LER-1979-033, Unisolatable Leak Discovered at Seal Cavity Pressure Sensing Line to 2PT-6006 for Reactor Coolant Pump 2P32A.Caused by Mechanical Fatigue Resulting from Low Stress Cyclic Loading.Mods Complete |
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Od REVISED REPORT - PREVIOUS REPORT DATE 5/25/79 U.S. NUCLE AR REGULATORY COMMISSION NRC f 0RM 364 LICENSEE EVENT REPORT EXHIBIT A CONTROL BLOCK: l l l l l l IPLEASE PRINT OR TYPE ALL REOUIRED INFORMATIONI l AlR l Al' N] 0 l 2 lgl 010 l -l0 l 0 l 0l Oj 0 l-l 0 l0 lg l1 l 1 l1 l 1 lgl clar lg 1,
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j EVENT DESCRIPTION AND PRO 8ABLE CONSEQUENCES O'o 4
rETrl i During Mode 3 operation, an unisolatable leak was discovered at the seal i I
EIT) I cavity pressure sensino line to 2PT-6006. for the Reactor Coolant Pumo. I I 2P32A.
The leak was verified to be from a crack in the weld and heat I
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The leakt o s to 1:; I rate was estimated to be less than GPM.
No similar occurrences.
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CAUSE DESCRsPTION AND CORREC flVE ACTIONS 27 l Based on macroscopic and microscopic observations, the crack is character +
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No signs of corrosion cracking.
Concluded i m i that the break is a result of a mechanical fatigue resulting from low i
m i stress cyclic loading. Vibration analysis completed. Modifications to i i angers and installation of vibration dampening material reduced vibratiop h
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Reportable Occurrence Report No.
50-368/79-033/01X Rev. 1 2.
Report Date:
11/20/80 3.
Occurrence Date:
5/14/80 4
Facility: Arkansas Nuclear One - Unit Two Russellville, Arkansas 5.
Identification of Occurrence:
Abnormal degradation discovered in the reactor coolant pressure boundary, identified as unisolatable leak.
Reportable per T.S. 6.9.1.8.c.
6.
Conditions Prior to Occurrence:
Steady-State Power Reactor Power 0
Mwth Hot Standby Net Output 0
Hwe Cold Shutdown Percent of Full Power 0 Refueling Shutdown Load Changes During Routine Power Operation Routine Startup X
opera tion MODE 3
Routine Shutdown Operation Other (specify) 7.
Description of Occurrence:
An unisolatable leak was discovered at the seal cavity pressure sensing line to 2PT-6006, for the Reactor Coolant Pump, 2P32A.
The leak was verified.to be from a crack in the weld and heat affected zone of the weld that attaches the line to the pump seal cavity.
Leak rate was estimated to be < GPM.
Cooldown and depressurization was initiated immediately per requirements of Action Statement T.S. 3.4.6.2.a.
b Rt ortabic Occurrence Report No. 50-368/79-033/01X Rev. 1
~
8.
Designation oc Apparent Cause of Occurrence:
Design Procedure Fhnufacture Unusual Service Condition Including Environmental Installation /
Construction Component Failure X
(See Failure Data)
Operator Other (specify)
The leaking pipe was removed from the pump seal by cutting through the weld behind the crack so the entire crack was preserved intact.
The type 316 stainless steel schedule 80 3/4 inch pipe was sent to Southwest Researcn Institute for failure analysis.
A fractographic examination was conducted on a section of the weld that included one crack tip. The macroscopic virface appearance indicated fatigue with multiple initiation sites.
Scanning electron microscope fractographs from the fracture surface revealed evidence of periodic markings indicative of high cycle fatigue.
Energy dispersive x-ray spectroscopy of the fracture surface revealed no contaminate species. Metallographic sections of the primary crack showed unbranched, predominately transgranular, propagation.
The pipe base metal was verified to be within tolerance of composition and hardness, as set in ASTM Standard A-312. There were no signs of external corrosion or chloride stress corrosion cracking.
Failure analysis concluded that the crack is purely the result of mechanical fe'.igue resulting from relatively low stress cyclic loading.
- 9. Analysis of Occurrence:
. Analysis of the fault indicated that the fatigue in the weld adjoining the rotating equipment was a result of (1) vibration (possible in resonance) of the pump, (2) Inadequately supported flange and/or associated piping hangs from the end of a horizontal pipe section.
