05000324/LER-1981-039-03, /03L-0:on 810410,reactor Core Isolation Cooling Turbine Tripped.Caused by Loss of Turbine Speed Control Due to Open Voltage Dropping Resistor R1 in Electronic Governor Module.Resistor Replaced

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/03L-0:on 810410,reactor Core Isolation Cooling Turbine Tripped.Caused by Loss of Turbine Speed Control Due to Open Voltage Dropping Resistor R1 in Electronic Governor Module.Resistor Replaced
ML19347E725
Person / Time
Site: Brunswick 
Issue date: 05/07/1981
From: Pastva M
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19347E721 List:
References
LER-81-039-03L-01, LER-81-39-3L-1, NUDOCS 8105130275
Download: ML19347E725 (2)


LER-1981-039, /03L-0:on 810410,reactor Core Isolation Cooling Turbine Tripped.Caused by Loss of Turbine Speed Control Due to Open Voltage Dropping Resistor R1 in Electronic Governor Module.Resistor Replaced
Event date:
Report date:
3241981039R03 - NRC Website

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l During the performance of the RCIC System 1000 PSIG Flow Rate Test.

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l RCIC turbine tripped due to overspeed making the RCIC System inoOerable.

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