05000368/LER-1981-012-03, /03L-0:on 810303,loop Two Svc Water Header Engineered Safety Feature Isolation Valve 2CV-1406-2 Would Not Open from Control Room.Caused by Valve Operator Torquing Out Due to Valve Stem Binding

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/03L-0:on 810303,loop Two Svc Water Header Engineered Safety Feature Isolation Valve 2CV-1406-2 Would Not Open from Control Room.Caused by Valve Operator Torquing Out Due to Valve Stem Binding
ML19350C219
Person / Time
Site: Arkansas Nuclear 
Issue date: 03/26/1981
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19350C218 List:
References
LER-81-012-03L, LER-81-12-3L, NUDOCS 8103310597
Download: ML19350C219 (1)


LER-1981-012, /03L-0:on 810303,loop Two Svc Water Header Engineered Safety Feature Isolation Valve 2CV-1406-2 Would Not Open from Control Room.Caused by Valve Operator Torquing Out Due to Valve Stem Binding
Event date:
Report date:
3681981012R03 - NRC Website

text

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O hRC FORM 364 U.S. NUCLE AR REGULATORY COMMisssON LICENSEE EVENT REPORT EXHIBIT A

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EVENT OESCRIPTION ANO PRQS AS([ CONSEOVENCES EE) IDurino Mode 1 operation, while performino a Containment Cooler monthiv

.1 isurveillance test, the Loop Two Service Water Header ESF Isolation Valve, i m.,

o, i2CV-1406-2, would not open from the Control Room.

Tne valve was placed i

'in its ES position, returning the Loop Two Service Water Header to oper-i g

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Loop One remained operable. There have been no similar i

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CAUSE DESCRIPTION AND CORRECOVE ACTIONS 27 Naintenance investigation revealed that the valve stem was binding, causing

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The valve was lubricated and exercised i tand returned to service.

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