05000366/LER-1981-053-03, /03L-0:on 810611,turbine First State Pressure Permissive Switches Found Out of Tolerance While Performing Barksdale Pressure Switch Calibr.Probably Caused by Setpoint Drift.Switches Recalibr

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/03L-0:on 810611,turbine First State Pressure Permissive Switches Found Out of Tolerance While Performing Barksdale Pressure Switch Calibr.Probably Caused by Setpoint Drift.Switches Recalibr
ML20009F540
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 07/02/1981
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009F537 List:
References
LER-81-053-03L, LER-81-53-3L, NUDOCS 8107310283
Download: ML20009F540 (2)


LER-1981-053, /03L-0:on 810611,turbine First State Pressure Permissive Switches Found Out of Tolerance While Performing Barksdale Pressure Switch Calibr.Probably Caused by Setpoint Drift.Switches Recalibr
Event date:
Report date:
3661981053R03 - NRC Website

text

U. S. NUCLEAR REGULATO?.Y COMMif,SION NRC FORM 366 (7 77)

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8 60 61 OOCKET NUMBER 68 69 EVENT OATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PnOBABLE CONSEQUENCES h ITTTI L With the plant in steady state operation at 1927 MWt and while performina I

HNP-2-5279, Barksdale Pressure Switch Calibration, 2C71-N003A,B and C, l

iO i3i l I o 141 l Turbine First State Pressure, Permissive Switches, were found out of tol-l lO isi l erance.

Tech Specs Table 3.3.1-1, Item 9, requires actuation at 160 psig l

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+12 psig head correction.

Plant operation nor the health and safety of I

l0l7j I the public was affected.

This is a non-repetitive event.

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40 43 42 43 44 47 CAUSE DESCRIPTION AND COARECTIVE ACTIONS h l i 10 l l The cause of this event has been attributed to setonint drift.

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I1 liI I switches were recalibrated oer HNP-2-5279 Barksdale Pressure Switch I

I li12i 1 Calibration, and functionally tested successfully oer HNP-2-3010.

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ml Turbine First Staae Pressure Permi,ssive Functional Test and Calibration.

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e LER No.:

50-366/1981-053 Licensee:

Georgia Power Company Facility:

Edwin I. Hatch Docket No. :

50-366

Narrative

Report for LER 50-366/1981-053 On June 11, 1981, while the plant was in steady state operation at 1927 MWt and while performing HNP-2-5279, Barksdale Pressure Switch Calibration, 2C71-N003 A,B and C, Turbine First Stage Pressure Permissive Switches, were found out of tolerance.

Switch 2C71-N003D was found to be operable and actuating within expected tolerance.

Tech Specs Table 3.3.1-1, Item 9, requires actuation at 160 psig + 12 psig head correction.

Plant operation nor the health and safety of the public was affected by this event. This is a non-repetitive event.

The cause of this event has been attributed to setpoint drift.. The switches was recalibrated per HNP-2-5279, Barksdale Pressure Switch Calibration, and functionally tested successfully per HNP-2-3010, Turbine First Stage Pressure Permissive Functional Test and Calibration, and returned to service.

Unit I uses the same type switch -for this application.

A generic review revealed no inherent problems.

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