ML20009D921

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Interim Deficiency Rept,Originally Reported on 801030,re Inadequate Nondestructive Exam of Spool Weld Buildup by Supplier.Vendor Has Completed Pipe Repairs.Indications Found to Be Harmless.Problem No Longer Deemed Reportable
ML20009D921
Person / Time
Site: Hope Creek  PSEG icon.png
Issue date: 07/14/1981
From: Martin T
Public Service Enterprise Group
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
10CFR-050.55E, 10CFR-50.55E, NUDOCS 8107240502
Download: ML20009D921 (2)


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i Thomas J. Martin Public Service Electric and Gas Company 80 Park Plaza Newark, N.J. 07101 201/4306316 Vice President Engirtaering and Construction July 14, 1981 mWLizSb Mr. Boyce H.

Grier, Director g

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U. S.

Nuclear Regulatory Commission e

"q Office of Inspection and Enforcement

,f' Region I J

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631: Park Avenue

.t King of Prussia, Pennsylvania 19406

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Dear Mr. Grier:

7 SPOOL WELD BUILDUP INSUFFICIENT EXAMINATION 10CFR50.55(e), POTENTIAL SIGNIFICANT DEFICIENCY NO. 1 AND.2 UNITS.

HOPE CREEK GENERATING STATION On October 30, 1980, a verbal report was made to Region I, Office of Inspection and Enforcement representative, Mr. J.

Mattia, advising of a potential significant item involving inadequate nondestructive examination of weld buildups by a 4

supplier of safety _ related pipe.

Supplemental information was suh ';ed to the NRC in writing on November 12, 1980, December 19, 1980, and March 4, 1981.

In addition, a detailed report of our investigation into this. matter was submitted on April 1, 1981, in final re-sponse to your Inspection Report 50-354/79-04.

That infor-mation is incorporated in this report by reference.

The l

content of the April 1, 1981, letter was also reviewed with i'

a representative of Region I on April 23, 1981; reference Inspection Report 50-354/81-05.

Bechtel Power Corporation has completed and evaluated the

.repa rs to the pipe spools identified in our April 1,

1981, i

' letter.

I The indications found by surface examination of the weld I

buildups ' on the two nuclear. Class 2 spools were eliminated bgy),77 E

by cosmetic grinding, without any encroachment on the minimum specified wall thickness.

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The indications found by radiography of the weld buildups on the ten nuclear Class 3 spools were eliminated by grinding, 3

.with subsequent weld repair to restore specified wall thick-ness.

All'of theselweld buildups were located on field ends and were ' surface examined by Dravo in accordance with their shop procedure.- -The surface examination performed by Dravo assured a weld quality consistent with that required by ASME "8107240502 810714 PDR ADOCK 05000354 -

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..Section III and Bechtel Specification P-201(Q) for the even-tual buttwald of the joint (buttwelds in 150-lb, nuclear Class 3 piping requires only a surface examination).

The indications found by the additional radiography con-sisted of porosity, slag, and lack of 0:sion.

The amount and severity of the indications have been evaluated to be such that had they remained undetected, would not have af-fected serviceability of the piping and, therefore, safe operation of the plant.

Therefore, we do not consider this problem to be a signif-icant deficiency, and we do not consider it reportable under 10CFR50.55(e).

Very truly yours,

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Office of Inspection & Enforcement Division of Reactor Construction Inspection Washington, D.C.

II.

E.

Morris Bechtel Power Corporation San Francisco, California NRC Resident Inspector llope Creek Generating Station 4

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