator did not stop the surveillance and

inform the I&C technicians in the auxiliary relay room of the potential

discrepancy. After the surveillance was completed the control room operator

discussed what was believed to be a discrepancy in the surveillance with the

shifts supervisor, shift technical advisor, and system engineer. The shift

supervisor initiated Operability Determinate 94-005 to ascertain if CS logic

was in accordance with design. The surveillance was signed off as

ratisfactory with a discrepancy noted. The operability determination verified

the CS system was operable and engineering decided to troubleshoot the CS

logic system using MWR 94-0114. The request allowed the technicians to review

the surveillance as specified in the procedure with stopping points to allow

an electrical maintenance technician to measure voltages across certain

relays, to assure no loose connections were evident.

Upon reperformance of

the test, no discrepancy could be found. The seal-in lamp for the pump

functioned as specified in the procedure.

The inspectors discussed with the

system engineer and electrical engineer how this discrepancy as-found in the

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first surveillance would now be documented. The engineers believed the

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procedure possibly needed to be more clear at Step 8.1.13 in that an

explanation could be written explaining when the indicating light should come

on and go off.

The inspectors questioned the engineers on how this

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discrepancy would be documented.

It did not appear that the engineers were

clear on what would be the best method for documenting the discrepancy.

However, the control room operator had already written Deficiency

Report 94-022.

The inspector discussed the procedure with the I&C technicians and learned

that another discrepancy existed which the I&C personnel would address.

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related to Step 8.1.9 which requires an electronic counter to be connected to

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Panel 9-32 in the auxiliary relay room to check the time delay of the relay.

The procedure did not require the electronic counter to be removed from

Panel 9-32, which should be done at Step 8.1.12.

The inspectors found the control room operators' questioning of the

surveillance procedure to be good.

However, it appears the surveillance

should have been stopped when the discrepancy was first observed. Also, the

determination by the I&C technicians that the procedure was not entirely

accurate was good. The inspector noted that the engineers appeared uncertain

on how to appropriately document the above activities using the corrective

action program.

5.2 Conclusions

Surveillance activities identified a discrepancy in a procedure.

However, the

reactor operator did not inform anyone of a potential discrepancy in the

surveillance procedure until the surveillance was completed.

6 FOLLOWUP ON CORRECTIVE ACTIONS FOR VIOLATIONS (92702)

6.1

(Closed) Violation 298/93025-01:

Alarm Procedure Was Not Established and

Maintained For a Safety System Alarm

This violation documented that Alarm Procedure 2.3.2.22 did not appropriately

specify the operator actions to be taken when the alarm was received during

the high pressure coolant system surveillance testing.

To correct the causes of this violation, the licensee issued two Temporary

Procedure Change Notices,93-303 and 93-306, clarifying operator actions

should the "HPCI Turbine Inlet Drain Pot High Level" alarm come in during

surveillance on the HPCI system or if the alarm stays in after securing the

HPCI system. The inspector reviewed the temporary procedure changes and

verified completion of the procedure enhancements.

6.2

(Closed) Violation 298/92019-03:

Failure to identify and Correct the

Presence of Temporary Startup Strainers in the CS System

This violation was subsequently the subject of Special NRC Inspection

50-298/93-06 and the subject of escalated enforcement actions,

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Violations 298/93006-01 and -02.

Violation 298/92019-03 is closed.

7 ONSITE REVIEW 0F LERs

(92700)

7.1

(Closed)

LER 93-016:

Design Change Installation Deficiency Control Room

Emergency Bypass System

This LER documents a condition that could have prevented the fulfillment of a

safety function of a system needed to mitigate the consequences of an

accident. During a design change implementation, an on-the-spot change was

issued. An error by craft personnel in lifting and sparing out the two cables

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specified in the Operations Support Center was committed. . In addition, no

quality control verification was specified in the design change instructions

to ensure the proper cables were lifted.

Bned on the above errors the control room ventilation (HVAC) system did not

isolate and transfer to the emergency bypass mode of operation during the

surveillance test of the control room ventilation system radiation monitor.

Had standard design installation procedures such as implementation of quality

control been incorporated into the Operations Support Center, this event might

have been prevented.

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The inspectors reviewed the documentation which incorporated this LER into

contractor craft training.

In addition, the inspectors verified that industry

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events training for engineering, operations, and station management personnel

who prepare, review, and approve Operations Support Center procedures, was

conducted.

7.2 (Closed LER 93-012: Violation of Primary Containment Integrity Due to

Operation of a 3/4-Inch Vent Valve Durina CS Surveillance Testina

On April 14, 1993, the licensee concluded that opening Valve CS-V-55 when

primary containment integrity was required was not in accordance with the

Technical Specifications. The primary containment integrity definition

required that all manually operated valves not required to be open during

accident conditions be closed.

Valve CS-V-55 was a 3/4-inch manual vent valve

located in the CS test return line, unisolable from the primary containment.

In June 1992, the monthly surveillance test procedure had been revised to open

the valve, attach a vacuum pump, and verify that the system piping had been

completely filled and vented after surveillance testing.

