LER-1981-052, /03L-0:on 810918,during Normal Operation,Ps 504-C Switch Failed.Caused by Worn Out Micro Switch.Switch Replaced |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2371981052R03 - NRC Website |
|
text
_.. _ _ -.. _.. _.. -. _ _ _ _. -
u.s. NUCLEAR REGULATCRY COMMISSION __
LICENSEE EVENT REPORT
. CCNTROL SLCCK:
l l
l l
l (PLEASE PRINT OR TYPE ALL REQUIRED INPORMATION)
Io i t l l T ! L l D l R l.S l 2 l@50 l0 l-l0 l0 l0 l0 l0 l-l0 l0 lgl4 l1l1l1l1gl l
l 7
8 9 UCENsEE CooE 14 1
UCP.NsE NUMSER 25 26 UCENSE TYPE Jo n7 CAT 58 CON'T l001I sovy l L @l 0 l 5 l 0 l 0 l 0 l 2 l 3 l7 gl 0l 8; 2l 3l 8l 1gl0 l9 l1 l8 l8 l1 7
8 80 61 coCKET NVVS E R 68 69 EVENT oATE 74 75 REPORT oATE 40 EVENT DESCRIPTION AND PRCBABLE CCNSECUENCES O'o
. I o l 21 l During normal operation, PS 504-C was found to have failed which caused an alarm indi-Since g cating bypass of generator load reject and turbine stop valve closure scrams.
,g,3,
- this bypass should not occur when power was above 45%, the bypass was removed by re-I l o ! s I l m Ving Power to the bypass relay. This action restored the requirements of Tech.
J l S ec Table 3.1.
Safety significance was minimized because three remaining aw Mches P
l o 16 l I
l o l 71 l were an operaw w pdm W muun n4 hn an m Wau gm bd6 x safety of the public.
First event of this type.
I ail 7
8 9 80 SYSTEM
CAuSE
CAUSE COMP.
VALVE cooE cooE suecoot suscooE susCooE II l^ l@ LEjg l B lg lI lgcuPgNEycogE gU 18 LSjg l Z j g lo i s l' l
g g
7 8
9 10 11 12 13 18 1
20 SEQUENTIAL OCCURRENCE REPORT REVlileN LER EVENT YEAR REPORT No.
CooE TYPE N
O asg/Ro 18lil l-i 1015 2l l-l l 0) 3l lLl l_._l l gl su 21 22 23 24 26 27 28 29 30 31 32 EN C P T
MET o
' R sus l PoR 8.
L
~
MAN lNlg lYlg lN[g l8l$lYlY g' l C gl34Z jg. l Z lg l6Zl@ l0l l
[
33 35 3
37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CCRREC IVE ACTIONS h I i l o I. l The cause of this event was attributable to a worn out micro switch in PS 504-C.
Put g i pres'sure switch was replaced with a like for like. switch.
DIS-500-7 was then per-gl fomed on the new switch to verify operability. DIS 500-7 will continue to be per-l, ; 31 l formed monthly._
l
.titelI I
7 8 9 80 STA
% POWER R STATUS I
Y otScoVERY oEsCRIPTToN l115 l l E l@ l0 l9 l2 lgl
$[A l
l Al l
Operator Observatior l
AbVITY Co TENT vNTCP ACTIVITY @ l LocArroN op RELEASE h (ELEAsE@o op RELEASE lZlgl N/A g lZ l
N l
l PERSONNEL ExposuEEs oEscR PricN h NumeER TYPE l 1 l 7 l l0 l0 l0 l@l Z l@l l
PERsoNNEt iNJu'EiEs oEscRiPrioN@
NuueER lt la l l0 l0 l0 l@l
[<^
l 7
8 9 11 12 80 Loss op oR oAuacE To PactuTY G B109290573 810918 TvPE oEscRiPTies c/
ADR ADOCK 05000237 l t 191 l Zl@l NA S
PDR l __ _
7 8 9 to 80 E CRIPTioN r2 lal lNISsuEfhl NA l
llllllllllll lg*
7 8 9 10 68 69 80 3 NAME OF PREPARER
.PHCNEt
n
((a)
DEVIATION REPORT '
7 DVR NO.
Commonwealth Ed.ison STA UNIT YEAR N O.
