Similar Documents at Byron |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20045A6941993-06-0404 June 1993 LER 93-003-00:on 930511,turbine Emergency Trip Oil Header Pressure Low Alert Received Followed by Reactor Trip & Turbine Trip Above P-8.Caused by Actuation of Overspeed Trip Relay.Faulty Power Supply Board replaced.W/930604 Ltr ML20024H2041991-05-22022 May 1991 LER 91-005-01:on 900817,preoutage Mod Work Initiated W/O Proper Operability Review Due to Programmatic Deficiencies. Daily Const Work Authorization Sheet formalized.W/910522 Ltr ML20029A6461991-02-20020 February 1991 LER 90-007-01:on 900612,main Steam Line Isolation Sys Declared Inoperable Due to Failure to Test Manual Initiation Handswitch.Caused by Deficiency in Procedure.Procedures reviewed.W/910219 Ltr ML18041A2251990-10-0303 October 1990 LER 90-006-00:on 900903,reactor Containment Fan Cooler 2C, Low Speed Fan Breaker Did Not Close,Resulting in Train a Safety Injection Signal.Caused by Miscommunication & Procedure Deficiency.Procedure revised.W/901003 Ltr ML20029A6901990-09-13013 September 1990 LER 90-011-01:on 900819,reactor Trip Occurred Due to Power Surge.Caused by Lightning Strike.Rod Drive Sys Will Be Modified W/New Model of Power Supply Less Likely to Cause Reactor trip.W/910221 Ltr ML20044B0991990-07-12012 July 1990 LER 90-007-00:on 900612,discovered That Steam Line Isolation Handswitch on Main Control Board Panel 1PM06J Not Tested During Past Refueling Outages.Caused by Deficient Procedure. All Similar Equipment Will Be reviewed.W/900712 Ltr ML20044A9871990-07-11011 July 1990 LER 89-005-01:on 890501,diesel Generator 1A Failed to Load to 5,500 Kw within 60 as Required.Caused by Max Fuel Setting on Fuel Control Sys Being Set Too Low.Vendor Instructions Added to Maint procedures.W/900629 Ltr ML20043D5841990-06-0101 June 1990 LER 90-006-00:on 900503,as Surveillance Underway All Indication on Digital electro-hydraulic Computer Panel Was Lost.Caused by Failure of Ampere Fuse Due to Short Circuit in Pushbutton.Lighting Circuit rewired.W/900530 Ltr ML20042G9121990-05-0808 May 1990 LER 87-012-01:on 870408,component Cooling Pump 1A Tripped When Surge Tank Level Dropped to Low Level Pump Trip Setpoint.Caused by Breakdown in Communication.Mod to Component Cooling Sys completed.W/900507 Ltr ML20042E1561990-04-0606 April 1990 LER 90-003-00:on 900307,individual Cell Voltage for Cell 53 Found to Be at 2.11 Volts,Contrary to Tech Spec Limit.Caused by Electrician Using Improper Acceptance Criteria Format & Inadequate Mgt Review of surveillance.W/900406 Ltr ML20006F7161990-02-16016 February 1990 LER 90-001-00:on 900118,determined That Containment Purge Isolation Sys Not Demonstrated Operable 100 H Prior to Start of Core Alterations.Caused by Cognitive Personnel Error. Task Force Formed to Review Tech Specs.W/900109 Ltr ML20006E1161990-02-0909 February 1990 LER 90-001-00:on 900118,during Functional Surveillance on Steam Generator Pressure Channel 526,channel 525 Spiked Low, Causing Reactor Trip & Safety Injection.Caused by Failure of Pressure Transmitter.Transmitter replaced.W/900126 Ltr ML20006D7401990-02-0505 February 1990 LER 87-004-01:on 870225,inadvertent Safety Injection Occurred During Maint Troubleshooting.Caused by Cognitive Personnel Error by Control Sys Technician Involved. Disciplinary Action Taken & Counseling done.W/900124 Ltr ML20005E2391989-12-26026 December 1989 LER 89-003-01:on 890227,area Radiation Monitor 2RT-AR012 Failed Automatic Checksource Test,Actuating Containment Ventilation Isolation Alarm.Caused by Faulty Detector. Detector Replaced & Monitor Returned to svc.W/891221 Ltr ML19327B9021989-11-0303 November 1989 LER 89-009-00:on 891005,conflicting Info Re Signals That Initiate Automatic Isolation of Steam Generator Blowdown Lines Found.Caused by Preservice Design Implementation Deficiency.Lines Isolated & Procedure changed.W/891103 Ltr ML19354D4681989-11-0101 November 1989 LER 89-008-01:on 890830,one Auxiliary Feedwater Suction Pressure Transmitter Calibr Not Head Corrected & Bases of Original Setpoints Not Questioned.Caused by Inadequate Procedures & Setpoint calculations.W/891101 Ltr 1993-06-04
