05000366/LER-1981-060-03, /03L-0:on 810622,inboard Reactor Water Cleanup Primary Containment Isolation Valve Found Open in Presence of Isolation Signal.Caused by Attempt to Electrically Close Valve After Backseating to Repair Packing Leak

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/03L-0:on 810622,inboard Reactor Water Cleanup Primary Containment Isolation Valve Found Open in Presence of Isolation Signal.Caused by Attempt to Electrically Close Valve After Backseating to Repair Packing Leak
ML20009E576
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 07/17/1981
From:
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009E555 List:
References
LER-81-060-03L, NUDOCS 8107280307
Download: ML20009E576 (2)


LER-1981-060, /03L-0:on 810622,inboard Reactor Water Cleanup Primary Containment Isolation Valve Found Open in Presence of Isolation Signal.Caused by Attempt to Electrically Close Valve After Backseating to Repair Packing Leak
Event date:
Report date:
3661981060R03 - NRC Website

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LICENSEE EVENT REPORT CONTROL SLOCK: l

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"5'C 60 61 OCCKET NLMSER 68 63 EVENT C ATE 74 75 AEPORT CATE 30 EVENT oEsCRIPTICN ANC pao 8ABLE CoNSECUENCEs h oi} l While the olant was in steadv state coeration at 2100 Wt. Inboard Reactor I

oi3; I Water C'.eanuo (RWCU) Primary Containment Isolation Valve, 2G31-F001,' was I

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found to be ocen in the cresence of an isolation sional on RWCu. ' out-I d idi L

oi3!I board Valve, 2G31-F004, was Closed and coerable and the inoperative I

i046l l Vdive was reDaired within four hours as recuired bv Tech Saecs 3.6.3.a.1, I

lai'i L so olant oceration was una ffected.

The health and safety of the oublic

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was una ffected.

This is a non-recetitive event.

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20 24 25 26 31 40 di 42 43 44 47 CAUSE OESCRIPTICN AND CCARECTIVE ACTICNS IiioIl The inocerable valve had been backseated to eoair a cackino leak andithe i

l l'it !l "close" torcue switch had ocened when an attentot had been made to elec-I li62l 1 trically close the' valve.

The "close" torcue switch was momentarily I

i i63t1 jumcered to move the valve stem from the 5ack seat.

The valve was then I

li64 11 oroven ooerable and returned to service.

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%PCvviR CTwER STATUS 1 C ERY OISCOVERY CESCRIPTICN N%

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'EP No.:

50-366/1981-060 Licensee:

Georgia Power Company Facility:

Plant E. I. Hatch Docket No. :

50-366 l

Narrative

Report

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for LER 50-366/1981-060 On June 22, 1981, Inboard Reactor Water Clean-up (RUCU) Primary Con-tainment Isolation Yalve, 2G31-F001, was found to be open in the presence of an RWCU Isolation Signal during a control board walkdown.

Cu ttoa rd Valve 2G31-F004 was closed and coerable, and the inoperative valve was repaired in four hours as required by Tech Specs 1.6.3.a. so olant operatinn was una f fec ted.

The heal th and sa fety of the out lic wa, una f fec ted.

The inoperable valve had been backsea ted to repair a packing leal and the "close" torque switch had opened when an attempt had been made to elec-trically cl'ose the valve.

The "close" ' torque switch was momentarily jumpered to move the valve stem from the back seat.

The valve was then proven operable and returned to service.

A g.eneric review found no other occurrences of this type ir. system 2G31 and few torque switch problems during the life of the plant.

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