LER-1981-044, /03L-0:on 810727,decay Heat Pump 1-1 Would Not Start.Caused by Improperly Handled Fuse Cartridge Causing Cartridge plug-in to Be bent.Plug-in Straightened to Proper Alignment |
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| 3461981044R03 - NRC Website |
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TOIJ:Da CD180" COMPA"Y DAV I S-id :SS!: ';l'Ci.!:A!: PC'.?l::t STAT 10S UNIT ONE SUI'Pl F:. ; FA!. I N POR :ATIO" ! O!! tr NP-33 -3 l-%
DATI: OF 1.VE!: f: July 27. 1981 FAC l f.1 TY :
Dav in-Ib";se Un it 1 iDFTliF! CATION M OMTFE::CL.
Decay !! eat (D!!) Pomp l-1 f ai1ed to ut art durlog a surveiilance test procedure Comlir ion s Prior to Occurrence:
The unit was in Mode 1 with Power (!TJT) = 2763 and 1.oa d (Gros > lNE) 923 D. wriet ion of Occurrence: On July 27, 1981 at 1005 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.824025e-4 months <br />, a control roen operator atter-ted to start D:1 Punp 1-1 for Surveillance Test NT 5051.10.
The pump did not start, and the eleetticians were called to inven t i p,a t e.
In the process of t rouble-l shooting, it can deternined that no control power van available to the breaker.
Further voltane checi.s nhered the loss of voltage was at the control power fuse
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blue:
A visucil inspection revcaJed a bent plug-in on the removable fuse cartridce.
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';he app! 1 cabl e Technical Specification 3.5.2 requires bot h low pressore injection /
t Dl! pumps to be operable in " ode 1.
Therefore, the stat. ion did cnter into an action statement.
The pump V:n returned to service within the action Statc9ent tire ] IrJ i t,
thereforc no url paver redoetion was regnited.
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_D_e s_.i r na " i on o f A n na r en t Caune of Occurrence: Tlie cause o f t he DH Pmp 1-1 f a il i ng t o start can be attributed to personnel error in that the failed compa..nt was improperly j
1 handled durinp nome ptevious operation causing the removable fuse cartridge,1ug-in to I
be bent.
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An tivsis of occurrence: There was no danner to the health and safety of the pui>1ic
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l or to utation personnel. Dil Pump 1-2 was operable dut ing this titre.
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Corrective Action
The removable fune cartridge plug-in was straightened t o be in i
proper aligr.nenL with the fuse suitch block under I-iaintenance Work Order 81-2925.
The breaker car tested utisfactortl'/ and returned to service. When available, a l
j new fune cartridge ulil be installed under Malatenance Uork Order 81-2926 Inspec-tion of ot her breaker enbieles tan conducted, and it ucs determined that the prob-lems were not repetitiv - in nature.
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Two previoua reported occurrenc;" of the DH pump failing to start I
railure pat a:
l wete reported in Licens e Event Re,) orts NP-33-78-13 (78-011) and HP-33-81-03 l
I (S1-03).
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LER #81-044 k
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| 05000346/LER-1981-001, Forwards LER 81-001/01X-1 | Forwards LER 81-001/01X-1 | | | 05000346/LER-1981-001-01, /01X-1:on 810107,discovered Contractor Personnel on 801204 Disassembled Restraints Other than Those Requested & Failed to Perform Reassembly in Timely Manner. Caused by Inadequate Procedural Control | /01X-1:on 810107,discovered Contractor Personnel on 801204 Disassembled Restraints Other than Those Requested & Failed to Perform Reassembly in Timely Manner. Caused by Inadequate Procedural Control | | | 05000346/LER-1981-002-03, /03L-0:on 810102,reactor Coolant Pump 1-2 Was Shutdown Due to High Seal Return Temp & Deteriorating Seal Staging & on 810106,pump 2-1 Was Shutdown for Deteriorating Seal Staging.Caused by Seal Degradation.Seals Replaced | /03L-0:on 