05000324/LER-1981-035-03, /03L-0:on 810225,during Normal Startup,While Moving Control Rods,Rod Overtravel Annunciator Was Received During Verification of rod-drive Coupling for Rod 30-23. Cause Will Be Determined During Outage

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/03L-0:on 810225,during Normal Startup,While Moving Control Rods,Rod Overtravel Annunciator Was Received During Verification of rod-drive Coupling for Rod 30-23. Cause Will Be Determined During Outage
ML20003E587
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 03/27/1981
From: Pastva M
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20003E586 List:
References
LER-81-035-03L, LER-81-35-3L, NUDOCS 8104060604
Download: ML20003E587 (1)


LER-1981-035, /03L-0:on 810225,during Normal Startup,While Moving Control Rods,Rod Overtravel Annunciator Was Received During Verification of rod-drive Coupling for Rod 30-23. Cause Will Be Determined During Outage
Event date:
Report date:
3241981035R03 - NRC Website

text

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