ML19344E279

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Forwards IE Circular 80-14, Radioactive Contamination of Plant Demineralized Water Sys & Resultant Internal Contamination of Personnel. No Written Response Required
ML19344E279
Person / Time
Site: Arkansas Nuclear  
Issue date: 06/24/1980
From: Seyfrit K
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To: Cavanaugh W
ARKANSAS POWER & LIGHT CO.
References
NUDOCS 8008280306
Download: ML19344E279 (1)


Text

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'p June 24, 1980 Docket Nos.

50-313 50-368 Arkansas Power and Light Company ATTN: Mr. William Cavanaugh III Vice President of Generation and Construction P. O. Box 551 Little Rock, Arkansas 72203 Gentlemen:

The enclosed IE Circular No. 80-14 is forwarded to you for infomation.

If there are any questions related to your understanding of the suggested actions, please contact this office.

Sincerely,

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M g4 Karl V. Seyfrit Director

Enclosures:

l 1.

IE Circular No. 80-14 l

2.

List of IE Circulars Recently Issued l

cc:

James P. O'Hanlon, Plant Manager Arkansas Nuclear One P. O. Box 608 Russellville, Arkansas 72801

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SSINS.: 6830 UNIr_D STATES Accession No.:

HUCLEAR REGULATORY COMMISSION 8005050074 0FFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, D. C.

20555 IE Circular No. 80-14 Date: June 24, 1980 Page 1 of 2 RADI0 ACTIVE CONTAMINATION OF PLANT DEMINERALIZED WATER SYSTEM AND RESULTANT INTERNAL CONTAMINATION OF PERSONNEL This circular describes an event which occurred at a nuclear power facility; however, the generic implications may be applicable to research reactors, and fuel cycle facilities.

On March 17, 1980, a licensee informed the NRC resident inspector that portions of the plant demineralized water (DW) system were found to be radioactively contaminated. A temporary hose used to add demineralized water to the spent fuel pool was the pathway for the cross-contamination. After this fuel pool makeup was completed on March 14, the temporary DW line (still connected to the DW header) was inadvertently left submerged in the fuel pool. Since the DW header pressure at the point of supply was relatively low (a DW booster pump had been secured), a siphoning action occurred, resulting in radioactive contamination of portions of the DW header.

On March 17, 1980, while performing.outine secondary system chemical analyses, the licensee discovered that the demineralized water tap in the chemistry lab contained high levels of boron and had activity of 1.5 x 10-4 uCi/ml (mainly Cs-134,Cs-137,Co-58,Co-60andMn-54).

It was subsequently discovered that demineralized water from the chemistry laboratory supply tap had been used to make five (5) pots of coffee. The remaining coffee was confiscated and the twenty-three (23) individuals who had consumed this coffee were whole-body counted. All involved individuals showed no intake greater than an equivalent 0.01 MPC-HRS. Analysis performed by the licensee's radiation consultant, based on the maximum concentration of radioactivity found in the coffee, indicated that the resultant 50-year dose commitment to an individual drinking eight ounces of this coffee would be less than 1 millirem.

Further licensee investigation revealed that the non-radiological chemistry OW supply tap was the only OW supply point outside the Auxiliary Building controlled area. This DW supply tap was tagged prohibiting human consumption to prevent a similar event in the future.

It is recomended that you review your facility's use of demineralized water (DW) via temporary connections and give attention to the following:

1.

Provisions should be made to assure that radioactive materials are not inadvertently introduced into your facility's DW system via the improper use of temporary connections. A tempca ry cross connection between contaminated systems and tha ?W systet without adequate physical controls to prevent cross-contaminatior $nould ;e prohibited.

IE Circular No. 80-14 Date:

June 24, 1980 P ge 2 of 2 2.

In addition to some physical means of preventing backflow into the OW system, appropriate administrative controls should be established to ensure that the DW supply valve is secured and temporary hosing is disconnected from the OW supply header after use.

3.

Use of plant-supplied DW for human consumption should be prohibited.

The potable water system should be the only authorized source of water for human consumption.

4.

Examine potable and demineralized water systems to determine if pathways exist allowing or having the potential to allow contamination of these systems including temporary connections whereby siphons could cause situations described above.

No written response to this Circular is required.

Your review of this matter to determine its applicability to your facility and any corrective and preven-tive actions taken or planned, as appropriate, will be reviewed during a subsequent NRC inspection.

If you desire additional information regarding this matter, contact the Director of the appropriate NRC Regional Office.

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IE Circular No. 80-14 June 24, 1980 RECENTLY ISSUED IE CIRCULARS Circular Subject Date Issued To No.

Issued 80-09 Prfilems With Plant 4/28/80 All holders of-a power Internal Communications reactor Operating License (OL)

Systems or Construction Permit (CP) 80-10 Failure to Maintain 4/29/80 All holders of Reactor Environmental Qualifi-Operating Licenses (0Ls) cation of Equipment and Construction Permits (cps) 80-11 Dnergency Diesel Generator 5/13/80 All holders of a power Lube Oil Cooler Failures reactor Operating License (0L) or Construction Permit (CP) 80-12 Valve-Shaft-To-Actuator 5/14/80 All holders of Reactor

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Key May Fall Out of Place Operating Licenses (OLs)

When Mounted Below and Construction Permits Horizontal Axis (cps) 80-13 Grid Strap Damage in 5/18/80 All holders of Reactor Westinghouse Fuel Operating Licenses (0Ls)

Assemblies and Construction Permits (cps)

Enclosure l

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