ML20004F233

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Monthly Operating Rept for May 1981
ML20004F233
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 06/01/1981
From: Hairston W
ALABAMA POWER CO.
To:
Shared Package
ML20004F231 List:
References
TASK-2.K.3.03, TASK-TM NUDOCS 8106160648
Download: ML20004F233 (6)


Text

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JOSEPH M. FARLEY NUCLEAR PLANT UNIT 2 Q-NARRATIVE

SUMMARY

OF OPERATIONS MAY, 1981 Projected date for conumercial operation is 8 /1/81.

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8106160(95

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TMI ACTION PLAN-SECTION II.K.3.3 - REPORTING SAFETY AND RELIEF VALVE FAILURES AND CHALLENGES 1.

At 2352 on 5/14/81 while performing the Natural Circulation with Simulated LOSP Phase III Test Procedure (T.P. 501-7-002), Power Operated

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Relief Valve 444B cycled four (4) times. The primary pressure was lower than the PORV setpoint, however, the primary pressure was higher than.

normal long enough for the PORV integral controller to integrate up.

2.

At 2030 on 5/15/81 while performing the Natural Circulation Phase III Test Procedure (T.F. 501-7-003), a steam generator code safety valve in 'B' steam line lifted and reseated.

3.

At 1540 on 5/25/81 while performing the Dynamic Automatic Steam Dump Centrol Phase III Test Procedure (T.P. 083-7-527), a steam generator code rafety valve in 'B' steam line lifted and stuck in the open position.

This event was initiated by a malfunction in the Steam Dump Control System which resulted in steam pressure exceeding the safety valve setpoint.

A gag has been installed on the safety valve to prevent opening.

The safety valve will be replaced with a new valve when plant conditions parmit.

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OPERATING DATA REPORT DOCKETNO. 50-364 DATE 6 /1/R1 COMPLETED BY W.C.Hairston, III TELEPHONE (205)899-5156 OPERATING STATUS

1. Unit Name:

Joseph M. Farley - Uni 2 Notes: (1) Projected date for

2. ReportingPeriod:

May. 1981 coanercial operation is

3. Licensed Thermal Power (MWt):

2652 8/8/81.

4. Nameplate Rating (Gross MWe):

860

5. Desagn Electrical Rating (Net MWe).

829

6. Maximum Dependable Capacity (Gross MWe):

860*

829*

7. Maximum Dependable Capacity (Net MWe):
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:

N/A

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9. Power Level To Which Restricted. lf Any (Net MWe):

N/A

10. Reasons For Restrictions. If Any:

N/A i

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' This Month Yr.-to.Date Cu[nulat,ive ',

146.2 146.2 146.2.

11. Hours in Reporting Period _
12. Number Of Hours Reactor Was Critical 343.2 343.2' 343.2 l
13. Reactor Reserve Shutdown Hours 26.4 26.4 26.4
14. Hours Generator On-Line 68.8 68.8 68.8
15. Unit Reserve Shutdown Hours 0

0 0

16. Gross Thermal Energy Generated (MWH) 49 210.2 49.210.2 49,210.2
17. Gross Electrical Energy Generated (MWH) 9.680 9,680 9,680
18. Net Electrical Energy Generated (MWH) 4.644 4.644 4,644
19. Unit Service Factor N/A,

N/A N/A

20. Unit Availability Factor N/A N/A N/A
21. Unit Capacity Factor (Using MDC Net) -

N/A _

N/A N/A

22. Unit Capacity Factor (Using DER Net)

N//

N/A N/A

23. Unit Forced Outage Rate N/A N/A N/A
24. Shutdowns Schecused Over Next 6 Months (Type. Date.and Duration of Each):

Maintanar.ce : June. 1981t One week

25. If Shur Down At End Of Report Period. Estimated Date of Startup:

N/A

26. Units in Test Status (Prior to Commercial Operation):

Forecast Achiesed INITIA L CRITICALITY 5/6/81 5/8/81 INITIAL ELECTRICITY 5/24/81 5/25/81 COMMERCIAL OPERATION 8/8/81

  • The Nameplate Rating / Design. Electrical Rating will be used for the Maximum Dependable Capacity until an accurate value can be determined from operating experience.

(0/77)

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AVERAGE DAILY UNITTOWER LEVEL

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50-364 DOCKET NO.

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ggg7 DA2 6/1/81 COMPLETED BY W.G.Hairston, III

,s" TELEPHONE (205)899-5156 MONTH May, 1981 i.

4 DAY AVERAGE DAILY POWER LEVEL

  • DAY AVERAGE DAIL POWER LEVEL (MW'N*t)

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INSTRUCUONS On this forner. list the avenge daily unit powe-levet in MWe Net for each day in the reporting month. Compute ta the ne:re:r whole meg: watt.

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UNIT SIIUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-364 UNIT NAME J.M.Farlev-Unit 2 DATE 6/1/81 COMPLETED BY u c.Hairston. III HEPORT MONTil Mav. 1981 TELEPif0NE (205)899-5156 i

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Licensec g%

Cause & Currective No.

Date c-5g

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Event a

a-3 Action to g$ 5 s2 j;$g Report

  • UI jU Prevent Recurrence 4

c5 810501 S

597.8 H

4 N/A N/A N/A Prior to initially putting turbine generator on line.

01 810525 F

43.2 A

1 N/A HA INSTRU Generator manually taken off line to investigate Digital Electro-Hydraulic Control system problems.

i 02 810528 F

20.9 H

1 N/A HC YYYYYY Unit t,ipped due to S/G level control problem after a turbine trip.

03 810530 F

7.0 B

1 N/A HH VALVEX Unit tcipped on S/G ?.c's-low level while testing the main feed regulat-ing valves.

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F: Forced Reason:

Method:

Exhibh G Instructions l

S: Scheduled A Equipment Failure (Explain) 1 Manual for Preparation of Data l

D-Maintenance or Test 2 Manual Scram-Ent y Sheets for IJeensee C-Refueling 3 Automatic Scram.

Event Report (LER) File INUREG-D-Regulatory Restriction 4 Other(limplain) 0161)

E-Operator Training & License Examination 3

4 F Administrative 5

G-Operational Erros (Explain)

Exhibit I - Same Source a

(9/77)

Il-Other (Explain)

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s DOCKET NO. 50-364 UNIT SilOTDOWNS AND POWER REDUCTIONS i

UNIT NAME J.M.Farley-Unit 2 DATE 6/1/81 COMPLETED BY (W.G.Hairston, ~III FEPORT MONTil May, 1981 TELEPif0NE 205)899-5156 i

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.$ ?

Y Licensee

$v, k3 1,

Cause & Corrective a

No.

Date g

3g jgg Event uT Action to b

$5 5

jigg Repert #

N0 yV-.

Prevent Recurrence j

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04 810530 F

6.3 B

1 N/A HH VALVEX Unit tripped while testing main feed regulating valves.. Turbine and SGFP's tripped on S/G high level.

j Reactor tripped on S/G low-low level after turbine ' trip.

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3 4-F: Forced Reason:

hlethoJ:

Exhibit G. instructions S: Scheduled A Equipment Failure (Explain) 1 Manual for Preparation of Data 1

B-Maintenance or Test 2 Manual Scram.

Entry Sheets for Licensee C-Refueling 3 Automatic Scram.

Eveni Report (LE R) File (NUREG.

D Regulatory Restriction 4 Other (Explain) 01611 E-Operator Tsaining & License Examination s

F Administrative 5

G-Operational Etrur (Explain)

Exhibit i.Same Source PJ/77)

Il-3ther (Explain)

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