05000368/LER-1981-030-03, /03L-0:on 810731,during Design Mod Check of Remote Control Hydrogen Analyzer Sample Pump 2P162,found No Air Flow Delivered to One Analyzer.Cause Undetermined.Sample Pump Operable within 30 Days

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/03L-0:on 810731,during Design Mod Check of Remote Control Hydrogen Analyzer Sample Pump 2P162,found No Air Flow Delivered to One Analyzer.Cause Undetermined.Sample Pump Operable within 30 Days
ML20010H939
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 08/31/1981
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20010H932 List:
References
LER-81-030-03L, LER-81-30-3L, NUDOCS 8109290429
Download: ML20010H939 (1)


LER-1981-030, /03L-0:on 810731,during Design Mod Check of Remote Control Hydrogen Analyzer Sample Pump 2P162,found No Air Flow Delivered to One Analyzer.Cause Undetermined.Sample Pump Operable within 30 Days
Event date:
Report date:
3681981030R03 - NRC Website

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8 60 61 DoCRET NUMGtm tie 69 (VENT DATE 74 iS HF,OHi DATE 80 EVENT DESCRlPTION AND PROSA8LE CONSEQUENCES to i During Mcde 1 operation, while c ecking a design modification for remote i o 2 (Control Room) control of Hydrogen Analyzer Semple pump, 2P162, it was m,n i a. i identified that no air flow was being delivered to the Hydrogen Analyzers L n panel 2C128. The redundant Hydrogen Analyzer remained operable.

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