[Table view] Category:RO)
MONTHYEARML20045A6941993-06-0404 June 1993 LER 93-003-00:on 930511,turbine Emergency Trip Oil Header Pressure Low Alert Received Followed by Reactor Trip & Turbine Trip Above P-8.Caused by Actuation of Overspeed Trip Relay.Faulty Power Supply Board replaced.W/930604 Ltr ML20024H2041991-05-22022 May 1991 LER 91-005-01:on 900817,preoutage Mod Work Initiated W/O Proper Operability Review Due to Programmatic Deficiencies. Daily Const Work Authorization Sheet formalized.W/910522 Ltr ML20029A6461991-02-20020 February 1991 LER 90-007-01:on 900612,main Steam Line Isolation Sys Declared Inoperable Due to Failure to Test Manual Initiation Handswitch.Caused by Deficiency in Procedure.Procedures reviewed.W/910219 Ltr ML18041A2251990-10-0303 October 1990 LER 90-006-00:on 900903,reactor Containment Fan Cooler 2C, Low Speed Fan Breaker Did Not Close,Resulting in Train a Safety Injection Signal.Caused by Miscommunication & Procedure Deficiency.Procedure revised.W/901003 Ltr ML20029A6901990-09-13013 September 1990 LER 90-011-01:on 900819,reactor Trip Occurred Due to Power Surge.Caused by Lightning Strike.Rod Drive Sys Will Be Modified W/New Model of Power Supply Less Likely to Cause Reactor trip.W/910221 Ltr ML20044B0991990-07-12012 July 1990 LER 90-007-00:on 900612,discovered That Steam Line Isolation Handswitch on Main Control Board Panel 1PM06J Not Tested During Past Refueling Outages.Caused by Deficient Procedure. All Similar Equipment Will Be reviewed.W/900712 Ltr ML20044A9871990-07-11011 July 1990 LER 89-005-01:on 890501,diesel Generator 1A Failed to Load to 5,500 Kw within 60 as Required.Caused by Max Fuel Setting on Fuel Control Sys Being Set Too Low.Vendor Instructions Added to Maint procedures.W/900629 Ltr ML20043D5841990-06-0101 June 1990 LER 90-006-00:on 900503,as Surveillance Underway All Indication on Digital electro-hydraulic Computer Panel Was Lost.Caused by Failure of Ampere Fuse Due to Short Circuit in Pushbutton.Lighting Circuit rewired.W/900530 Ltr ML20042G9121990-05-0808 May 1990 LER 87-012-01:on 870408,component Cooling Pump 1A Tripped When Surge Tank Level Dropped to Low Level Pump Trip Setpoint.Caused by Breakdown in Communication.Mod to Component Cooling Sys completed.W/900507 Ltr ML20042E1561990-04-0606 April 1990 LER 90-003-00:on 900307,individual Cell Voltage for Cell 53 Found to Be at 2.11 Volts,Contrary to Tech Spec Limit.Caused by Electrician Using Improper Acceptance Criteria Format & Inadequate Mgt Review of surveillance.W/900406 Ltr ML20006F7161990-02-16016 February 1990 LER 90-001-00:on 900118,determined That Containment Purge Isolation Sys Not Demonstrated Operable 100 H Prior to Start of Core Alterations.Caused by Cognitive Personnel Error. Task Force Formed to Review Tech Specs.W/900109 Ltr ML20006E1161990-02-0909 February 1990 LER 90-001-00:on 900118,during Functional Surveillance on Steam Generator Pressure Channel 526,channel 525 Spiked Low, Causing Reactor Trip & Safety Injection.Caused by Failure of Pressure Transmitter.Transmitter replaced.W/900126 Ltr ML20006D7401990-02-0505 February 1990 LER 87-004-01:on 870225,inadvertent Safety Injection Occurred