05000277/LER-1983-002-01, /01T-0:on 830120,RCIC Inboard Steam Supply Isolation Valve Found in Open Position.Caused by Operator Mistakenly Removing Feed from Valve.Operators Counseled to Take Better Precautions

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/01T-0:on 830120,RCIC Inboard Steam Supply Isolation Valve Found in Open Position.Caused by Operator Mistakenly Removing Feed from Valve.Operators Counseled to Take Better Precautions
ML20028G440
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 01/28/1983
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20028G430 List:
References
LER-83-002-01T, LER-83-2-1T, NUDOCS 8302090349
Download: ML20028G440 (1)


LER-1983-002, /01T-0:on 830120,RCIC Inboard Steam Supply Isolation Valve Found in Open Position.Caused by Operator Mistakenly Removing Feed from Valve.Operators Counseled to Take Better Precautions
Event date:
Report date:
2771983002R01 - NRC Website

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80 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10131 lDuring Unit operation, observation in the control' room revealed i

l indicating lights for the RCIC inboard steam supply isolation valve were l O 3 lnot lit, because the breaker for the valve had been opened. Since the i

0 4 Ivalve was opened when the feed breaker was opened,it was not capable of I.

O a O 6 lClosind on an isolation siQnal. DurinG that time the redundant isolationI lTITl Ivalve was not in the closed rosition as required when an isolation valvei 10 l81 lis operable.

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I l The inoperable isolation valve was caused by an operator applying i O l block to remove the reactor water cleanup system from service and I

i i l mistakenly removing the feed from the RCIC system steam supply isolationi

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