D-12 81 - 95 PART 1[ Tl TLE OF DEV1AT Received Alarm [ON OCCU RRED Turbine Pressure Generator Load Reject and Stop Valve 8/23/81 2025 Bvoass" DATE TIME SYSTEM decCTED 500
PLANT CONDITIONS
TESTING C C Reactor Protecticn System Run 2343 760 E
p,,
, LOAD (MWE)
YES NO
~
DESCRIPTION OF EVENT
At 2023 received alarm 902-5 (H-4) " Turbine Pressure Generator Load Reject and Stop Valve Scram Bypass." Went to panel 902-15 and found relay 590-123C energized.
Looked at print 12E2465 and 302-15 then pulled fuse 590-726C to verify that relay 590-123C would drop out.
Relav 590-123C did (OVER)
DESCRIPTION OF CAUSE Bellave at this time pressure switch 504C has failed. Called in IM's to repair switch.
OTHER APPLICABLE INFORMATION Relays 590-123A. B, and D were de-energized as expected.
EQUIPMENT YES DR NO.
WR NO.
Gary L. Smith 8/23/81 FAILU RE R NO N/A 15331 eESPONSISLE SUPEEVISOR DATE PART 2 l OPFoATING ENGINEERS COMMENTS Bvpass txtav 590-123C placed in the conservative position upon operability verification until repair to oressure switch 504C were completed.
SAFETY-TYPE OF CEVIATION EVENT CF POTENTIAL TECH SPEC NON-REPORTABLE ANNUAL RELATED REPORTABLE OCCURRENCE PUBLIC INTEREST VIOLATION OCCURRENCE.
REPORTI NG WR ISSUED"
- I 14 DAY YES X YES X lX 30 DAY N
ON NO NO PEPORTABLE CCCURRENCE ACTION ITEM NO.
PROMPT ON-SITE NOTIFICATION NUMaER R. M. Ragan 8/24/81 0600 1 - 4X 81-52/0LC TITLE DATE TIME TITLE CATE TIME 24-HOUR NRC NOTIFICATION PROMPT OFF-SITE NOT!FICATION X
TPH Mike Jordan 24/81 0800 F. A. Palmer 8/24/81 0902 REGION III DATE TIME TI TL E
- - DATE
. TIME TGM REGION III & COL CATE TIME _._
TlTLE DATE TIME
/-
I RESPONSI BLE CCMP ANY 0FFI CER INFORMED OF 10 C FR 21
- - _ - ~
i M M /fL 4 / M m
)
CATE Ith CONDI TIONS AND TWEt A PEPO AT TO NPC (John /. Wujcig/a ~ Q 8/24/81 W
REVI EW AND COMPLETED OPERATING ENGINEEF DATE ACCEPTANCE BY STATION REVIEW g ^g W '
N-A
~
AS REOUIRED A
DATE IIT b RESOLUTION APPROVED AND
/ f/
AUTHORIZED FOR DISTRIBUTICN
' -STATI S
l N TENDEN T
/ DATE
$4*st7' fo 77 (F0#u 15*$2-7) a
e e
y.
DESCRIPTION OF EVENT
da-energize and the alarm 902-5 (H-4) did clear. At 2027 we left this fuse pulled allowing the unit to run as permitted by Tech. Spec. Table 3.1, which requires that we have a minimum number of operable instrument channels per Trip System for both the gsnarator load retect (>45%) and Turbine Stop Valve Closure (>45%) scrams. Fuse was taksn OOS per outage II-1425.
