05000334/LER-1981-058-03, /03L-0:on 810610,refueling Water Storage Tank Level Indicator LI-QS-100A Failed Low.Caused by Failure of Force Motor within Low Loop Level Transmitter.Transmitter Repaired & Replaced on 810624

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/03L-0:on 810610,refueling Water Storage Tank Level Indicator LI-QS-100A Failed Low.Caused by Failure of Force Motor within Low Loop Level Transmitter.Transmitter Repaired & Replaced on 810624
ML20009D799
Person / Time
Site: Beaver Valley
Issue date: 07/10/1981
From: Lacey W
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20009D797 List:
References
LER-81-058-03L, LER-81-58-3L, NUDOCS 8107240359
Download: ML20009D799 (2)


LER-1981-058, /03L-0:on 810610,refueling Water Storage Tank Level Indicator LI-QS-100A Failed Low.Caused by Failure of Force Motor within Low Loop Level Transmitter.Transmitter Repaired & Replaced on 810624
Event date:
Report date:
3341981058R03 - NRC Website

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lotil EVENT DESCniPTION Af,0 PROBA LE C ENCES l o 12 l l At 3755 hours0.0435 days <br />1.043 hours <br />0.00621 weeks <br />0.00143 months <br /> on 6/10/81 with reactor power at 9 E _Befueline Uator Storape Tank I

(iWST) Icvel indicator, [L1-QS-100A}, f ailed low then returned to normal several

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j o g.i i l minutes later. Af ter declaring the channel inoperatsle, power operation continued l

go is; l - lii accordance with Technical Specification 3.3.2.1.

Public ? calth and safety were l 10161'l not jeopardized since suf ficient redundant channels were availa.le for auto safety l lc l7) [

injection transfer which initiates on low icvel in the RI?ST.

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gil2 l investigation traced the failure to the force motor within the loop level 1

- l: 131 l transmitter and on 6/24/81 the transmitter was removed for repair and replaced.

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,.b Attachment to LER 81--58/031.

l Ilea er Valley Power Station Duquesne 1ight Company Docket l'o. 50-334 No further information is available or needed to satisfy the reportitig requircra tnt.

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