During Maint Troubleshooting.Caused by Cognitive Personnel Error by Control Sys Technician Involved. Disciplinary Action Taken & Counseling done.W/900124 Ltr ML20005E2391989-12-26026 December 1989 LER 89-003-01:on 890227,area Radiation Monitor 2RT-AR012 Failed Automatic Checksource Test,Actuating Containment Ventilation Isolation Alarm.Caused by Faulty Detector. Detector Replaced & Monitor Returned to svc.W/891221 Ltr ML19327B9021989-11-0303 November 1989 LER 89-009-00:on 891005,conflicting Info Re Signals That Initiate Automatic Isolation of Steam Generator Blowdown Lines Found.Caused by Preservice Design Implementation Deficiency.Lines Isolated & Procedure changed.W/891103 Ltr ML19354D4681989-11-0101 November 1989 LER 89-008-01:on 890830,one Auxiliary Feedwater Suction Pressure Transmitter Calibr Not Head Corrected & Bases of Original Setpoints Not Questioned.Caused by Inadequate Procedures & Setpoint calculations.W/891101 Ltr 1993-06-04
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H5221999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Byron Station, Units 1 & 2.With ML20217P6351999-09-29029 September 1999 Non-proprietary Rev 6 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212B9261999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Byron Station,Units 1 & 2.With ML20210R3431999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Byron Station, Units 1 & 2.With ML20210E2251999-07-21021 July 1999 B1R09 ISI Summary Rept Spring 1999 Outage, 980309-990424 ML20209G1751999-07-0808 July 1999 SG Eddy Current Insp Rept,Cycle 9 Refueling Outage (B1R09) ML20207H7941999-06-30030 June 1999 Rev 0 to WCAP-15180, Commonwealth Edison Co Byron,Unit 2 Surveillance Program Credibility Evaluation ML20207H8071999-06-30030 June 1999 Rev 0 to WCAP-15178, Byron Unit 2 Heatup & Cooldowm Limit Curves for Normal Operations ML20207H7851999-06-30030 June 1999 Rev 0 to WCAP-15183, Commonwealth Edison Co Byron,Unit 1 Surveillance Program Credibility Evaluation ML20207H7771999-06-30030 June 1999 Rev 0 to WCAP-15177, Evaluation of Pressurized Thermal Shock for Byron,Unit 2 ML20209H3711999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Byron Station, Units 1 & 2.With ML20207H7561999-06-28028 June 1999 Pressure Temp Limits Rept (Ptlr) ML20207H7621999-06-28028 June 1999 Pressure Temp Limits Rept (Ptlr) ML20195J8001999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Byron Station,Units 1 & 2.With ML20207B6481999-05-25025 May 1999 SER Accepting Revised SGTR Analysis for Byron & Braidwood Stations.Revised Analysis Was Submitted to Support SG Replacement at Unit 1 of Each Station ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations ML20206R6991999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Byron Station Units 1 & 2.With ML20195C7961999-04-28028 April 1999 Rev 2 to NFM9800233, Byron Station Unit 2 COLR for Cycle 8A (BY2C8A) M980023, Rev 2 to NFM9800233, Byron Station Unit 2 COLR for Cycle 8A (BY2C8A)1999-04-28028 April 1999 Rev 2 to NFM9800233, Byron Station Unit 2 COLR for Cycle 8A (BY2C8A) ML20205P7001999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Byron Station,Units 1 & 2.With ML20205B5091999-03-26026 March 1999 SER Accepting Relief Requests 12R-24,Rev 0 & 12R-34,Rev 0, Related to Second 10-year Interval Inservice Insp for Byron Station,Units 1 & 2 ML20205C5101999-03-21021 March 1999 Revised Safety Evaluation Supporting Improved TS Amends Issued by NRC on 981222 to FOLs NPF-37,NPF-66,NPF-72 & NPF-77.Revised Pages Include Editorial Corrections ML20204G3831999-03-19019 March 1999 Safety Evaluation Accepting Second 10-yr Interval ISI Request for Relief 12R-11 M990004, Rev 