8-4 t
16
'i o
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000249/LER-1981-001, Has Been Cancelled | Has Been Cancelled | | | 05000010/LER-1981-001-03, /03X-1:on 801210,radwaste Storage Tank Sampling Frequency Failed to Meet Tech Spec Requirements.Caused by Personnel Failure to Follow Procedures.Personnel Reinstructed | /03X-1:on 801210,radwaste Storage Tank Sampling Frequency Failed to Meet Tech Spec Requirements.Caused by Personnel Failure to Follow Procedures.Personnel Reinstructed | | | 05000010/LER-1981-001, Forwards LER 81-001/03X-1 | Forwards LER 81-001/03X-1 | | | 05000249/LER-1981-003-03, /03L-0:on 810120,Model 288 Differential Pressure Indicating switch,3-1349B,tripped Above Tech Spec Limit. Caused by Instrument Drift.Switch Readjusted & Repeatability Verified | /03L-0:on 810120,Model 288 Differential Pressure Indicating switch,3-1349B,tripped Above Tech Spec Limit. Caused by Instrument Drift.Switch Readjusted & Repeatability Verified | | | 05000249/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000010/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000237/LER-1981-005, Forwards Updated LER 81-005/03X-L.Deviation Rept Encl | Forwards Updated LER 81-005/03X-L.Deviation Rept Encl | | | 05000237/LER-1981-005-03, During Local Leak Rate Testing,Measured Leakage of Single Isolation Valve Exceeded Tech Specs.Caused by Normal Deterioration of Valve Seat. Valve Replaced | During Local Leak Rate Testing,Measured Leakage of Single Isolation Valve Exceeded Tech Specs.Caused by Normal Deterioration of Valve Seat. Valve Replaced | | | 05000237/LER-1981-006, Forwards Updated LER 81-006/01X-1 | Forwards Updated LER 81-006/01X-1 | | | 05000237/LER-1981-006-01, Excessive Leakage Indicated Various Penetrations in Feedwater Check Valves. Caused by Cracked O Ring & Worn Swing Pins.Valves Repaired & Broken Components Replaced | Excessive Leakage Indicated Various Penetrations in Feedwater Check Valves. Caused by Cracked O Ring & Worn Swing Pins.Valves Repaired & Broken Components Replaced | | | 05000237/LER-1981-007-03, /03L-0:on 810122,temp Switch TS 2-261-18D Failed to Trip.Caused by Fill Matl Leakage Due to Broken Capillary Tube Close to Sensing Bulb.Broken Switch Replaced W/New Calibr Switch | /03L-0:on 810122,temp Switch TS 2-261-18D Failed to Trip.Caused by Fill Matl Leakage Due to Broken Capillary Tube Close to Sensing Bulb.Broken Switch Replaced W/New Calibr Switch | | | 05000237/LER-1981-007, /03L for Dresden, Unit 2 Re While Conducting Steam Line Area Temperature Switch Calibration Surveillance, Temperature Switch TS 2-261-180 Failed to Trip | /03L for Dresden, Unit 2 Re While Conducting Steam Line Area Temperature Switch Calibration Surveillance, Temperature Switch TS 2-261-180 Failed to Trip | | | 05000237/LER-1981-011-03, L-0 for Dresden, Unit 2 Re Observed Inadequacies in the Implementation of Administrative or Procedural Controls Which Threaten to Cause Reduction of Degree of Redundancy Provided in Reactor Protection Systems or Engineered S | L-0 for Dresden, Unit 2 Re Observed Inadequacies in the Implementation of Administrative or Procedural Controls Which Threaten to Cause Reduction of Degree of Redundancy Provided in Reactor Protection Systems or Engineered Safety Feature | | | 