05000334/LER-1981-062-03, /03L-0:on 810619,auxiliary Flow Path to Steam Generator 1A Was Isolated.Caused by Maint on Leaking Feed Flow Transmitter Instrument Line Penetration Into Auxiliary Feed Flow Header A.Piping Refabricated

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/03L-0:on 810619,auxiliary Flow Path to Steam Generator 1A Was Isolated.Caused by Maint on Leaking Feed Flow Transmitter Instrument Line Penetration Into Auxiliary Feed Flow Header A.Piping Refabricated
ML20009E873
Person / Time
Site: Beaver Valley
Issue date: 07/16/1981
From: Lacey W
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20009E868 List:
References
LER-81-062-03L, LER-81-62-3L, NUDOCS 8107280505
Download: ML20009E873 (2)


LER-1981-062, /03L-0:on 810619,auxiliary Flow Path to Steam Generator 1A Was Isolated.Caused by Maint on Leaking Feed Flow Transmitter Instrument Line Penetration Into Auxiliary Feed Flow Header A.Piping Refabricated
Event date:
Report date:
3341981062R03 - NRC Website

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EVENT DESC PTION A' O PROB A C NS *ENCES 121:1 l On 6/19/81 at 1654 hours0.0191 days <br />0.459 hours <br />0.00273 weeks <br />6.29347e-4 months <br /> with reactor power at 99%. the auxiliary flow nach I

to the 1A Steam Generator was isolated for the repair of a leaking feed flow l

g.3, 3, g gl transmitter instrument line penetration into the "A" aux feed flow header. Power l ml operation continued under the guidelines of Technical Specification 3.7.1.2.

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[TT:n l There were no safety implications and in the event of a safety injection or the l

lc l7 l l loss of normal station power there would have been slightly reduced auxiliary

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j:ta;l feed flow to the 1A Steam Generator due to the leak.

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l'I: 1 L threaded into the penetration then seal welded.

1A Steam Generator was restored and tested on 6/20/81 at 2124 hours0.0246 days <br />0.59 hours <br />0.00351 weeks <br />8.08182e-4 months <br />.

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A Attachment to LER 81-60/03L Beaver Valley Power Station Duquesne Light Company Docket No. 50-334 No further information is available or needed to satisfy the reporting requirement.

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