05000324/LER-1981-052-03, /03L-0:on 810609,reactor Recirculation Pump Motor Generator 2A Tripped During Unit Load Changes.Cause Unknown. Dirty Electrical Contacts Found in Field Breaker Closure Circuitry Cleaned

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/03L-0:on 810609,reactor Recirculation Pump Motor Generator 2A Tripped During Unit Load Changes.Cause Unknown. Dirty Electrical Contacts Found in Field Breaker Closure Circuitry Cleaned
ML20009G177
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 06/29/1981
From: Pastva M
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009G167 List:
References
LER-81-052-03L-01, LER-81-52-3L-1, NUDOCS 8108030398
Download: ML20009G177 (1)


LER-1981-052, /03L-0:on 810609,reactor Recirculation Pump Motor Generator 2A Tripped During Unit Load Changes.Cause Unknown. Dirty Electrical Contacts Found in Field Breaker Closure Circuitry Cleaned
Event date:
Report date:
3241981052R03 - NRC Website

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LICENSEE EVENT REPORT o

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8 60 61 DOCKET NUMBER 68 69 EVENT DATE 14 75 REPCAT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10121 l While performing unit load changes af ter a normal reactor startup. 2A Reactor Recir-I o a i culation Pump motor generator (MG) tripped.

Following a reset of the MG trip signals,l l o 141 l the pump could not be started because the MG set generator field breaker would not l

[TTT1 I close.

2A Reactor Recirculation Pump was declared inoperable in accordance with l

0 6 l technical specifications. This event did not affect the health and safety of the 1

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I I o Ia l i Technical Specifications 3.4.1.1. 6.9.1.9B l

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CODE TYPE N O.

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33 34 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i 11 IOII A visual inspection of the MG field win 9nes and an electrical check of the MG trio I

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y l circuitry did not reveal the cause of the,7 trip.

Dirty electrical contacts were j

i 2 i found in the field breaker closur? circuitry d ich prevented a pump restart but l

l which would not have caused the initial trip. Tee contacts were cleaned and on l

3 gl 6-10-81 the MG was started and the pump vas returned to operation.

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M. J. Pastva, Jr.

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NAME OF PREPARER

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