05000249/LER-1981-014, Forwards LER 81-014/03L-0 | Forwards LER 81-014/03L-0 | | | 05000249/LER-1981-014-03, /03L-0:on 810616,during Scram Air Sys Header Pressure Switch Calibr,Pressure Switches 3-302-99A & B Actuated W/Setpoint Lower than Required.Caused by Instrument Setpoint Drift.Switches Reset | /03L-0:on 810616,during Scram Air Sys Header Pressure Switch Calibr,Pressure Switches 3-302-99A & B Actuated W/Setpoint Lower than Required.Caused by Instrument Setpoint Drift.Switches Reset | | | 05000237/LER-1981-015, /03L-0 for Dresden, Unit 2 Re the Fire Marshall Discovered That the Heat Detectors Were Not Functionally Tested within the 6 Month Interval Required by Tech. Spec. 4.12.A.1 | /03L-0 for Dresden, Unit 2 Re the Fire Marshall Discovered That the Heat Detectors Were Not Functionally Tested within the 6 Month Interval Required by Tech. Spec. 4.12.A.1 | | | 05000249/LER-1981-015-03, /03L-0:on 810618,switch Actuated at 32.8 Inches During Calibr of Isolation Condenser Steam/Condensate Line High Flow.Caused by Instrument Drift.Switch Reset | /03L-0:on 810618,switch Actuated at 32.8 Inches During Calibr of Isolation Condenser Steam/Condensate Line High Flow.Caused by Instrument Drift.Switch Reset | | | 05000249/LER-1981-015, Forwards LER 81-015/03L-0 | Forwards LER 81-015/03L-0 | | | 05000237/LER-1981-016, Forwards LER 81-016/03X-1 | Forwards LER 81-016/03X-1 | | | 05000237/LER-1981-016-03, /03X-1:on 810408,noted That off-stream Liquid Effluent Monitor Had Not Been Functionally Tested on Monthly Basis.Caused by Deletion of Surveillance After Replacing on-stream Monitor w/off-stream Monitor | /03X-1:on 810408,noted That off-stream Liquid Effluent Monitor Had Not Been Functionally Tested on Monthly Basis.Caused by Deletion of Surveillance After Replacing on-stream Monitor w/off-stream Monitor | | | 05000249/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000249/LER-1981-016-03, /03L-0:on 810618,water Level Instrument Surveillance Found LIS 263-57A Tripping Above Tech Spec Levels for Low Level Scram & Low Water Level Isolation. Caused by Instrument Setpoint Drift.Setpoint Adjusted | /03L-0:on 810618,water Level Instrument Surveillance Found LIS 263-57A Tripping Above Tech Spec Levels for Low Level Scram & Low Water Level Isolation. Caused by Instrument Setpoint Drift.Setpoint Adjusted | | | 05000249/LER-1981-017, Forwards Updated LER 81-017/03X-1 | Forwards Updated LER 81-017/03X-1 | | | 05000249/LER-1981-017-03, 3B Motor Generator Set Undervoltage Relay Failed to Trip on Undervoltage Signal. Caused by Sticking Relay Tripping Device.Tripping Device Cleaned,Lubed & Placed Back in Svc | 3B Motor Generator Set Undervoltage Relay Failed to Trip on Undervoltage Signal. Caused by Sticking Relay Tripping Device.Tripping Device Cleaned,Lubed & Placed Back in Svc | | | 05000237/LER-1981-017-03, /03L-0:on 810408,QA Audit Discovered That Temp of Cells Adjacent to Pilot Cell Had Not Been Taken,Per Tech Specs.Caused by Inadvertent Oversight Due to Inadequate Procedures.Change Will Be Implemented by June 1981 | /03L-0:on 810408,QA Audit Discovered That Temp of Cells Adjacent to Pilot Cell Had Not Been Taken,Per Tech Specs.Caused by Inadvertent Oversight Due to Inadequate Procedures.Change Will Be Implemented by June 