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- - r Reportable Occurrence Report No. 50-368/79-033/01X Rev. 1 i
10
Corrective Action
The pipe section was upgraded to a schedule 160. A design change
~
4 modified associated hangers and added rubber material on several
- - hanger to pipe attachments to dampen pipe vibrations.
The reactor
- - coolant pump seal removal procedures were revised for added insurance thai. the rubber vibration dampening material is reinstalled following maintenance on each of the affected pipe hangers and tr.at the pipe-hangers are tightened properly.
l Vibration measurements were taken on.the 2P32A and 2P32C pumps following modification. The data was evaluated and it was verified t
i that the vibration was reduced to an acceptable level.
Dye penetrant
- - inspections were made at several weld connections on the seal piping j
and no additional evidence of cracks were discovered.
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Failure Da'ta:
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No similar occurrences.
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| 05000368/LER-1979-001-03, /03L-0 on 790102:refueling Water Tank Level Indicator Failed High.Caused by Frozen Transmitter Sensing Line.Line Was Thawed & Returned to Operable Status within 20-h | /03L-0 on 790102:refueling Water Tank Level Indicator Failed High.Caused by Frozen Transmitter Sensing Line.Line Was Thawed & Returned to Operable Status within 20-h | | | 05000313/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000313/LER-1979-001-03, /03L-0 on 790112:during Mode 5 Operation,Purge Supply Flow from VSF-30B Would Not Meet Surveillance Requirements.Caused by Supply Filter VFA-20B Collapsing from Water Restricting Air Flow.Filter Changed | /03L-0 on 790112:during Mode 5 Operation,Purge Supply Flow from VSF-30B Would Not Meet Surveillance Requirements.Caused by Supply Filter VFA-20B Collapsing from Water Restricting Air Flow.Filter Changed | | | 05000313/LER-1979-002-01, /01T-0 on 790205:during Startup,Nuclear Instrumentation Was Not Calibr as Required by Tech Spec 4.1, Table 4.1-1.Caused by Personnel Error.Occurrence Discussed W/Shift | /01T-0 on 790205:during Startup,Nuclear Instrumentation Was Not Calibr as Required by Tech Spec 4.1, Table 4.1-1.Caused by Personnel Error.Occurrence Discussed W/Shift | | | 05000313/LER-1979-002, Forwards LER 79-002/01T-0 | Forwards LER 79-002/01T-0 | | | 05000368/LER-1979-002-03, /03L-0 on 790103:refueling Water Level Transmitter Refroze.Caused by Frozen Transmitter Sensing Line.Addl Insulation & Heat Lamps Added to Sensing Lines & Transmitter Cabinets | /03L-0 on 790103:refueling Water Level Transmitter Refroze.Caused by Frozen Transmitter Sensing Line.Addl Insulation & Heat Lamps Added to Sensing Lines & Transmitter Cabinets | | | 05000313/LER-1979-003-01, /01T-0 on 790425:leak Discovered in Heat Affected Zone of 1 Inch Drainline Socket Weld in B Decay Heat Discharge Cross Connect to a Loop.Caused by Vibration Fatigue.Outer Drainline Isolation Valves Replaced | /01T-0 on 790425:leak Discovered in Heat Affected Zone of 1 Inch Drainline Socket Weld in B Decay Heat Discharge Cross Connect to a Loop.Caused by Vibration Fatigue.Outer Drainline Isolation Valves Replaced | | | 05000368/LER-1979-004-03, /03L-0 on 790107:during Power Escalation Testing, Both Control Element Assembly Clusters Declared Inoperable. Caused by Weak Reed Switch Position Transmitter Power Supply | /03L-0 on 790107:during Power Escalation Testing, Both Control Element Assembly Clusters Declared Inoperable. Caused by Weak Reed Switch Position Transmitter Power Supply | | | 05000313/LER-1979-004-03, /03L-0 on 790424:reactor Bldg Spray Pump Unresponsive to Engineered Safeguards Signal.Caused by Incorrect Agastat Time Relay Setting.Relay Adjusted | /03L-0 on 790424:reactor Bldg Spray Pump