05000324/LER-1981-095-03, /03L-0:on 810904,reactor Level Instrument 2-B21-LIS-NO42B Found to Be Actuating Below Required Reactor Level.Caused by Instrument Being Out of Calibr Due to Instrument Drift.Instrument Calibr & Returned to Svc

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/03L-0:on 810904,reactor Level Instrument 2-B21-LIS-NO42B Found to Be Actuating Below Required Reactor Level.Caused by Instrument Being Out of Calibr Due to Instrument Drift.Instrument Calibr & Returned to Svc
ML20010H848
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 09/18/1981
From: Pastva M
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20010H847 List:
References
LER-81-095-03L, LER-81-95-3L, NUDOCS 8109290351
Download: ML20010H848 (1)


LER-1981-095, /03L-0:on 810904,reactor Level Instrument 2-B21-LIS-NO42B Found to Be Actuating Below Required Reactor Level.Caused by Instrument Being Out of Calibr Due to Instrument Drift.Instrument Calibr & Returned to Svc
Event date:
Report date:
3241981095R03 - NRC Website

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NRC FORM 386 U. S. NUCLE AR REGULATORY COMMISSION 17 77)

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60 61 DOCKET NUMBER 68 69 EVENT DATE 74 7b REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h lDuring the performance of ADS Reactor Low Water Level No.1 Channel Calibration and l

O 2 l Functional Test, PT ll.l.6PC, it was found that reactor level instrument, 2-B21-LIS-l o 3 4

fB TTI l N042B, Model No. 4418, actuated at 154.8" reactor level. This instrument is required l lio151ltoprovideaninputtothe"B"ADSlogicat162.5"reactorvessellevel.

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