810102,reactor Coolant Pump 1-2 Was Shutdown Due to High Seal Return Temp & Deteriorating Seal Staging & on 810106,pump 2-1 Was Shutdown for Deteriorating Seal Staging.Caused by Seal Degradation.Seals Replaced | | | 05000346/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000346/LER-1981-003-03, /03L-0:on 810106,breaker HX02B Tripped, de-energizing Bus B Which Reduced Electrical Distribution Less than Tech Specs Required.Caused by Personnel Error. Breakers Restored.Operators Counselled Re Attentiveness | /03L-0:on 810106,breaker HX02B Tripped, de-energizing Bus B Which Reduced Electrical Distribution Less than Tech Specs Required.Caused by Personnel Error. Breakers Restored.Operators Counselled Re Attentiveness | | | 05000346/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000346/LER-1981-004, Forwards LER 81-004/03X-1 | Forwards LER 81-004/03X-1 | | | 05000346/LER-1981-005-03, /03L-0:on 810114,RCS Chloride Concentration Exceeded Tech Spec Limit.Caused by Use of Spotcheck in Cleaning Reactor Coolant Pump Seal Cavities.Instructions Issued for Use of Solvents in RCS | /03L-0:on 810114,RCS Chloride Concentration Exceeded Tech Spec Limit.Caused by Use of Spotcheck in Cleaning Reactor Coolant Pump Seal Cavities.Instructions Issued for Use of Solvents in RCS | | | 05000346/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000346/LER-1981-006-03, /03L-0:on 810119,power Lost to Safety Features Actuation Sys Channel 1 Cabinet.Caused by Blown Supply Fuse from Panel Y-1 Due to Procedure Deficiency.Fuse Replaced & Procedure Modified | /03L-0:on 810119,power Lost to Safety Features Actuation Sys Channel 1 Cabinet.Caused by Blown Supply Fuse from Panel Y-1 Due to Procedure Deficiency.Fuse Replaced & Procedure Modified | | | 05000346/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000346/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000346/LER-1981-007-03, /03L-0:on 810122,door 306 Found Partially Open,So That Spent Fuel Pool Emergency Ventilation Sys Could Not Have Maintained Area at Correct Pressure.Caused by Maladjusted Door Closure.Maint Work Order Issued | /03L-0:on 810122,door 306 Found Partially Open,So That Spent Fuel Pool Emergency Ventilation Sys Could Not Have Maintained Area at Correct Pressure.Caused by Maladjusted Door Closure.Maint Work Order Issued | | | 05000346/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000346/LER-1981-008-03, /03L-0:on 810127,345 Kv Switchyard Bus K Tripped & Locked out,de-energizing Startup Transformer 02.Caused by Action from Directional Ground Current Relay & Charred Phase Lightning Arrestor C on Startup Transformer | /03L-0:on 810127,345 Kv Switchyard Bus K Tripped & Locked out,de-energizing Startup Transformer 02.Caused by Action from Directional Ground Current Relay & Charred Phase Lightning Arrestor C on Startup Transformer | | | 05000346/LER-1981-009-03, /03L-0:on 810128,diesel Generator 1-2 Could Not Be Started W/Left Side Set of Air Start Motors During Diesel Generator Surveillance Test 5081.01.Caused by Failure of One Air Start Motor Due to Broken Solenoid Drive Shaft | /03L-0:on 810128,diesel Generator 1-2 Could Not Be Started W/Left Side Set of Air Start Motors During Diesel Generator Surveillance Test 5081.01.Caused by Failure of One Air Start Motor Due to Broken Solenoid Drive Shaft | | | 05000346/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000346/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000346/LER-1981-010-03, /03L-0:on 810202,MSIV Bypass Valve Ms 100 a Failed to Close.Probably Caused by Component Failure.Actuator Spring Adjusted to Increase Tension Until Valve Would Close | /03L-0:on 810202,MSIV Bypass Valve Ms 100 a Failed to Close.Probably Caused by Component Failure.Actuator Spring Adjusted to Increase Tension Until Valve Would Close | | | 05000346/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000346/LER-1981-011-03, /03L-0:on 810205,post-accident Monitoring Instrument HPI Flow 1-2 Was Declared Inoperable.Caused by Bad Current