ML20005A812

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Interim Deficiency Rept,Originally Reported on 810107,re Nonconservative Analysis of Load Limits of Spent Fuel Cask Handling Crane.Mod to Cranes to Be Seismically Qualified, Accompanied by Mod to Lifting Device
ML20005A812
Person / Time
Site: Washington Public Power Supply System
Issue date: 06/01/1981
From: Mazur D
WASHINGTON PUBLIC POWER SUPPLY SYSTEM
To: Faulkenberry B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
References
10CFR-050.55E, 10CFR-50.55E, G1-81-163, GO1-81-163, NUDOCS 8107010306
Download: ML20005A812 (2)


Text

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  • y Washington Public Power Supply System A JOINT OPERATING AGENCY
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1990 N. California Boulevard .

Walnut Creek, California 94596 hj[(\i-h 0p T{f by 5.E p/fg,h Attention: Mr. B. H. Faulkenberry 7 Chief, Reactor Constructf

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Projects Branch JA

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Subject:

PROJECTS 1 AND 4 DOCKET NOS. 50-460 AND 50-513 i u, [8 '

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REPORTABLE CONDITI0ft 10CFR50.55(e)

SPENT FUEL CASK HANDLING CRANE

Reference:

1) Telecon TJ Houchins, Supply System to DF Kirsch, Region V Nuclear Regulatory Commission dated January 7, 1981
2) G01-81-27, dated February 2, 1981, DW Mazur to RH Engelken, Director In reference 1) the Supply System informed your office of a reportable deficiency under 10CFR50.55(e) and reference 2) was an interim report on the subject condition.

Attachment A includes a restatement of the reportable condition and a brief description of our selected alternative for correcting the deficiency. Although a final alternative has been selected, not all of the details and schedules have been completed by Engineering; therefore, in keeping with reference 2), we are submitting this report (Attachment A), however, this should also be considered an interim report pending completion of the Engineering design. A final report will be submitted by November 1,1981. This report will be more explicit regarding the details of the selected alternative.

If ycu have any questions or desire further information, please l

advise.

Very truly yours, f.

D. W. I ur Program Director l WNP-1/4 1 Attachments DWM:MER:pm cc: CR Bryant, Bonneville Power Administration /399 S-#

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ATTACHMENT A WNP-1/4 DOCKET NOS 50-460 AND 50-513 REPORTABLE CONDI!10N 10 CFR 50.50(e) ,

SPENT FUEL CASK HANDLING SYSTEM INTERIM REPORT  !

BACKGROUND As described in the WNP-1/4 PSAR in 1973, the spent fuel storage pool and handling equipment was designed based on a 150 ton spent fuel cask dropping a maximum distance of 30 feet in the General Services Building (GSB). The structural design was based on analysis of missile penetra-tion into a rigid barrier at that time. It was determined, based on the analysis, that the structure could withstand the drop of the loaded cask due to a single failure or as a result of SSE without affecting the cbility to shut down the plant.

DESCRIPTION OF DEFICIENCY It has been determined that more restrictive load limits must be placed on the GSB structure as the previous analysis was non-conservative. The GSB could not withstand the drop of a 150 ton spent fuel cask through 30 feet without affecting critical plant equipment.

SAFETY IMPLICATIONS The drop of a 150 ton cask could damage critical plant equipment either through direct impact, through the spalling of concrete, or by affecting the building structure and subsequently the equipment itself. The Containment Spray System, Decay Heat Removal System and Auxiliary Feedwater System could be affected by the drop.

REPORTIBILITY It was determined that the condition, if left uncorrected could have affected adversely the safety of operation of the plant upon failure of the spent fuel cask crane. This condition has been determined to be reportable.

CORRECTIVE ACTION TAKEN Modification of the existing spent fuel cask handling cranes (1 per plant) to be seismically qualified accompanied by modifications to the lifting device to make it redundant will meet the requirements. The reliance for the safe handling of critical loads as defined in NUREG 554 will be placed on the Crane System itself. The system will be redesigned for the lifted load, so that a single failure will not result in the loss of the capability of the system to safely retain the load.

Once the details of this alternative are finalized, a final report will be prepared and submitted. This report will be submitted by November 1, 1981.

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