05000316/LER-1981-031-03, /03L-0:on 810711,during Startup,Average Temp Decreased Below Tech Spec Requirement.Caused by Using Excessive Feed Rate Which Created Larger Heat Sink & Lower Temp for Rcs.Feed Rate Reduced.Control Rods Withdrawn

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/03L-0:on 810711,during Startup,Average Temp Decreased Below Tech Spec Requirement.Caused by Using Excessive Feed Rate Which Created Larger Heat Sink & Lower Temp for Rcs.Feed Rate Reduced.Control Rods Withdrawn
ML20010C230
Person / Time
Site: Cook 
Issue date: 08/10/1981
From: Draper D
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20010C229 List:
References
LER-81-031-03L, LER-81-31-3L, NUDOCS 8108190266
Download: ML20010C230 (2)


LER-1981-031, /03L-0:on 810711,during Startup,Average Temp Decreased Below Tech Spec Requirement.Caused by Using Excessive Feed Rate Which Created Larger Heat Sink & Lower Temp for Rcs.Feed Rate Reduced.Control Rods Withdrawn
Event date:
Report date:
3161981031R03 - NRC Website

text

U. S. NUCLE AR REGULATORY COMMISSION NRC FORP.) 366 (7'7 7 )

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!o I2 I l DURING A STARTUP WITH THE REACTOR CRITICAL, TAVG DECREASED BELOW 541 DEGREES. THIS ISI Io i3i l CONTRARY TO T.S. 3.1.1.5.

TAVG WAS INCREASED AB0VE 541 WITHIN APPR0XIMATELY 1 MIN.

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l i i il l TEMPERATURE DECREASE BUT THIS DID NOT PREVENT REACHING THE T.S. MINIftUM. ALL LICENSEDI ii ;.,1 OPERATORS WILL BE REQUIRED TO REVIEU THIS REPORT TO MAKE THEM AWARE OF THE CAUSE-l 8'

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