Unresponsive to Engineered Safeguards Signal.Caused by Incorrect Agastat Time Relay Setting.Relay Adjusted | | | 05000313/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000368/LER-1979-005-03, /03L-0 on 790109:during Power Escalation Testing, Bistable Primary Power System 6 C Failed,Rendering C Pressurizer Low Pressure Trip Inoperable | /03L-0 on 790109:during Power Escalation Testing, Bistable Primary Power System 6 C Failed,Rendering C Pressurizer Low Pressure Trip Inoperable | | | 05000313/LER-1979-005-03, /03L-0 on 790524:during Leak Rate Testing, Penetration V-1 Leaked in Excess of 50,000 Cubic Cm/Minute. Caused by Buildup of Boric Acid Crystals on Valve Seating Surfaces.Repairs Made & Penetrations Retested | /03L-0 on 790524:during Leak Rate Testing, Penetration V-1 Leaked in Excess of 50,000 Cubic Cm/Minute. Caused by Buildup of Boric Acid Crystals on Valve Seating Surfaces.Repairs Made & Penetrations Retested | | | 05000313/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000368/LER-1979-006-03, /03L-0 on 790109:during Power Escalation Testing, B Core Protection Computer Declared Inoperable When Low Pressurizer Pressure Trips Received.Investigation Showed Ground Fault Relays Fall Out on Low Bus Voltage | /03L-0 on 790109:during Power Escalation Testing, B Core Protection Computer Declared Inoperable When Low Pressurizer Pressure Trips Received.Investigation Showed Ground Fault Relays Fall Out on Low Bus Voltage | | | 05000368/LER-1979-006, Forwards Revised LER 79-006/03X-1 | Forwards Revised LER 79-006/03X-1 | | | 05000313/LER-1979-006-01, /01T-0 on 790607:vendor Notified Util of Possibility That Turbocharger Thrust Bearing Could Be Damaged Under Certain Repeat Start Operating Modes. Procedures Modifided & Improved Lube Oil Sys Being Designed | /01T-0 on 790607:vendor Notified Util of Possibility That Turbocharger Thrust Bearing Could Be Damaged Under Certain Repeat Start Operating Modes. Procedures Modifided & Improved Lube Oil Sys Being Designed | | | 05000313/LER-1979-006, Forwards LER 79-006/01T-0 | Forwards LER 79-006/01T-0 | | | 05000368/LER-1979-007, Forwards LER 79-007/03L-0 & LER 79-009/03L-0 | Forwards LER 79-007/03L-0 & LER 79-009/03L-0 | | | 05000368/LER-1979-007-03, /03L-0 on 790113:during Power Escalation Test, Control Element Assembly Position as Received by Core Protection Computer B Was Incorrect.Caused by Bad Multiplexer Card,Which Was Replaced | /03L-0 on 790113:during Power Escalation Test, Control Element Assembly Position as Received by Core Protection Computer B Was Incorrect.Caused by Bad Multiplexer Card,Which Was Replaced | | | 05000313/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000313/LER-1979-007-03, /03L-0 on 790616:during Heatup,Emergency Feedwater Pump Automatically Started W/Inadvertent Actuation.Caused by Valve Lineup Error.Outboard Pump Bearing Found to Be Hot Due to Faulty Installation.Maint Procedure Revised | /03L-0 on 790616:during Heatup,Emergency Feedwater Pump Automatically Started W/Inadvertent Actuation.Caused by Valve Lineup Error.Outboard Pump Bearing Found to Be Hot Due to Faulty Installation.Maint Procedure Revised | | | 05000313/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000368/LER-1979-008-03, /03L-0 on 790114:during Power Ascension Testing, Refueling Water Tank Level transmitter,2LT-5639-3,sensing Line Froze Due to Temporary Heat Lamp Burnout | /03L-0 on 790114:during Power Ascension Testing, Refueling Water Tank Level transmitter,2LT-5639-3,sensing Line Froze Due to Temporary Heat Lamp Burnout | | | 05000313/LER-1979-008-03, /03L-0 on 790621:emergency Feed Actuation Received When once-through Steam Generator a Startup Level Transmitter Selection Was Shifted.Caused by Overspeed Trips Due to Water in Steam Supply Line | /03L-0 on 790621:emergency Feed Actuation Received When once-through Steam Generator a Startup Level