LER-1981-027, /03L-0:on 810604,during Mod Outage,Switch 2-PdIS-75-56 Was Found Outside Tech Spec Limits.Caused by Setpoint Drift of Barton Model 288 D/P Switch.Switch Recalibr |
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la t-J l During a mndification outage, while performing core spray sparger to RPV d/p g,3 g ] I 4.2.B-24), switch 2-PdIS-75-56 was found at 1.5 psid.
T.S. table 3.2.B 1
limit is 2 -r 0.4 psid. There was no danger to the health or safety of the i
F:E]t ll'l.3 LP"_b1ic. Redundant switch 2-pdIS-75-28 was available and operable. Previous
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[ijT] [The Barton model 288 d/o switeb,etpoint had drifted.
Th_e__ switch was 1
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Te.nne:,see Valley Authorit y BF 15. 2 6: owns Fer ry Nucleai Plant C/01/31 l.El: SUPPL,F. MEN l' Al. IN H >l:M ATIOn' hl HO-LO. 260_ _ / 81027 T.. hnical Specifit.itein inco!ved Table _ 3. 2.B _._
Hnported Unde:r Technica! Sp cification 6.7.2.b (1)
- na t e due NRc._.7./4/81 _
Date of O< currr.nce 6/4/81 Time of occut rena 0930.,_ Unit __.,2_,.
'derJificar, ion and Ir:.scriptwn of ()cedrrence Core sprav soarger to PPV d/p switch 2-PdIS-75-56 was found at 1.5 osid (AF decreasing). The T.S. table 3.2.B limit is 2 + 0.4 psid.
(' >ntiit tons Prior 'o Occur; ence trni t 1 - refueling outage.
tin i t 2 - modification outage.
Unit 3 - at 100%.
Acts. n
.pc< >ficii in t hi. Technical Specification Surveillance Requirement:, met
' in Ia inop -ral le "tpapi:n ut.
Describe,
None Apparent Caupe gf Orcuri;ence' Setnoint drift.
Anaivsis of ()ccurrence There was no danger to the health or safety of the pub 1!.c, no release of activity, no damage to the plant or equipment, and no resulting significant chain or events.
( on. ci s ce A c t ic in :
The Barton model 288 d/p switch was recalibrated and successfully tested for repeatability. This is considered a random event and no recurrence control is required.
Failure Data:
BFRn-50-259/8087, 8101 Hetention :
PerWd. Lifetime; Responsibility - Document Control Supervisor
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T H evision.
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