05000368/LER-1980-060, Updated LER 80-060/03X-2:800730 & 1202,D Core Protection Calculator Failed.C Core Protection Calculator Failed on 801120.Watchdog Timer Timed Out Preventing Console Communications.Core Protection Calculator Sys Reinitialized

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Updated LER 80-060/03X-2:800730 & 1202,D Core Protection Calculator Failed.C Core Protection Calculator Failed on 801120.Watchdog Timer Timed Out Preventing Console Communications.Core Protection Calculator Sys Reinitialized
ML19351F394
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 01/07/1981
From: Bramlett L
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19351F380 List:
References
LER-80-060-03X, LER-80-60-3X, NUDOCS 8101120389
Download: ML19351F394 (1)


LER-1980-060, Updated LER 80-060/03X-2:800730 & 1202,D Core Protection Calculator Failed.C Core Protection Calculator Failed on 801120.Watchdog Timer Timed Out Preventing Console Communications.Core Protection Calculator Sys Reinitialized
Event date:
Report date:
3681980060R00 - NRC Website

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  1. 4 R(,QH T 0 4 T E 80 EVENT DESCRirTION AND PRC8 ASLE CONSEQUENCES h (HD IDuring Mode 1 coeration. the "D" Core Protection Calculator (CPC) failed 1 EIT) lon 7/30/80 and 12/2/80.

The "C" CPC failed on 11/20/80.

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ITrips were bypassed on the affected CPC channel, placing the Reactor i

o A io ni ITrio Loaic in a two out of three trip sequence. The unaffected channels i t o is i tremained operable.

Similar LER's for CPC "C" are 50-368/80-002,79-098, i 179-096: For the "D" CPC is 50-368/80-008: for "A" CPC are 50-368/80-51, I

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CAUSE DESCRIPTION AND COSREC fivE ACTIONS h FFTTl i Investigation did not reveal the root cause of the CPC orocram halt.

I w 1 " Watchdog" timer timed out preventing console communications, rendering i EID i the CPC technically inoperable.

The CPC system was re-initialized. by-1 I

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