Transmitter Selection Was Shifted.Caused by Overspeed Trips Due to Water in Steam Supply Line | | | 05000368/LER-1979-009-03, /03L-0 on 790121:during Power Escalation Testing, Reactor Protection Sys Channel C Trip Path Solid State Relay Failed,Opening Reactor Trip Path Circuit Breakers 3 & 7.Relay Was Replaced;Within 4-h Circuit Breakers Closed | /03L-0 on 790121:during Power Escalation Testing, Reactor Protection Sys Channel C Trip Path Solid State Relay Failed,Opening Reactor Trip Path Circuit Breakers 3 & 7.Relay Was Replaced;Within 4-h Circuit Breakers Closed | | | 05000313/LER-1979-009, Forwards LER 79-009/03L-0 & 79-010/01T-0 | Forwards LER 79-009/03L-0 & 79-010/01T-0 | | | 05000313/LER-1979-009-03, /03L-0 on 790628:during Power Operation Reactor Bldg Hydrogen Purge Fan VSF-30A Tripped After 90 Minutes of 10-h Run.Caused by Overcurrent.Fan Restarted Using Less Sealing Water | /03L-0 on 790628:during Power Operation Reactor Bldg Hydrogen Purge Fan VSF-30A Tripped After 90 Minutes of 10-h Run.Caused by Overcurrent.Fan Restarted Using Less Sealing Water | | | 05000313/LER-1979-010, Forwards Updated LER 79-010/01X-1 | Forwards Updated LER 79-010/01X-1 | | | 05000313/LER-1979-010-01, /01T-0 on 790714:design of Main Steamline Restraints Did Not Consider Steam Hammer Transient Forces. Review Performed.Overstressed Area Will Be Modified | /01T-0 on 790714:design of Main Steamline Restraints Did Not Consider Steam Hammer Transient Forces. Review Performed.Overstressed Area Will Be Modified | | | 05000368/LER-1979-010-03, /03L-0 on 790124:pump Discharge valve,2CV-5667-2, Stroked Fully Open But Immediately Reclosed.Caused by sodium-hydroxide Tank Low Level Alarm & Indication Circuit Being Out of Alignment | /03L-0 on 790124:pump Discharge valve,2CV-5667-2, Stroked Fully Open But Immediately Reclosed.Caused by sodium-hydroxide Tank Low Level Alarm & Indication Circuit Being Out of Alignment | | | 05000368/LER-1979-011-03, /03L-0 on 790125:during Power Escalation,Channel B Core Protection Computer Failed,Resulting in Departure from Nucleate Boiling Ratio & Linear Power Density Trips. Caused by Movement of Temporary Cables Connected to B | /03L-0 on 790125:during Power Escalation,Channel B Core Protection Computer Failed,Resulting in Departure from Nucleate Boiling Ratio & Linear Power Density Trips. Caused by Movement of Temporary Cables Connected to B | | | 05000368/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000313/LER-1979-011, Forwards LER 79-011/01T-O | Forwards LER 79-011/01T-O | | | 05000313/LER-1979-011-01, /01T-0 on 790809:during NRC Performance Appraisal Team Interview,Discovered That Pressurizer Safety Relief Valve PSV-1002 Was Not Properly Tested in Mar 1978.Valve Retested 790812 W/No Adjustments Required | /01T-0 on 790809:during NRC Performance Appraisal Team Interview,Discovered That Pressurizer Safety Relief Valve PSV-1002 Was Not Properly Tested in Mar 1978.Valve Retested 790812 W/No Adjustments Required | | | 05000313/LER-1979-012, Forwards LER 79-012/03L-1 | Forwards LER 79-012/03L-1 | | | 05000313/LER-1979-012-03, Leak Rate Testing of Reactor Bldg Purge Valves at Penetration V-1 Indicated Leak Rate in Excess of Tech Spec Limits.Caused by Maladjusted Valve Seat Shims.Leak Rate Test Performed | Leak Rate Testing of Reactor Bldg Purge Valves at Penetration V-1 Indicated Leak Rate in Excess of Tech Spec Limits.Caused by Maladjusted Valve Seat Shims.Leak Rate Test Performed | | | 05000368/LER-1979-012-03, /03L-0 on 790127:core Protection Computer Channel B Failed,Resulting in Trips.Caused by Analog High Level Amplifier Card Improperly Seating in Connector.Card Reseated & Functional Test Conducted | /03L-0 on 790127:core Protection Computer Channel B Failed,Resulting in Trips.Caused by Analog High Level Amplifier Card Improperly Seating in Connector.Card Reseated & Functional Test