05000334/LER-1980-102-03, /03L-0:on 801129,all Three Chlorine Detectors Noted Not Dripping.Caused by Fluid Tank Being Under Slight Vacuum & Clogged Wick.Vent & Wick Cleaned.Engineering Requested to Evaluate

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/03L-0:on 801129,all Three Chlorine Detectors Noted Not Dripping.Caused by Fluid Tank Being Under Slight Vacuum & Clogged Wick.Vent & Wick Cleaned.Engineering Requested to Evaluate
ML19353A237
Person / Time
Site: Beaver Valley
Issue date: 12/26/1980
From: Lacey W
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19353A235 List:
References
LER-80-102-03L, LER-80-102-3L, NUDOCS 8101070531
Download: ML19353A237 (2)


LER-1980-102, /03L-0:on 801129,all Three Chlorine Detectors Noted Not Dripping.Caused by Fluid Tank Being Under Slight Vacuum & Clogged Wick.Vent & Wick Cleaned.Engineering Requested to Evaluate
Event date:
Report date:
3341980102R03 - NRC Website

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Attachment To LER 80-102/03L Beaver Valley Power Station Duquesne Light Company Docket No. 50-334 No further information is available or needed to satisfy the reporting require =ent.