05000334/LER-1980-086-01, /01T-0:on 801121,pipe Support on Seal Injection Header from Discharge of High Head Safety Injection Pumps Determined to Be in Overstressed Condition.Cause Unknown. Support Mods Made

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/01T-0:on 801121,pipe Support on Seal Injection Header from Discharge of High Head Safety Injection Pumps Determined to Be in Overstressed Condition.Cause Unknown. Support Mods Made
ML19345D346
Person / Time
Site: Beaver Valley
Issue date: 12/05/1980
From: Lacey W
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19345D337 List:
References
LER-80-086-01T, LER-80-86-1T, NUDOCS 8012120535
Download: ML19345D346 (2)


LER-1980-086, /01T-0:on 801121,pipe Support on Seal Injection Header from Discharge of High Head Safety Injection Pumps Determined to Be in Overstressed Condition.Cause Unknown. Support Mods Made
Event date:
Report date:
3341980086R01 - NRC Website

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Attachment To LER 80-86/0lT Beaver Valley Power Station Duquesne Light Company Docket No. 50-334 No further information is availabic or needed to satisfy the reporting requirement.

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