Buffer.Current Buffer Was Repaired,Recalibr & Reinstalled.Hpi Flow 1-2 Was Returned to Operable Status | /03L-0:on 810205,post-accident Monitoring Instrument HPI Flow 1-2 Was Declared Inoperable.Caused by Bad Current Buffer.Current Buffer Was Repaired,Recalibr & Reinstalled.Hpi Flow 1-2 Was Returned to Operable Status | | | 05000346/LER-1981-012-03, /03L-0:on 810212,control Rod 1-3 Absolute Position Indication Declared Inoperable Due to Fluctuating Signals Causing Asymmetric Rod Alarms.Exact Cause Undetermined,But Absolute Position Indication Leads Picking Up Noise | /03L-0:on 810212,control Rod 1-3 Absolute Position Indication Declared Inoperable Due to Fluctuating Signals Causing Asymmetric Rod Alarms.Exact Cause Undetermined,But Absolute Position Indication Leads Picking Up Noise | | | 05000346/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000346/LER-1981-013-03, /03L-0:on 810218,control Room Normal Ventilation Dampers Tripped Shut Resulting in No Power Available to Chlorine Detector 1 Above Control Room or in Block House. Caused by Failure of 10 Amp Fuse of Circuit Y111 | /03L-0:on 810218,control Room Normal Ventilation Dampers Tripped Shut Resulting in No Power Available to Chlorine Detector 1 Above Control Room or in Block House. Caused by Failure of 10 Amp Fuse of Circuit Y111 | | | 05000346/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000346/LER-1981-014-03, /03X-1:on 810226,decay Heat Valve 64 Would Not Open During Testable ECCS Valves Quarterly Test.Caused by Loose Set Rod Bushing,Allowing Gear Box Set Rod to Move Which Unlocked Limit Switches from Adjusted Position | /03X-1:on 810226,decay Heat Valve 64 Would Not Open During Testable ECCS Valves Quarterly Test.Caused by Loose Set Rod Bushing,Allowing Gear Box Set Rod to Move Which Unlocked Limit Switches from Adjusted Position | | | 05000346/LER-1981-014, Forwards LER 81-014/03X-1 | Forwards LER 81-014/03X-1 | | | 05000346/LER-1981-015-03, /03L-0:on 810227,access Door 107 Found Propped Open from ECCS 2 Pump Room 115 to Miscellaneous Waste Monitor Tank & Pump Room 114.Caused by Failure to Follow Posted Signs While Clearing Odor from Room | /03L-0:on 810227,access Door 107 Found Propped Open from ECCS 2 Pump Room 115 to Miscellaneous Waste Monitor Tank & Pump Room 114.Caused by Failure to Follow Posted Signs While Clearing Odor from Room | | | 05000346/LER-1981-015, Forwards LER 81-015/03L-0 | Forwards LER 81-015/03L-0 | | | 05000346/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000346/LER-1981-016-03, /03L-0:on 810308,dose Equivalent I-131 Level Exceeded Tech Spec Limit.Caused by Gas Leakage Through Fuel Cladding.Levels Monitored | /03L-0:on 810308,dose Equivalent I-131 Level Exceeded Tech Spec Limit.Caused by Gas Leakage Through Fuel Cladding.Levels Monitored | | | 05000346/LER-1981-017-03, /03L-0:on 810309,train 2 Hpi/Low Pressure Injection cross-connect Isolation Valve Dh 63 Would Not Open from Control Room During Quarterly Valve Surveillance Test 5051.13.Caused by Faulty Torque Switch in Valve Operator | /03L-0:on 810309,train 2 Hpi/Low Pressure Injection cross-connect Isolation Valve Dh 63 Would Not Open from Control Room During Quarterly Valve Surveillance Test 5051.13.Caused by Faulty Torque Switch in Valve Operator | | | 05000346/LER-1981-017, Forwards LER 81-017/03L-0 | Forwards LER 81-017/03L-0 | | | 05000346/LER-1981-018-03, /03L-0:on 810322 & 0401,chlorine Detector Ae 5358B Tripped.First Trip Probably Caused by Fouled Detector. Detector Cleaned.Detector & Circuit Board Replaced After Second Failure | /03L-0:on 810322 & 0401,chlorine Detector Ae 5358B Tripped.First Trip Probably Caused by Fouled Detector. Detector Cleaned.Detector & Circuit Board Replaced After Second Failure | | | 05000346/LER-1981-018, Forwards LER 81-018/03L-0 | Forwards LER 81-018/03L-0 | | | 05000346/LER-1981-019-03, /03L-0:on 810323,fluctuating Signals W/Numerous Asymmetric Rod Alarms Received,Resulting in Control Rod 4-7 Absolute Position Indication