05000324/LER-1981-085-03, /03L-0:on 810808,rod 26-11 Did Not Have RTGB Position Indication at Position 47.Probably Caused by Defective Rod Position Indication Probe Switch.Problem Will Be Corrected During Future Outage

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/03L-0:on 810808,rod 26-11 Did Not Have RTGB Position Indication at Position 47.Probably Caused by Defective Rod Position Indication Probe Switch.Problem Will Be Corrected During Future Outage
ML20010F116
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 08/27/1981
From: Pastva M
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20010F110 List:
References
LER-81-085-03L, LER-81-85-3L, NUDOCS 8109090385
Download: ML20010F116 (1)


LER-1981-085, /03L-0:on 810808,rod 26-11 Did Not Have RTGB Position Indication at Position 47.Probably Caused by Defective Rod Position Indication Probe Switch.Problem Will Be Corrected During Future Outage
Event date:
Report date:
3241981085R03 - NRC Website

text

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3 60 61 DOCKET NUVBER ti8 09 EVENT DATE 74 75 REPORT DATE 80 EVENT DE5CRIPTION AND PROBA8LE CONSEQUENCES h lo121 lDuring plant operation while doing a weekly performance of control rod operability l

[ o 13 j l check, PT 14.1, it was discovered that rod 26-11 did not have RTGB position indication l lo l4 ] lat position "47."

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