05000331/LER-1981-022-03, /03L-0:on 810607,during Testing,Reactor Core Isolation Cooling Turbine Repeatedly Tripped on Overspeed on Fast Starts.Caused by Upward Drift of Flow Controller FIC-2509 High Limit Setpoint.Setpoint Recalibr

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/03L-0:on 810607,during Testing,Reactor Core Isolation Cooling Turbine Repeatedly Tripped on Overspeed on Fast Starts.Caused by Upward Drift of Flow Controller FIC-2509 High Limit Setpoint.Setpoint Recalibr
ML20009A966
Person / Time
Site: Duane Arnold NextEra Energy icon.png
Issue date: 07/07/1981
From: Schmidt A
IES UTILITIES INC., (FORMERLY IOWA ELECTRIC LIGHT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20009A959 List:
References
LER-81-022-03L, LER-81-22-3L, NUDOCS 8107140557
Download: ML20009A966 (1)


LER-1981-022, /03L-0:on 810607,during Testing,Reactor Core Isolation Cooling Turbine Repeatedly Tripped on Overspeed on Fast Starts.Caused by Upward Drift of Flow Controller FIC-2509 High Limit Setpoint.Setpoint Recalibr
Event date:
Report date:
3311981022R03 - NRC Website

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