1981 | | | 05000237/LER-1981-017, Forwards LER 81-017/03L-0 | Forwards LER 81-017/03L-0 | | | 05000249/LER-1981-018, Forwards LER 81-018/03L-0 | Forwards LER 81-018/03L-0 | | | 05000249/LER-1981-018-03, /03L-0:on 810619,LIS 263-72B Found Tripping Above Tech Spec Limit During Monthly Water Level ECCS Instrument Surveillance.Caused by Instrument Setpoint Drift.Setpoint Adjusted.Deviation Rept Encl | /03L-0:on 810619,LIS 263-72B Found Tripping Above Tech Spec Limit During Monthly Water Level ECCS Instrument Surveillance.Caused by Instrument Setpoint Drift.Setpoint Adjusted.Deviation Rept Encl | | | 05000249/LER-1981-019-03, /03L-0:on 810821,main Steam Line High Flow Switches Dpis 3-261-2 & 3-261-2D Found Above Tech Spec Limits.Caused by Torque Shaft Gears Binding on Linkage Gears from Normal Wear & Filings Buildup.Gears Cleaned | /03L-0:on 810821,main Steam Line High Flow Switches Dpis 3-261-2 & 3-261-2D Found Above Tech Spec Limits.Caused by Torque Shaft Gears Binding on Linkage Gears from Normal Wear & Filings Buildup.Gears Cleaned | | | 05000249/LER-1981-019, Forwards LER 81-019/03L-0 | Forwards LER 81-019/03L-0 | | | 05000237/LER-1981-020-01, During ASME Hydrostatic Test,Water Observed Seeping from Cracks in 2.5-inch Rx Head Spray Line.Caused by Chloride Induced Stress Corrosion Cracking.Cracks Cut Out & Piping Replaced | During ASME Hydrostatic Test,Water Observed Seeping from Cracks in 2.5-inch Rx Head Spray Line.Caused by Chloride Induced Stress Corrosion Cracking.Cracks Cut Out & Piping Replaced | | | 05000237/LER-1981-020, Forwards Updated LER 81-020/01X-1 | Forwards Updated LER 81-020/01X-1 | | | 05000249/LER-1981-020, Is Canceled | Is Canceled | | | 05000249/LER-1981-021-03, Pinhole Leak Found on Reactor Water Cleanup Line from Regenerative Heat Exchanger. Caused by Sensitization During Initial Welding.Other Internal Cracks Discovered.Heat Exchanger Loop Replaced | Pinhole Leak Found on Reactor Water Cleanup Line from Regenerative Heat Exchanger. Caused by Sensitization During Initial Welding.Other Internal Cracks Discovered.Heat Exchanger Loop Replaced | | | 05000249/LER-1981-021, Forwards LER 81-021/03L-0 | Forwards LER 81-021/03L-0 | | | 05000249/LER-1981-022, Forwards LER 81-022/03L-0 | Forwards LER 81-022/03L-0 | | | 05000249/LER-1981-022-03, /03L-0:on 810902,vessel low-low Water Level Isolation Switch Had Setpoint of 116.8 Inches,Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Setpoint Adjusted | /03L-0:on 810902,vessel low-low Water Level Isolation Switch Had Setpoint of 116.8 Inches,Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Setpoint Adjusted | | | 05000237/LER-1981-023, Forwards LER 81-023/03L-0 | Forwards LER 81-023/03L-0 | | | 05000237/LER-1981-023-03, /03L-0:on 810511,while Running HPCI Pump Test, Operator Observed Torus Wide Range Level Instrument Reading 0 Inches & Narrow Range Level Instrument Reading Approx 2 Inches & Oscillating.Caused by Personnel Error | /03L-0:on 810511,while Running HPCI Pump Test, Operator Observed Torus Wide Range Level Instrument Reading 0 Inches & Narrow Range Level Instrument Reading Approx 2 Inches & Oscillating.Caused by Personnel Error | | | 05000249/LER-1981-023-03, /03L-0:on 810904,while Conducting Quarterly Scram Discharge Vol Continuous