05000334/LER-1981-041-01, /01T-0:on 810513,tritium Activity Collected in Oh River Downstream of Facility Exceeded ETS Level of 1390 pCi/1.Subsequent Tritium Releases for First Quarter 1981 Were Below 10CFR20 Limit

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/01T-0:on 810513,tritium Activity Collected in Oh River Downstream of Facility Exceeded ETS Level of 1390 pCi/1.Subsequent Tritium Releases for First Quarter 1981 Were Below 10CFR20 Limit
ML20004B892
Person / Time
Site: Beaver Valley
Issue date: 05/22/1981
From: Lacey W
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20004B891 List:
References
LER-81-041-01T, LER-81-41-1T, NUDOCS 8106010246
Download: ML20004B892 (2)


LER-1981-041, /01T-0:on 810513,tritium Activity Collected in Oh River Downstream of Facility Exceeded ETS Level of 1390 pCi/1.Subsequent Tritium Releases for First Quarter 1981 Were Below 10CFR20 Limit
Event date:
Report date:
3341981041R01 - NRC Website

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U.S. NUCLEAR REGULATORY COMMISSION NRC FORM 358 mm

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60 61 DOCKET NUMSER 68 69 EVENT QATE 74 75 REPORT D ATE S0 EVENT DESCRIPTION AND PROS ABLE CONSEQUENCET h ITTTI I The tritium activity in a quarterly composite of weekly grab samples, Collected in i

lTTTI I the Ohio River downstream of the Beavur Valley Power Station effluent during the iTTTT I first quarter of 1981, was found to be 2290 pCi/1. This exceeds the Environmental l This is the Ioisi I Technical Specification, Table 3.2-4, reporting level of 1390 pCi/1.

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. Docket No. 50-334 No further information is available or needed to satisfy the reporting requirement.

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