05000316/LER-1982-087-03, /03L-0:on 821101,circuit Breaker for Auxiliary Feedwater Valve from West Auxiliary Feed Pump to Steam Generator 24 Found in Off Position.Cause Not Determined. Parts Bin Repositioned to Preclude Inadvertent Operation

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/03L-0:on 821101,circuit Breaker for Auxiliary Feedwater Valve from West Auxiliary Feed Pump to Steam Generator 24 Found in Off Position.Cause Not Determined. Parts Bin Repositioned to Preclude Inadvertent Operation
ML20028B352
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 11/19/1982
From: Camp M
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20028B346 List:
References
LER-82-087-03L-01, LER-82-87-3L-1, NUDOCS 8211300311
Download: ML20028B352 (1)


LER-1982-087, /03L-0:on 821101,circuit Breaker for Auxiliary Feedwater Valve from West Auxiliary Feed Pump to Steam Generator 24 Found in Off Position.Cause Not Determined. Parts Bin Repositioned to Preclude Inadvertent Operation
Event date:
Report date:
3161982087R03 - NRC Website

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60 68 OOCK ET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 PVENT DESCRIPTION AND PROBABLE CONSEQUENCES Oio 10121 ICIRCUIT BREAKER FOR MOTOR OPERATED AUXILIARY FEEDWATER VALVE FROM WEST MOTOR I

lO 131 l DRIVEN AUXILIARY FEED PUMP TO STEAM GENERATOR 24 WAS FOUND IN THE "0FF" POSITION. l iTHIS IS CONTRARY TO T.S. 3.7.1.2.

THE CONTRCL ROOM OPERATOR NOTICED VALVE LAMPJ O 4 O s IWAS NOT LIT. AN OPERATOR WAS SENT TO VERIFY BREAKER POSITION, FOUND IT "0FF",

1 F5Tiil 1THEN RECLOSED BREAKER. THE VALVE REMAINED IN ITS NORMALLY OPEN POSITION.

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