ML20010D191

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Monthly Operating Rept for Jul 1981
ML20010D191
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 08/01/1981
From: Hairston W
ALABAMA POWER CO.
To:
Shared Package
ML20010D189 List:
References
NUDOCS 8108240090
Download: ML20010D191 (5)


Text

. _ _ _ _

i I

OPERATING DATA REPORT DOCKET NO. 50-36'.

DATE 3 /1/ M COMPLETED BY k*/; MWston, III 1

TELEF110NE (205)699-5156

]_.

OPERATING STATUS

1. Unit Name:

Joseph M. Farley - Unit 2 Notes: : 1) Joseph M. Farley

2. Reporting Period:

July, 1981 Nuclear Plant Unit 2 vent

3. Licensed Thermal Power (MWr):

2652 into commercial operation on j

4. Nameplate Rating (Gross MWe):

860 July 30, 1981.

5. Design Electrical Hating (Net MWe):

829

6. Maximum Dependable Capacity (Gross MWe):

860*

7. Maximum Dependable Capacity (Net MWe):

829*

8. If Changes Occur in Capacity Ratings (items Nun'ber 3 Through 7) Since Last Report. Give Reasons:

N/A

9. Power Level To which Restricted.lf Any(Net MWe):

N/A

10. Reasons For Restrictions,If Any:

N/A k

This Month Yr.-to-Date Cu'mulatise

!I. Ilours In Reporting Period 744 1,610.2 1 610.2

12. Number OfIlours Reactor Was Critical 426.7 1,108.2 1,a 3.2
13. Reactor Reserve Shutdown llours 317.3 528.8 528.8 14, flours Generator On-Line 398.7 759.2 759.2
15. Unit Rewne Shutdown ilours 0

0 0

16. Gross Thermal Energy Generated (MWH) 839,252.7 1,257,899.4 1,257,899.4
17. Gross Electrical Energy Generated (MWil) 264.338 ___,_,

359,618 359,618

18. Net Electrical Energy Generated (MWH) 239,070 311,226 311,226
    • 19. Unit Senice Factor 100.0 100.0 100.0
    • 20. Unit Availability Factor 100.0 100.0 100.0
    • 21. Unit Capacity Factor IUsing MDC Net) 41 ?

01.2 91,2

    • 22. Unit Capacity Factor (Using DER Net) 91.2 91.2 91.2
    • 23. Unit Forced Outage Rate 00.0 00.0 00.0
24. Shutdowns Scheduled Oier Next 6 Months (Type.Date.and Duration of Each):

N/A

25. If Shot le..n At End Of Report Period. Estimated Date of Startup: N/A'
26. Units in.est Status (Prior to Commercial Operation):

Forecast Achiesed f310:240090 810817 PDR ADOCK 05000364 NITI \\ L CRITICALITY

'i /6 /8_1 3/8/81 R

PDR INITIAL ELECTRICITY 5/24/81 5/25/81 COMMERCI AL OPER ATION 8/1/81 7!30/81

  • The Nameplate Rating / Design Electrical. Rating will be used for the Maxinus Dependable Capacity until an accurate value can be determined from operating

.i experience.

em7:

    • Items calculated from July 30, 1981, date of commercial operation.

_ _ _, _., - ~

e AY. ERAGE DAILY UNITPOWER LEVEL

[

  • ,s-DOCKETNO. 50-364 h

2 1

UNIT DATE 8/l/81 COMPLETED BY W.G.Hairston,III

/

TELEPHONE. (205)899-5156 MONTH July, 1981 DAY AVERAGE DAILY POWER LEVEL

  • DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe. Net) 788 -

g, 37 2

-O' 539 jg gg.

3

-0 C

4 _ !.:

20 228 5 -

  • ~

21 6

92 307 g

7 590- -

23 m,

. (-.(

g 580 ~

^

.j, 4

9 574

~-

25 -

10 579 -

.,j, Ig 350 183

'f"

~

\\

l 12 335

.. f,,s 442-c-

637 592 j3 3

14 641 757 30

~

756 IS 537

33 712 16

>+"

INSTRUCTIONS

~

~

On this formst.!ist the ave.sge daily unit power levelin MWe-Net for each day in the reporting mon:5. Compute to the nestest whole megsw it.

J

'.e (9(77) i l

t

i

' % (-

A A.

A UNITS!!UTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-364 UNIT NA%fE J.M.Farlev-Unit 2 DATE 8/1/81 REPORT.\\f 0NTI! Julv. 1981 CO\\tPLETED BY E C ue stm. TII i

IELEPl!ONE (2051899-5156 1

1

.3 =c

=

en 5

.E _e 75'4 Licensee

=.r c%

Cause & Corrective i

No.

Date g

3g g

_g g 5 Event u?

o E-3 Action to

$E E

j5 RCPort =

rN G U

Prevent Recurrence C

4 Continued Phase III Testing at vari-ous reactor power levels.

013 810701 S

134.9 H

1 N/A CI HTEXCH Unit outage centinued from 6/22/81 1

to repair a tube leak on S/G 2A.

