05000277/LER-1980-029-01, /01T-0:on 801113,reactor Core Isolation Cooling Sys Declared Inoperable.Caused by Turbine Trip Valve Switch Being Out of Adjustment.Switch Readjusted & Tested

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/01T-0:on 801113,reactor Core Isolation Cooling Sys Declared Inoperable.Caused by Turbine Trip Valve Switch Being Out of Adjustment.Switch Readjusted & Tested
ML20002B128
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 11/26/1980
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20002B125 List:
References
LER-80-029-01T, LER-80-29-1T, NUDOCS 8012090470
Download: ML20002B128 (1)


LER-1980-029, /01T-0:on 801113,reactor Core Isolation Cooling Sys Declared Inoperable.Caused by Turbine Trip Valve Switch Being Out of Adjustment.Switch Readjusted & Tested
Event date:
Report date:
2771980029R01 - NRC Website

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