During monthly

surveillance testing from about June 1992 until March 1993, the licensee had

opened Valve CS-V-55 for short periods when primary containment integrity was

required. This event was identified by the licensee's Safety Review and

Assessment Board Safety Evaluation Sub-Committee during a review of

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10 CFR 50.59 evaluations that were done for procedure changes.

The licensee changed Procedure 6.3.4.1, "CS Test Mode Surveillance Operation,"

to prevent opening Valve CS-V-55 unless the plant was in a mode where primary

containment integrity was not required.

Inspectors reviewed Revision 33 and

verified that the procedure prohibited opening Valve CS-V-55 if primary

containment integrity was required.

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Nonconformance Report 93-076 root cause analysis identified the causes for the

event to be personnel miscue in that those who performed the 10 CFR 50.59

review did not recognize that opening Valve CS-V-55 violated primary

containment integrity, and that no programmatic method existed to identify

manual containment isolation valves whose operation would jeopardize primary

containment integrity.

As corrective action, the licensee reviewed the circumstances associated with

the procedure change and 10 CFR 50.59 evaluation with all technical staff,

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operations staff, and Station Operations Review Committee personnel.

The

licensee also planned to develop and implement a method to uniquely identify

manual containment isolation valves, but this action was not completed at the

time of the inspection.

Licensee personnel stated that the planned completion

date of this action was March 18, 1994.

Inspectors walked down the CS system and observed that, for both core spray

subsystems, there were single manual vent valves (Valves CS-V-54 and -55)

between the test return valves and the containment. The valves were not

locked and were not uniquely identified as primary containment isolation

valves.

For Valve CS-V-55, a plug was observed, and licensee representatives

stated that a plug was installed for Valve CS-V-54.

The process and

instrumentation diagram (P&ID) for the CS system, Drawing 2045, showed one

valve and no pipe cap or plug.

Inspectors walked down accessible portions of other systems that penetrated

the primary containment and found several additional examples of single manual

containment isolation valves.

These were Valves PC-V-506 and -507, torus

drain connection (no pipe caps or plugs), Valves RW-V-254 and -258, drywell

equipment and floor sump pump discharges (no pipe caps or plugs), and

Valve RHR-V-145, torus pool cooling return line to torus (pipe plug

installed) .

In addition, from review of the residual heat removal system

P&ID, Drawing 2040, inspectors found several examples of a single manual

containment isolation valve (Valves RHR-V-143, -144, and -146).

In each

example, the valves were not locked and were not identified as primary

containment isolation valves, although the valves performed that function.

The licensee did not control the installation of pipe caps or plugs, and was

not consistent in identifying the caps or plugs on P& ids.

Some caps were

shown on the P&ID and some were not.

Updated Safety Analysis Report (USAR) Chapter V, Section 2.3.5, " Primary

Containment Isolation Valves," classified process line isolation valves as:

Class A valves that communicated directly with the reactor vessel and

penetrated the primary containment; Class B valves that did not directly

communicate with the reactor vessel, but penetrated the primary containment

and communicated with the primary containment free space; and Class C valves

that penetrated the primary containment but did not communicate directly with

the reactor vessel, with the primary containment free space, or with the

environs.

Class A required two valves, Class B required two valves, and

Class C required one valve.

Except for check valves, this discussion required

valves to either automatically close or have remote operation from the control

room. This discussion only addressed process valves and did not address vent,

drain, or test connection manual valves; however, the licensee used it as a

basis for their classification of manual vent, drain, and test connection

valves.

Inspectors questioned the acceptability of a single, unlocked, manual valve

for containment isolation.

Licensee representatives indicated that there was

not a requirement for CNS to lock manual containment isolation valves, since

the plant was licensed before the current general design criteria.

USAR,

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Appendix F, described CNS' design considering the draft general design

criteria published in June 1967. USAR, Appendix F, Section 2.7.3, evaluated

CNS' design considering draft Criterion 53, " Containment Isolation Valves" as

"All lines which penetrate the primary containment anu which communicate with

the reactor vessel or the primary containment free space are provided with at

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lest two isolation valves (or equivalent) in series." Draft Criterion 53

stated " Penetrations that require closure for the containment function shall

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be protected by redundant valving and associated apparatus."

For Valves CS-V-54, CS-V-55, RW-V-254, RW-V-258, PC-V-506, PC-V-507,

RHR-V-145, and RHR-V-146, licensee representatives stated that one unlocked

valve was acceptable since these process lines did not communicate with the

reactor vessel or the free air space.

For Valves RHR-V-143 and -144, which did communicate with the containment free

space (located on the torus spray line), licensee representatives stated that

these valves were not within the containment design basis.

The torus spray

line was a Class B penetration, and two valves were required. The licensee

documented this configuration in Deficiency Report 94-107, dated

February 8, 1994, and performed an operability determination for the as-found

condition. The licensee concluded that the configuration was operable, taking

credit for the pipe plugs as the second boundary.

This operability

determination was not completed by the end of the inspection period and,

consequently, was not reviewed as part of this inspection.

Inspectors asked if the single valve configuration for Valves CS-V-54 and -55

was the original design.

