ML19343B397
| ML19343B397 | |
| Person / Time | |
|---|---|
| Site: | Millstone |
| Issue date: | 12/08/1980 |
| From: | Howlett G NORTHEAST NUCLEAR ENERGY CO. |
| To: | |
| Shared Package | |
| ML19343B396 | List: |
| References | |
| NUDOCS 8012230347 | |
| Download: ML19343B397 (6) | |
Text
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OPERATING DATA REPORT 50-336 DOCKET NO.
DATE I2/d/00 CO.\\lPLETED BY G.H. Howlett TELEPHONE (203)447-1791 X364 OPERATING STATUS Millstone 2 Notes
- Items 21 & 22
- 1. Unit Name:
November 1980 cumulative are computed
- 2. Reporting Period:
2700 using a weichted averaae.
- 3. Licensed Thermal Power I51Wt):
909
- 4. Nameplate Rating (Gross 31We):
- 5. Design Electrical Rating (Net 31We): 870 895
- 6. Staximum Dependable Capacity (Gross 31We):
864
- 7. Stasimum Dependable Capacity (Net 51We):
S. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Gise Reasons:
None N0ne
- 9. Power Level To Which Restricted.If Any (Net 5tWe):
- 10. Reasons For Restrictions. If Any:
None This Stonth Yr..to.Date Cumulative i1. Hours in Reporting Period 8.040 43.248 720 5,426.2 30,505.3
- 12. Number Of Hours Reactor Was Critical
- 13. Reactor Rewne Shutdown Hours 0
4.5 2,076.9
- 14. Hours Generator On.Line 720-5,204.8 29,025 0
132.8 468.2
- 15. Unit Reserve Shutdown Hours l
- 16. Cross Thermal Energy Generated (31WH) l.862,268 13,541,545 71,240,173
- 17. Gross Electrical Energy Generated (.\\lWH) 6 0 7. 4.0.0._ _.
4.437.072 23.021.717
- 18. Net Electrical Energy Generated (AlWH) 585.141 4,253,675 22,033,933 100 64.7 6/.I
- 19. Unit Senice Factor
- 20. Unit Asailability Factor 100 66.3 68.2
- 21. Unit Capacity Factor IUsing 51DC Net) 94.1 61.2 61.7 93.4 60.8 60.5
- 22. Unit Capacity FactorIUsing DER Net)
- 23. Unit Forced Outage Rate 0
19.9 23.1
- 24. Shutdowns Scheduled Oser Ne.st 6 Stonths IType, Date.and Duration of Each):
l None
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
- 26. Units In Test Status (Prior to Commercial Operation):
Forecast Achiesed INITIA L CRITICALITY INITIAL ELECTRICITY N/A N/A C051\\lERCI A L OPERATION N/A N/A NOTE: Correction made for error reported for Item 12 Cumulative in October 1980 Operating Data Report.
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6 AVER AGE D AILY UNIT PObER LEVEL i>OCKET NO. ___50-336 user Millstone 2 D A TE 12/8/80-1 CON!PLE TED BY
_.G.H. Howlett TELEPHONE (203)447-1791X364 November 1980 MONTH DAY AVERAGE DAILY POhER LEVEL DAY AVER AGE DAILY POhER LEVEL (MWe-Net)
(MWe-Net) 850 764 -
t 37 2'
851 18 849 3
850 19 835 834 850 4
- o 468 770 5
21 6
849 830 22 7
850 850 23 8
. 852 850 24 9
852-25 850 852 850 to.
26 11 852-850.
27 12 852 850 28 851 849 13 2,
14 850
- 30 850 15 850 31 16 323
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er 50-336 UNITSilUTDOWNS AND POWER REDUCTIONS DOCKET NO.
UNIT N AME Miiistone 2 DATE l?/9/80 flovember 1980 COMPLETED BY G. ll. Ilowlett REPORT MONTil TELEPilONE (20M447 1791 X364 "i
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Date 8.
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Action to
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N0 jV p, event Recurrence c5 4
15 801104 S
0 11 M
CB PUMPXX Power was reduced manually to approx-imately 10% power to allow investiga-tion of P-40D Reactor Coolant Pump low oil level problem. Found no leak added oil and returned to 100% power opera tions.