Conducted | | | 05000313/LER-1979-013-03, /03L-0:on 790808,decay Heat Boron Concentration Was Not Monitored During Prescribed Interval & Inservice Decay Heat Loop Was Switched W/O Switching Sample Lineup. Caused by Communications Breakdown Between Depts | /03L-0:on 790808,decay Heat Boron Concentration Was Not Monitored During Prescribed Interval & Inservice Decay Heat Loop Was Switched W/O Switching Sample Lineup. Caused by Communications Breakdown Between Depts | | | 05000313/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000368/LER-1979-013-03, /03L-0 on 790127:control Element Assembly Cluster (Ceac) Deviation Alarms Received.Caused by Disturbance of Ceac Cable Connections | /03L-0 on 790127:control Element Assembly Cluster (Ceac) Deviation Alarms Received.Caused by Disturbance of Ceac Cable Connections | | | 05000313/LER-1979-014, Forwards LER 79-014/99X-0 | Forwards LER 79-014/99X-0 | | | 05000313/LER-1979-014-99, /99X-0:on 790813,w/75% Reactor Power,Switchyard Relay 21Z1 Failed,Causing Turbine Trip.Caused by Lug Failure on Terminal Leads to Turbine Lockout Relay 286-T.Failed Lug Replaced,Terminals Tightened & Turbine Interlocks Teste | /99X-0:on 790813,w/75% Reactor Power,Switchyard Relay 21Z1 Failed,Causing Turbine Trip.Caused by Lug Failure on Terminal Leads to Turbine Lockout Relay 286-T.Failed Lug Replaced,Terminals Tightened & Turbine Interlocks Tested | | | 05000368/LER-1979-014-03, /03-0 on 790127:plant Protection Sys C Containment Bldg Pressure Transmitter 2PT-5603-3N Failed, Causing Hi & Hi-Hi Containment Pressure Trips.Caused by Loose Output Connection,Which Was Subsequently Reconnected | /03-0 on 790127:plant Protection Sys C Containment Bldg Pressure Transmitter 2PT-5603-3N Failed, Causing Hi & Hi-Hi Containment Pressure Trips.Caused by Loose Output Connection,Which Was Subsequently Reconnected | | | 05000368/LER-1979-015-03, /03L-0 on 790128:failure of Core Protection Computer D & C,Resulting in Respective Channel Trips;One Caused by Tripped Power Supply & Other Appears non-repetitive.Both Channels Were Successfully Restarted | /03L-0 on 790128:failure of Core Protection Computer D & C,Resulting in Respective Channel Trips;One Caused by Tripped Power Supply & Other Appears non-repetitive.Both Channels Were Successfully Restarted | | | 05000313/LER-1979-015-99, /99X-0:on 790817,as Result of Analysis of Seismic Category I Pipe supports,37 Restraints Were Identified to Have Safety Factor of Less than Two.Supports Modified | /99X-0:on 790817,as Result of Analysis of Seismic Category I Pipe supports,37 Restraints Were Identified to Have Safety Factor of Less than Two.Supports Modified | | | 05000368/LER-1979-015, Forwards LER 79-015/03L-0 | Forwards LER 79-015/03L-0 | | | 05000368/LER-1979-016-03, /03L-0 on 790130:during Power Escalation Testing, Mode 1 Operation,Safety Injection Tank D Pressure Dropped Below Tech Spec Limit.Caused by Excessive Leakage Due to Oversized Valve Body.Seal Ring Replaced W/Oversized Ring | /03L-0 on 790130:during Power Escalation Testing, Mode 1 Operation,Safety Injection Tank D Pressure Dropped Below Tech Spec Limit.Caused by Excessive Leakage Due to Oversized Valve Body.Seal Ring Replaced W/Oversized Ring | | | 05000313/LER-1979-016, Forwards Updated LER 79-016/03X-1 | Forwards Updated LER 79-016/03X-1 | | | 05000313/LER-1979-016-03, /03L-0:on 790827,diesel Generator 2 Tripped on Low Oil Pressure,Rendering Generator Inoperable.Caused by Leak Allowing Water to Enter Oil Sys,Causing High Crankcase Pressure.Oil Cooler Replaced | /03L-0:on 790827,diesel Generator 2 Tripped on Low Oil Pressure,Rendering Generator Inoperable.Caused by Leak Allowing Water to Enter Oil Sys,Causing High Crankcase Pressure.Oil Cooler Replaced | | | 05000368/LER-1979-016, Forwards LER 79-016/03L-0 | Forwards LER 79-016/03L-0 | |
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