0 to NFM9900043, Byron Unit 1,Cycle 10 COLR in ITS Format W(Z) Function1999-03-17017 March 1999 Rev 0 to NFM9900043, Byron Unit 1,Cycle 10 COLR in ITS Format W(Z) Function ML20206A8831999-03-17017 March 1999 Rev 0 to NFM9900043, Byron Unit 1,Cycle 10 COLR in ITS Format W(Z) Function ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20204H9941999-03-0303 March 1999 Non-proprietary Rev 4 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations ML20204C7671999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Byron Station,Units 1 & 2.With ML20199G8271998-12-31031 December 1998 Rev 1 Comm Ed Byron Nuclear Power Station,Unit 1 Cycle 9 Startup Rept ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with ML20202F6181998-12-31031 December 1998 Cycle 8 COLR in ITS Format & W(Z) Function ML20206B4001998-12-31031 December 1998 Annual & 30-Day Rept of ECCS Evaluation Model Changes & Errors for Byron & Braidwood Stations ML20199E6371998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Byron Station,Units 1 & 2.With ML20202F6021998-12-31031 December 1998 Cycle 9 COLR in ITS Format & W(Z) Function ML20196K6731998-12-31031 December 1998 10CFR50.59 Summary Rept for 1998 ML20207H7731998-11-30030 November 1998 Rev 0 to WCAP-15125, Evaluation of Pressurized Thermal Shock for Byron,Unit 1 ML20207H8011998-11-30030 November 1998 Rev 0 to WCAP-15124, Byron Unit 1 Heatup & Cooldown Limit Curves for Normal Operation ML20198D1501998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Byron Nuclear Power Station,Units 1 & 2.With ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20195F8321998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Byron Nuclear Power Station,Units 1 & 2.With 05000454/LER-1998-018, Corrected LER 98-018-00:on 980912,inoperable Unit 1 DG Was Noted.Caused by Low Lube Oil Pressure Condition.Immediately Entered Into Lcoar for AC Sources TS 3.8.1.1,Action a1998-10-0909 October 1998 Corrected LER 98-018-00:on 980912,inoperable Unit 1 DG Was Noted.Caused by Low Lube Oil Pressure Condition.Immediately Entered Into Lcoar for AC Sources TS 3.8.1.1,Action a ML20207H7671998-10-0505 October 1998 Rv Weld Chemistry & Initial Rt Ndt ML20154L5501998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Byron Nuclear Power Station,Units 1 & 2.With ML20197C9051998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Byron Nuclear Power Station,Units 1 & 2.With ML20151Z9651998-08-31031 August 1998 Revised MOR for Aug 1998 for Byron Nuclear Power Station. Rept Now Includes Page 9 Which Was Omitted from Previously Issued Rept ML20238F6551998-08-28028 August 1998 SE Authorizing Licensee Request for Relief NR-20,Rev 1 & NR-25,Rev 0 Re Relief from Examination Requirement of Applicable ASME BPV Code,Section XI for First ISI Interval Exams ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237B3361998-08-14014 August 1998 B2R07 ISI Summary Rept,Spring 1998 Outage, 961005-980518 ML20237B4841998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Byron Nuclear Power Station Units 1 & 2 1999-09-30
[Table view] |
Text
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/ ) B ron Nucint Station
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..! ; T 4 50 North G!rman Church Road M'
Nv,/ - Byron, Illinois 61010 -
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-January 26, 1990 l> -Ltra . BYRON 90-0108.
U.:S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 Dear Sirt.
l The enclosed Licensee Event Report from Byron Generating Station is being E transmitted to you in accordance with the requirements of 10CFR50.73(a)(2)(lv).
i This report is number 90-001; Docket No. 50-455. ;
a Sincerely,
-i Yi !