Licensee representatives were unable to answer this

question definitively since they had not yet completed the design

reconstitution for the primary containment system; however, they did find that

Drawing 2045, Revisions 1 and 2 showed two valves.

This drawing was changed

to reflect the one-valve as-built condition by Drawing Change Notice 77-459,

which was approved on June 14, 1977. This change was made to make the P&ID

match the piping isometric drawings and the actual field configuration, which

was only one valve.

No evaluation of the single versus double vent valve

configuration could be found.

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Inspectors also found that P&ID Drawing 2028 showed two manual vent valves

where, in the field, only single Valve RW-V-254 was installed.

Inspectors identified several examples where only one manual valve was used to

provide containment isolation.

In each case, the manual containment isolation

valves were not identified as containment isolation valves and the valves were

not locked.

It appeareo', from the original P& ids, that the original design

provided for two valves. and draft General Design Criterion 53 implied that

redundant valves should be provided for the containment function.

Licensee

personnel stated that redundant valves were only required for lines that

communicated directly with the free air space or the reactor vessel.

The use

of a single manual valve for the containment function is an unresolved item

(298/9403-01) pending additional NRC review.

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Inspectors reviewed the valve line-up procedures and verified that

Valves RHR-V-143, -144, -145, -146, RW-V-254, -258, and CS-V-54, and -55 were

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controlled by approved procedures requiring the valves to be verified in the

closed position. Valves PC-V-506 and -507, however, were not controlled by

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procedure.

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Inspectors reviewed the safety evaluation for Design Change 90-036, which

installed Valves PC-V-506 and -507 during the last refueling outage.

The

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licensee eventually planned to add new instrument lines, but Design

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Change 90-036 only installed the root valves on the torus.

The completion of

the instrument lines was to be done at a later date. The safety evaluation

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concluded that the possibility of operator error to open the valves was not

increased by the design change because the new instrume..t taps will be capped,

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preventing suppression pool water loss.

Inspectors found that the valve caps

were not installed and that the valves were not controlled by procedure.

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licensee personnel installed the pipe caps before the end of the inspection

period.

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10 CFR Part 50, Appendix B, Criterion V, " Instructions, Procedures, and

Drawings," states, in part, " Activities affecting quality shall be prescribed

,

by documented instructions, procedures, or drawings, of a type appropriate to

the circumstances and shall be accomplished in accordance with these

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instructions, procedures, or drawings. The control of primary containment

isolation valve position is an activity affecting quality.

Inspectors

concluded that the failure to control the position of manual primary

containment isolation Valves PC-V-506 and -507 in an approved procedure is a

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violation (298/9403-02) of the regulatory requirements stated above.

7.3 (Closed) LER 93-011:

Secondary Containment Surveillance Methodology

Failed to Identify Leakage Path Between Secondary Containment and the

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Radwaste Building

The events documented in the LER were reviewed in detail in NRC Inspection

Report 50-298/93-17, discussed in an enforcement conference, and the subject

of subsequent escalated enforcement actions.

The licensee's corrective

actions are being tracked under Violation 298/93017-01.

7.4 Conclusions

The licensee had identified that manual primary containment isolation valves

were not uniquely identified and controlled as a result of the event

documented in LER 93-012, but had not implemented corrective action, at the

time of the inspection, to address this issue.

Inspectors identified

additional examples of manual primary containment isolation valves that were

not controlled in approved station procedures.

The use of a single, unlocked, manual valve for the containment function is an

unresolved item.

Two examples of single valves that did not meet the design

intent were identified.

Several examples where a single, unlocked valve was

used for the containment function were identified.

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ATTACHMENT

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1 PERSONS CONTACTED

1.1 Licensee Personnel

R. L. Beilke, Acting Radiological Manager

L. E. Bray, Regulatory Compliance Specialist

S. L. Bray, Quality Assessment Supervisor

R. Brungardt, Operations Manager

J. W. Dutton, Nuclear Training Manager

C. M. Estes, Corrective Actions Program Overview Group (CAP 0G)

R. L. Gardner, Plant Manager

G. R. Horn, Vice President, Nuclear

J. E. Lynch, Plant Engineering Manager

E. M. Mace, Senior Manager Site Support

J. M. Meacham, Senior Nuclear Division Manager of Safety Assessment

D. R. Overbeck, Purchasing and Materials & Supervisor

R. X. Sanchez, CAP 0G

M. E. Unruh, Maintenance Manager

D. A. Whitman, Division Manager of Nuclear Support

V. L. Wolstenholm, Division Manager of Quality Assurance

1.2 NRC Personnel

R. A. Kopriva, Senior Resident Inspector

W. C. Walker, Resident Inspector

C. J. Paulk, Reactor Inspector

The personnel listed above attended the exit meeting.

In addition to the

personnel listed above, the inspectors contacted other licensee personnel

during this inspection period.

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2 EXIT MEETING

An exit meeting was conducted on February 16, 1994.

During this meeting, the

inspectors reviewed the scope and findings of this report. The licensee did

not identify as proprietary any information provided to, or reviewed by, the

inspectors.

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