05000334/LER-1980-119-03, /03L-0:on 801231,cooling Tower Discharge Temp High Alarm Setpoint Found High.Probably Caused by Instrument Drift.Setpoint Adjusted

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/03L-0:on 801231,cooling Tower Discharge Temp High Alarm Setpoint Found High.Probably Caused by Instrument Drift.Setpoint Adjusted
ML19345E982
Person / Time
Site: Beaver Valley
Issue date: 01/30/1981
From: Lacey W
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19345E983 List:
References
LER-80-119-03L, LER-80-119-3L, NUDOCS 8102060485
Download: ML19345E982 (2)


LER-1980-119, /03L-0:on 801231,cooling Tower Discharge Temp High Alarm Setpoint Found High.Probably Caused by Instrument Drift.Setpoint Adjusted
Event date:
Report date:
3341980119R03 - NRC Website

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