.[V _ R. L Plenlewicz -
Station Manager Byron Nuclear Power Station l 1
1
~RP/bb .:
Enclosure Licensee Event Report No.90-001
- cc A. Bert Davis, NRC Region III Administrator -I W' Kropp, NRC Senior Resident Inspector l INPO Record Center
-i .., Ceco Distribution List
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i 9002220074 900209 ;
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6 ADOCK 05000455 PDC ,
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LICENSEE EVENT REPORT (LER)
Form Res 2.0 (ccll'ity Name (1)
Docket Number (2) _fage (3)
Byron. Unit 2 01 51 01 01 01 41 51 5 1lof!0!_1_
Title (4)
_RLAC10R TRIP QHJO STEAMLINE PRESSURE DUE TO ONE CHARNEL SPIKIMG LOW DURING A FUNC110N.6L SURVEILLA
_EysttLDate ($1 LER J4 umber (6) _ _RepnLDate (7) Other Facilities Involved (8)
Month Day Year Year fj/j// Sequential ,/j// Revision Month Day Year Facility Names Docket Numberft)
/// Number ///, Number
~
NONE 0151010101 l l
~~~
QJ 1 1 18 910 91 0 0 1 0 11 010 012 Ol 9 91 0 0151010101 ( l' OPERATING (Check one or more of the followino) (11) 1 20.402(b) ___ 20.405(c) l_ 50.73(a)(2)(tv) ___ 73.71(b)-
POWER 20.405(a)(1)(1) 50.36(c)(1)
__ _ _._ 50.73(a)(2)(v) _ 73.71(c)
LEVEL 20.405(a)(1)(ll) 50.36(c)(2) 50.73(a)(2)(vii)
(10) l9l9 _
20.405(a)(1)(tii) _
50.73(a)(2)(i)
_ 50.73(a)(2)(viii)(A)
___ Other (Specify (a Abstract
/////,///////,/,/,//,/////,/////, _., 20.405(a)(1)(iv) ._._ 50.73(a)(2)(ii) ___ 50.73(a)(2)(viii)(B) below and in
////j///////j'/j' j' /j' /////'j /////'j
// / _ 20.405(a)(1)(v) _ 50.73(a)(2)(iii) _ 50.73(a)(2)(x) Text)
LICENSEE CONTACT FOR THIS LER (12)
Name TELEPHONE NUPSER AREA CODE
. T. Gierich. Doeratino Enoineer Ext. 2218 8l115 213141 l514141 COMPLETE ONE LINE FOR EACH COM ON N FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFAC- REPORTABLE CAUSE SYSTEM COMPONENT MANUFAC- REPORTABLE TURER TO NPRDS TURER TO NPRDS X SlB l l Pl T I l 21 01 4 Y I I I i 1 1 I l l l l Jl I, I I l i 1 I l-SUPPLEMENTAL REPORT EXPECTED (14) Expected Month l pg M ear Submission lyes (If_ythmjete EXPECTED SUBMISS 1011 DATE) #
X l NO 1 l ll ABSTRACT (Limit to 1400 spaces, i.e. approximately fif teen single-space typewritten lines) (16)
On January-18, 1990. Unit 2 was operating at 99% power. An Instrument Maintenance Technician was performing a functional surveillance on steam pressure channel 526 when channel 525 spiked low. A reactor trip and safety injsction followed.
Th2 most probable cause of the event was the failure of the 525 pressure transmitter. The transmitter was rep 1:ced, and the spiking has not recurred. This is the first time the coincidence was satisfied during a pr3ssure transmitter f ailure and resulted in a reactor trip.
This event is reportable per 10CFR50.73(a)(2)(iv) for any event or condition that resulted in manual or automatic actuttion of any Engineered Safety Feature, including the Reactor Protection System.
(0516R/0059R)
r' :
.p-LICENSEE EVENT REPORT (LER) TEXT CQMUHUATION' Form Rev 2.0 :
. FACILITY NAME (1) DOCKET NUMBER (2) JJfLNUMBER (6) Page (3)
Year /// Sequential Revision
,, //
, fff
/// . Number
/j//
ff
/ Number Jyron. Unit 1 0 l 5 1 0 1.jLj .Q_jJllj_1 9 1 0 -
01.0l1 - 010 012 0F Ol 3
- TEX 1 Energy Industry Identification System (EIIS) codes are identified in the text as (XX)-
A. 11 ANT CONDITIONS PRIOR TO EVENT:
~ Event Date/ Time 1/18/90 / 0042 ,
Unit 2 H0DE 1 - Power Operations _ Rx Power _o9% RCS ( AB) Temperature / Pressure _HQDnA]_0Reratino
~
B. bESCRIPTIONOFEVENT:
At-the start of this event, steam pressure channel 526 (corresponding to the 2B steam generator) was in test for calibration under 2 BIS 3.2.1-015, Surveillance Functional Test for Loop 526 Steam Generator 2B Pressure Protection Channel III. Limiting Condition for Operation Action Requirements (LCOAR)
.280$ 3.2-la and 200$ 3.3.6-la we re in ef fect. The surveillance placed the channel's protection blstables i in the tripped condition. At 0042 on January 10, 1990, steam pressure channel 525 (corresponding to the ;
2D steam generator) spiked low creating a 2 out of 3 coincidence in 1 out of 4 main steam lines for a low
~ steam line pressure safety injection / reactor trip. Procedure 2BEP-0, Reactor Trip or Safety Injection (SI) was entered. At step 32 in 2BEP 0, the safety injection termination criteria was met and 2BEP ES 1.1 SI Termination procedure was entered. The safety injection was reset at 0050. All safety systems functioned as designed.- All operator actions were correct.
