ML20009E922

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LER 81-058/03L-0:on 810622,during steady-state Operation at 2,194 Mw,Reactor Bldg to Torus Vacuum Breaker Isolation Valve 2T48-F310 Failed Open.Cause Attributed to Torus Differential Pressure Switch Setpoint Drift.Switch Recalibr
ML20009E922
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 07/15/1981
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009E910 List:
References
LER-81-058-03L, LER-81-58-3L, NUDOCS 8107280546
Download: ML20009E922 (2)


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NRC FOIM 366 U. Lk MELGA] RTGULATE.Y COMMIO31oM (7-77)

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EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h IO I2I I While the olant was in steadv state coeration at 7194 MWt. Reactnr Ruild- 1 10i3 1 ing to Torus Vacuum Breaker Isolation Valve. 2T48-F310. failed open. I IO I4 l l Tech Specs 3.6.3 reauires that Primary Containment Isolation Valves be l lo isi l operable. Redundant Reactor Building to Torus Vacuum Breaker Isolation l 10isl l Valve, 2T48-F311 was operable. Neither olant ooeration nor oublic health 1 10171I and safety were affected. This is a repetitive event as reported on l l 0 ia i l Reportable Occurrence Report 50 ^66/1981-051. I DE CODE SLBCO E COMPONENT CODE SUBCODE SU DE lTJ il l S l Dl @ [E_j @ (_E_j @ l I l N l S l T l R l U l@ l_Sj @ l Z l @

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44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS lilOIl The cause of the event has been attributed to Reactor Buildino to Torus I i i I Differential Pressure Switch. 2T48-N210_ setonint drift. The switch wac I yl recalibrated as per HNP-2-5240. Static "0" Rino Pressure Switch Calibra- I Li_,L_j l tion, and functionally tested successfully. A new switch has been ordered I li14l l and will be installed when received. I 7 8 9 80 SA S  % POWER OTHER STATUS DIS O RY DISCOVERY DESCRIPTION W lEl@

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LER No.: 50-366/1981-058 Licensee: Georgia Power Company Facility: Edwin I. Hatch Docket No. : 50-366 Narrative Report for LER 50-366/1981-058.

On June 22, 1981, while the plant was in steady state operation at 2194 MWt, Reactor Building to Torus Vacuum Breaker Isolation Valve, 2T48-F310, failed open. Tech Specs 3.6.3 requires that primary containment isolation valves be operable. Redundant Reactor Building to Torus Vacuum Breaker Isolation Valve, 2T48-F311, was operable. Neither plant operation nor public health and safety were affected. This is a repetitive event as reported on Reportable Occurrence Report No. 50-366/1981-051.

The cause of the event has been attributed to Reactor Building to Torus Differential Pressure Switch, 2T48-N210, setpoint drift. The switch was found to actuate at 5" water column and 'it should be 14" water column. The switch was recalibrated as per HNP-2-5240, Static "0" Ring Pressure Switch Calibration, and functionally tested successfully. The switch was returned to service. A new switch has been ordered and will be installed when received.

A generic review revealed no inherent problems with this type switch, i

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