Level Monitor Calibr Check,West & East Bank/East Transducer high-high Level Alarm Tripped. Caused by Setpoint Drift | /03L-0:on 810904,while Conducting Quarterly Scram Discharge Vol Continuous Level Monitor Calibr Check,West & East Bank/East Transducer high-high Level Alarm Tripped. Caused by Setpoint Drift | | | 05000249/LER-1981-023, Forwards LER 81-023/03L-0 | Forwards LER 81-023/03L-0 | | | 05000249/LER-1981-024-01, /01T-0:on 810914,ultrasonic Testing Revealed Water in Steam Supply Line to HPCI Turbine.Caused by Low Point in Horizontal Section of Pipe.Drain Line Installed in Low Point & Routed Back to Same Line at Lower Elevation | /01T-0:on 810914,ultrasonic Testing Revealed Water in Steam Supply Line to HPCI Turbine.Caused by Low Point in Horizontal Section of Pipe.Drain Line Installed in Low Point & Routed Back to Same Line at Lower Elevation | | | 05000237/LER-1981-024-03, /03L-0:on 810513,monthly Surveillance for Standby Liquid Control Tank Sampling Found 3 Days Overdue.Caused by Lack of Personnel Attention.Personnel Admonished.Tank Sampled | /03L-0:on 810513,monthly Surveillance for Standby Liquid Control Tank Sampling Found 3 Days Overdue.Caused by Lack of Personnel Attention.Personnel Admonished.Tank Sampled | | | 05000249/LER-1981-024, Forwards LER 81-024/01T-0 | Forwards LER 81-024/01T-0 | | | 05000237/LER-1981-024, /03L-0 for Dresden, Unit 2 Re While Conducting Routine Review of Surveillance, It Was Found That the Monthly Surveillance Required by Tech. Spec. 4.4.c.1 for Standby Liquid Control Tank Sampling Was Three Days Overdue | /03L-0 for Dresden, Unit 2 Re While Conducting Routine Review of Surveillance, It Was Found That the Monthly Surveillance Required by Tech. Spec. 4.4.c.1 for Standby Liquid Control Tank Sampling Was Three Days Overdue | | | 05000237/LER-1981-025, Forwards LER 81-025/03L-0 | Forwards LER 81-025/03L-0 | | | 05000237/LER-1981-025-03, /03L-0:on 810518,during Plant Tour by Operations Personnel,Low Pressure Leg of Isolation Condenser Level Indication Found Valved Out.Probably Caused by Valve Not Being Reopened After Sampling.Valve Opened | /03L-0:on 810518,during Plant Tour by Operations Personnel,Low Pressure Leg of Isolation Condenser Level Indication Found Valved Out.Probably Caused by Valve Not Being Reopened After Sampling.Valve Opened | | | 05000249/LER-1981-025-01, During Automatic Depressurization Sys Valve Operability Surveillance,B Electromatic Relief Valve Failed to Open at Rated Pressure. Caused by Excessive Leakage on Threads | During Automatic Depressurization Sys Valve Operability Surveillance,B Electromatic Relief Valve Failed to Open at Rated Pressure. Caused by Excessive Leakage on Threads | | | 05000249/LER-1981-025, Forwards Updated LER 81-025/01X-1 | Forwards Updated LER 81-025/01X-1 | | | 05000249/LER-1981-026-03, /03L-0:on 810915,while Shutting Down,Rod P-10 Showed Wrong Position on Rod Worth Minimizer.Caused by Several Diode Failures on Two Digital Output Printed Circuit Boards.Boards Removed,Repaired & Tested Satisfactorily | /03L-0:on 810915,while Shutting Down,Rod P-10 Showed Wrong Position on Rod Worth Minimizer.Caused by Several Diode Failures on Two Digital Output Printed Circuit Boards.Boards Removed,Repaired & Tested Satisfactorily | |
|