This event is reportable under 10CFR50.73 (a)(2)(iv).
C. CAUSE OF EVENT:
1he proximate cause of the event was a low spike on a transmitter combined with a coincident channel in test. The root cause cf the transmitter spike is indeterminate.
The Inst'rument Maintenance Technician perfonning the surveillance on channel 526 was several feet away from the protection cabinet (2PA03J) signing a step in the survel11ance package when the trip occurred.
The surveillance was_ essentially complete except for restoring the blstables. Thetehnician'sactivities did not affect channel 525 spiking.
D .~ 1AFETY ANALYSL$:
There was no effect on the health and safety of the plant or public. The plant responded nonnally following the trip and all Engineered Safety Feature Systems actuated properly. The steam pressure loops supply logic to the-water hammer prevention system and initiate safety injection on low steam pressure and steamline isolation on high negative steam pressure rate. Two of the three loops must respond for any
- safety actuation to occur.
E.- [DRRECTIVE ACTION 1:
tNR B73382 was written to investigate the spike on the 525 steam pressure channel (2PT-0525).
During troubleshooting, a variety of checks were performed on the equipment associated with this loop.
The transmitter input loop power supply, both isolated and non-isolated outputs, power to the transmitter, the signal comparator, and both lead lag amplifiers were checked and found functioning properly.
.The pressure transmitter was replaced as a conservative measure under this NWR, PNR B73400 was written to monitor transmitter 2PT-0525. No abnormalities were noted. Based on the. lack of further spikes, .the transmitter replacement is considered to be adequate corrective action.
[(0516R/0059R)
o LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Form Rev 2.0 eFACI[ITYkA'ME(1) DOCKET NUMBER (2) LER NUMBER (6) Pace (3)
. Year- /
j/((
Sequential /j{
/
/j/J Revision
// Number Number
.BJtan. Unit 1 0 l 5 l 0 1 0 l 0 l 41 5.1 4 910 -
0_l 0 l 1 - _0__j 0 01 3 0F 01 3 TEXT Energy Industry Identification System (E!!S) codes are identified in the text as (XX)
F. EREVIDU$ OCCURRENCE 1:
No previous LERs were attributed to pressure transmitter failures. A Nuclear Plant Reliability Data System (NPRDS) Component Failure Analysis Report (CFAR) showed a slightly higher f ailure rate (f allures / component-hour) for Unit 1 (2.38E-05) as compared to the industry (7.24E-06). Unit 2 showed a similar comparison (which excluded Unit I f ailures) of 1.34E-05 failures / component-hour compared to an industry rate of 7.65E-06. The significance criterion for the Unit I comparison was 2.642 (which is slightly higher than the 1.645 standard used to indicate higher than industry average) and 0.949 for Unit 2. A review of the NPRDS search did not reveal a common mode failure mechansim. A Total Job Management (TJM) search of the Station's maintenance history identified 35 equipment identification numbers with ITT Barton #763 pressure transmitters. A total of 65 work requests were found. Work request 73382 was the only work request found on 2PT-0525. No common mode failure was identified from the TJM search.
G. !
(QMPONENT FAILURE DATA:
HANUFACTURER NOMENCLATURE MODEL NUMBER ITT Barton Pressure Transmitter 763 e
1 1
1 l
l l
(0516R/0059R)