014 810711 F

8.8 A

3 N/A HH VALVEX Reactor Trip-Turbine Trip on S/G 2B High-High icyc1 due to S/G 2B feed regulating valve nalfunction during Phase III 50% Load Rejection Test.

015 810714 F

6.9 H

3 N/A HA ZZZZZZ Reactor Trip-Turbine Trip due to high.

main generator hydrogen temperature.

3 015 810718 S

66.3 B

1 N/A HA ZZZZZZ Reactor Trip-Turbine Trip due to l

Phase III Test, Manual Turbine Trip from 100% power.

Commenced outage to recalibrate all steam flow / feed flov transnitter s and repair transmitter vent..in e s.

I 2

3 4

F: Forced Reason:

Method:

Exhibit G-Instructions S: Scheduled A. Equipment Failure (Explain) 141anual for Pseparation of Data II. Maintenance or Test 2-M in ual Scram.

Entry Sheets for Licensee C-Refueling 3 Automatic Scram.

Event Report (LER) File (NUREG-D-Regulatory Restriction

-t-Other (Esplain) 0161)

E-Operator Train ng & License Examination i

F Administrative 5

G O vrational Error (Explain) i (9/77)

Il-OLher (Explain)

Exhibit I Same Source

O A.g A

z DOCKET NO. 50-364 UNIT S!!UIDOWNS AND POWER REDUCI10NS UNIT NAME J.M,Faricy-Unit 2 DATE 8/1/8L REPORT MONTil _ July, 1981 COMPLETED BY W.G.llairston, III TELEPifONE (205) 899-5156 i

~

T 5"

=

c.

3=

.E e E

- >.5 M Licensee g%

Cause & Correstive c

8 ".

Date g

g g

jg5 Event u?

Action to c$ E 5

j di g Report u N0 Pr* vent Recurrence d

017 810722 F

4.8 G

3 N/A UA INSTRU Reactor Trip-Turbine Trip due to shorting of test leads in parallel with manual Turbine trip switch.

018 810722 S

113.7 B

1 N/A HA ZZZZZZ Reactor Trip-Turbine Trip as part of Phase III testing program. Commenced

=a!.ntenance outage.

019 810727 F

0.6 A

4 N/A HH INSTRU Turbine Trip due to S/G 2A High-High level. Main feed pump contr.1 prob-lems.

020 810727 F

0.8 A

4 N/A HH INSTRU Turbine Trip due to S/G 2A High-High level. Main feed pu=p control prob-lems.

l i

2 3

4 F: Forced Reason:

Method:

Exhibit G. Instructions 5: Scheduled A-Equipment Failure (Explain)

I-Manual for Preparation of Data B. Maintenance of Test 2-Manual Scram.

Entry Sheets for Licenace C Refueling 3-Automatic Scram.

Event Report (LER) File (NURl!G.

D Regulatory Restriction 4-Other (Explain) 0161)

I!-Operator Training & l.iceme lixamination F-Admini:,t rative 5

G-Operational lis tor (IIxplain)

Exhibit I Same Source (9/77)

Il-Other (Explain)

i i

~

O O.

i UNIT SIIUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-364 UNIT NAME J.M.Farley-Unit 2 DATE - 8/1/81 REPORTMONTH ulv. 1981 COMPLETED BY W.C.Mairsten. III J

TELEPitONE (205)899-515o l

3 e,

.5 -x =

e*

.=E r

,.s ~4 Licensee g *r.

Cause & Corr:ctive c

o o

No.

Date g

3g i;

jg5 Event u2

$.?

Action to H

g$ ~

j di g Report :

viC

]O Prevent Recurrence 6

021 310728 F

2.6 B

3 N/A HH INSTRJ Reactor Trip-Turbine Trip due to S/G 2A Low -Low level while perfom-ing Phase III 100% Pcwer Load Swing Test.

022 310728 F

5.9 B

3 N/A HH INSTRU Reactor Trip-Turbine Trip due to Low-Low L/G 1evels in all S/G's while perfoming Phase III 50%

Load Rejection Test.

f

  • Unit 2 declared com::tercial at 1

0001 on July 30, 1981.

l l

5 I

2 3

l I;; l'orced Reamn:

Methoti:

Exhitut G Inst:uctions S: Stheduled A Inguipn.cnt l'ailure (Explain) l4tannal for Pieparation of Daia ll41aintenance of Test 241 annal Sesam.

Entsy Shetts foi I.ieemee C Refueling 3 Automatic Scram.

Event Report (f.ER) liite (NUREG-D Regulatory Restriction 4-Other (Explain) 0161)

I. Operatur Tsaining & !.icense Examination F-Administ rative 5

G-O srational lit tor (Explain)

Exhibit 1 Same Source i

(')/77)

Il-Other (Expbin) q I