16 801116 S
0 H
M CB PilMPXX Power was reduced manually to approx-imately 10% power to allow investiga-tion and repair of P-40D Reactor Coolant Pump low oil level problem.
Found and repaired leak in oil level transmitter, added oil and returned to 100% power operations.
1 Summary: The unit operated at or near 100% rated thermal power throughout the month except for the power reductions on the 4th and 16th.
1 i
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Decem.50-336 ____
Docket'No.
3 oer iv, acu Date:
Completed By: G.H. Howlett III Telephone: 203/447-1971 X364 REFUELING INFORMATION REQUEST 1.
Name of facility:
Millstone 2 2.
Scheduled date for next refueling shutdown:
Commence refuel outage November _28,1981.
3.
Schedule date for restart following refueling: January 16, 1982 j
4.
Will _ refueling or resumption of operation thereafter require a technical specification change or other license amendment?
It is not anticipated that Cycle 5 operations will require.
Technical Specification changes or other License amendments.
5.
Scheduled date(s) for submitting licensing action and supporting information:
Licensing documentation will be provided a minimum of 90 days prior to start-up of Cycle 5 or as documented in the R.A. Clark letter to W.G. Counsil, dated 10/6/80, authorizing Cycle 4 operation.
/
6.
Important licensing considerations associated with refueling, e.g., new or-different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures:
N/A i
7.
The number of fuel assemblies (a) in the core and (b) in the-spent fuel storage pool:
(a) In Core:
217 (b) 216 I
8.
The present licensed spent fuel pool storage capacity and the size of any-increase in licensed storage capacity that has been requested or is planned,-
l in number of fuel assemblies:
667 i-9.
The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity:
1985, Spent Fuel Pool, full core off load capability is reached.
1987,. Core Full, Spent Fuel. Pool contains 648: bundles.
l l
50-336
~
Docket No.
Page 1 of 2 Date 12/11/60 Unit Name Millstone ?
Completed By G.H. Howlett Telephone (203)447-1791 X364 CORRECTIVE MAINTENANCE
SUMMARY
FOR SAFETY RELATED EQUIPMENT Report Month October 1980 DATE SYSTEM COMPONENT MAINTENANCE ACTION 10/3/80 Main Steam 2-MS-64B, Main Steam Isolation Replaced valve actuator cylinders.
Valve.
10/3/80 Containment Spray P-43B, Containment Spray Pump Motor Repaired crack in motor end bell at bearing drain plug.
10/3/80-Auxiliary feed P-9A, Aux Steam Generator Feed Repaired crack in motor end bell at bearing drain Pump Motor pluo.
10/5/80 Auxiliary feed H-21 Steam driven aux feed pump Rebuilt valve, turbine trip valve 10/7/80 Main Feedwater 2-FW-12B #2 S/G Aux. feed supply Rebuilt valve operator header air operate check valve 10/7/80 Reactor Building 2-RB-37.2A RBCCW Header "B" Rebuilt motor operator Closed Cooling Water Containment Iso. Valve 4
10/8/80 Main Feedwater 2-FW-5A #1 Steam Generator Main Rebuilt valve operator feed air operated check valve 10/10/80 Reactor Coolant Pressurizer Safety Valves Rebuilt, tested and reinstalled 2-RC-200 and 2-RC-201 10/13/80 Chemical & Volume P-18B Charging Pump Repacked pump.
Control 10/17/80 120 Volt Vital INV. -3 Inverter Replaced failed voltage sensor regulated instrument A.C.
Docket No. 50-336 Page 2 of 2 Date 12/11/80 Unit Name Millstone 2 Completed By G.II. Ilowlett Telephone (203) 447-1791 X364 CORRECTIVE MAINTENANCE
SUMMARY
FOR SAFETY RELATED EQUIPMENT Report Month October 1980 DATE SYSTEM COMPONENT MAINTENANCE ACTION 10/28/80 Chemical & Volume P-18A Charginq Pump Repacked pump Control 10/31/80 Chemical & Volume P-19A Boric Acid Pump Replaced bearings Control 4