Inoperability.Probably Caused by Electrical Penetration Module Deficiency | /03L-0:on 810323,fluctuating Signals W/Numerous Asymmetric Rod Alarms Received,Resulting in Control Rod 4-7 Absolute Position Indication Inoperability.Probably Caused by Electrical Penetration Module Deficiency | | | 05000346/LER-1981-019, Forwards LER 81-019/03L-0 | Forwards LER 81-019/03L-0 | | | 05000346/LER-1981-020-03, /03L-0:on 810324,valve CV5011A,on Containment Air Sample Inlet Line to Hydrogen Analyzer,Would Not Stroke Closed W/Monitor Operator.Caused by Badly Worn Tripper in Motor Operator.Tripper Levers Replaced | /03L-0:on 810324,valve CV5011A,on Containment Air Sample Inlet Line to Hydrogen Analyzer,Would Not Stroke Closed W/Monitor Operator.Caused by Badly Worn Tripper in Motor Operator.Tripper Levers Replaced | | | 05000346/LER-1981-020, Forwards LER 81-020/03L-0 | Forwards LER 81-020/03L-0 | | | 05000346/LER-1981-021-03, /03L-0:on 810401,half Trip Occurred from Steam & Feedwater Rupture Control Sys Channel 1 Low Steam Generator Level Trip.Caused by Power Supply Failure.Power Supply Replaced Per Work Order on 810402 | /03L-0:on 810401,half Trip Occurred from Steam & Feedwater Rupture Control Sys Channel 1 Low Steam Generator Level Trip.Caused by Power Supply Failure.Power Supply Replaced Per Work Order on 810402 | | | 05000346/LER-1981-021, Forwards LER 81-021/03L-0 | Forwards LER 81-021/03L-0 | | | 05000346/LER-1981-022, Forwards LER 81-022/03L-0 | Forwards LER 81-022/03L-0 | | | 05000346/LER-1981-022-03, /03L-0:on 810316,NRC Site Inspector Reported Finding Four 0.5-inch Holes Through Control Room Equipment Room East Fire Wall.On 810403,two Holes Found in Wall of Room 427B.Caused by Personnel Error | /03L-0:on 810316,NRC Site Inspector Reported Finding Four 0.5-inch Holes Through Control Room Equipment Room East Fire Wall.On 810403,two Holes Found in Wall of Room 427B.Caused by Personnel Error | | | 05000346/LER-1981-023-03, /03L-1:on 810403,decay Heat Cooler Outlet Valve CC1467 Stroked Closed During Component Cooling Water Monthly Test & Would Not Reopen.Caused by Excessive Wear on Actuator Due to Design Deficiency.Actuator Rebuilt | /03L-1:on 810403,decay Heat Cooler Outlet Valve CC1467 Stroked Closed During Component Cooling Water Monthly Test & Would Not Reopen.Caused by Excessive Wear on Actuator Due to Design Deficiency.Actuator Rebuilt | | | 05000346/LER-1981-023, Forwards LER 81-023/03L-1 | Forwards LER 81-023/03L-1 | | | 05000346/LER-1981-024, Forwards LER 81-024/03L-0 | Forwards LER 81-024/03L-0 | | | 05000346/LER-1981-024-03, /03L-0:on 810418,bus J Was Rapidly Taken Out of Svc W/O Providing for Alternate Power Supply for Decay Heat Pump 1-1.Caused by Personnel Error.Procedure Modified & Operator Informed of Mods | /03L-0:on 810418,bus J Was Rapidly Taken Out of Svc W/O Providing for Alternate Power Supply for Decay Heat Pump 1-1.Caused by Personnel Error.Procedure Modified & Operator Informed of Mods | | | 05000346/LER-1981-025, Forwards LER 81-025/03L-0 | Forwards LER 81-025/03L-0 | | | 05000346/LER-1981-025-03, /03L-0:on 810423,during Review of Safety Tagging Log,Unit Entered Mode 4 W/O Required Two Makeup Pumps Operable.Caused by Personnel Error.Pumps Restored to Operation.Personnel Reinstructed in Procedures | /03L-0:on 810423,during Review of Safety Tagging Log,Unit Entered Mode 4 W/O Required Two Makeup Pumps Operable.Caused by Personnel Error.Pumps Restored to Operation.Personnel Reinstructed in Procedures | | | 05000346/LER-1981-026-03, /03L-0:on 810428,reactor Protection Sys Channel 1 Tripped on Flux/Delta Flux/Flow.Caused by Failure of Flow Differential Pressure Transmitter Primary Power Transformer Shorting to Ground.New Amplifier Installed & Calibr | /03L-0:on 810428,reactor Protection Sys Channel 1 Tripped on Flux/Delta Flux/Flow.Caused by Failure of Flow Differential Pressure Transmitter Primary Power Transformer Shorting to Ground.New Amplifier Installed & Calibr | |
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