ML19345B730

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Forwards Responses to NRC Questions Re Fifth Cycle License Application
ML19345B730
Person / Time
Site: Calvert Cliffs Constellation icon.png
Issue date: 11/26/1980
From: Lundvall A
BALTIMORE GAS & ELECTRIC CO.
To: Clark R
Office of Nuclear Reactor Regulation
References
NUDOCS 8012020432
Download: ML19345B730 (3)


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B ALTIMORE G AS AN D ELECTRIC COM P ANY P.O. D O X 1475 U A LTI M O R E. MAHYLAND 21203 A n t n u s C t.U N OV A LL, Ja.

v.a ret,.. :. v.s November 26, M80 s.<.

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Of fice of Nuclear ReacYor Regulation U. S. Nuclear Regulatory Cornmission 9

Washington, D. C. 20555 ATTENTION:

Mr. R. A. Clark, Chief t;

, Operating Reactors Branch //3 e

pj Division of Licensing Eb C'

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SUBJECT:

Calvert Clif fs Nuclear Power Plant i

Unit No.1, Docket No. 50-317 d

Arnendrnent to Operating License DPR-53 g

Fif th Cycle License Application

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Responses to NRC Staff Questions e.

G entjemen:.

Enclosed are our reponses to questions posed by NRC staf f on the subject application.

Very truly yours, BALTIMORE GAS AND eld TRIC COMPANY

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('}' ' A. E. Lundva,II, Jr.

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Vice President - Supply AEL/WJL/rnit Copy To:

3. A. Biddison, Esquire (w/out Encl.)

G. F. Trow bridge, Esquire (w/out Encl.)

Messrs.

E. L. Conuer, Jr., NRC P. W. Kruse, CE F012020@A

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ENCLOSURE I

QUESTION Provide a list of the assumptions applicable to dose rate calculations of the Seized Rotor Event.

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RESPONSE

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1) During first 1800 sec there is no operator action.
Thus, bypass valve dump to the condenser and dump valves to atmosphere.

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2) Beyond 1800 seconds steam dump is to condenser via operator action.
3) Primary activity released to secondary assumed to be released without mixing within the S.G. secondary liquid.

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4) Primary to secondary leak rate.*

1 GPM 5)

Initial Reactor Coolant System Maximum Allowable Tech Spec Concentration * (DEQ 1-131) 1.0uC 1 gm l

6)

Initial Steam Generator Maximum Allowable i

Concentration (DEQ-131)*

0.1 uC 1 i

gm

7) Reactor Coolant System Maximum Allowable Concentration of Noble Gases (DEQ-133)*

100/E 4

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8) Partition Factor for Primary Release Through Atmospheric Dumps-1.0 4
9) Partition. Factor for Secondary Steam Release Through Atmospheric Dump 0.1
  • Tech Soec. Limits-

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Enclosure Page 2 10)

Feed' Pump Turbine' Air Ejector Partition Factor

.0005 3

11) Atmospheric Dispersion Coefficient 1.8 X 10~4 sec/m i

3

12) Breathing Rate 3.47 X 10- m /sec 6

13)

Dose Conversion Factor-(I-131) 1.486 X 10 REM /C y

14) All Activity in the Gap is Assumed to be 4

Released to the Coolant 15)

STEAM REl. EASES i

Steam Release Point Approximate Amount of Steam Release Dump Valves (0-1800 sec) 55130 lbm l

Bypass to' Turbine (0-1800 sec) 12265 lbm Bypass to Turbine (1800-7200 sec) 53200 lbm Primary to Secondary Mass Transfer (0-7200sec) s1000 lbm 1

Thyroid Dose = 3.60 REM (2 hr) j j

Whole Body Dose = 0.4 REM.(2 hr) i i

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