05000271/LER-1980-038-03, /03L-0:on 801027,during Refueling Operations LIS- 2-3-72A Isolated from Svc During Installation of Analog Trip Sys.Cause Not Stated.New Analog Instrument Installed

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/03L-0:on 801027,during Refueling Operations LIS- 2-3-72A Isolated from Svc During Installation of Analog Trip Sys.Cause Not Stated.New Analog Instrument Installed
ML19345B736
Person / Time
Site: Vermont Yankee File:NorthStar Vermont Yankee icon.png
Issue date: 11/26/1980
From: Murphy W
VERMONT YANKEE NUCLEAR POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19345B733 List:
References
LER-80-038-03L, LER-80-38-3L, NUDOCS 8012020439
Download: ML19345B736 (1)


LER-1980-038, /03L-0:on 801027,during Refueling Operations LIS- 2-3-72A Isolated from Svc During Installation of Analog Trip Sys.Cause Not Stated.New Analog Instrument Installed
Event date:
Report date:
2711980038R03 - NRC Website

text

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60 61 CCCKET NUM8ER id 69 EVENT QATE 14 75 MEPCRT CAT 3 30 EVENT CESCRIPTICN AND PRCSA8LE CONSECUENCES h Ioi2l l During refueling operations LIS-2-3-72A was isolated from service during installa- [

10,31 l tion of the analog trip system without first failing the trip system as required by l lotal l T.S. Table 3.2.1.

At the time the instrument was isolated, both core spray systems l Ioisl I were required to be operable per T.S. 3.5.H.4.

All other level instruments for the I l o is I l systems were onerable and would have initiated core sorav if recuired. There were loI7i l no significant occurrences as a result of this event nor were there any adverse i

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