05000219/LER-1980-042-03, /03L-0:on 800911,high Drywell Switches IP-15A, IP-15B & IP-15C Tripped at Value Greater than 2.0 Psig as Specified in Tech Specs.Caused by Instrument Drift.Switches Adjusted to Trip within Tech Spec Limit

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/03L-0:on 800911,high Drywell Switches IP-15A, IP-15B & IP-15C Tripped at Value Greater than 2.0 Psig as Specified in Tech Specs.Caused by Instrument Drift.Switches Adjusted to Trip within Tech Spec Limit
ML19347B640
Person / Time
Site: Oyster Creek
Issue date: 10/07/1980
From: Crosby P
JERSEY CENTRAL POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19347B634 List:
References
LER-80-042-03L, LER-80-42-3L, NUDOCS 8010150479
Download: ML19347B640 (1)


LER-1980-042, /03L-0:on 800911,high Drywell Switches IP-15A, IP-15B & IP-15C Tripped at Value Greater than 2.0 Psig as Specified in Tech Specs.Caused by Instrument Drift.Switches Adjusted to Trip within Tech Spec Limit
Event date:
Report date:
2191980042R03 - NRC Website

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ic i:j i On September 11, 1980. whil'e oorforming The "Conta %mont Soray Systom 1

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IP-15C tripped at a value greater than that soecified in Tech Soec

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I Table 3.1.1, item E.1.

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IP-15B was 2.05 psic and IP-15C was "AlR osio. The desired setonint is i

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