05000334/LER-1980-063-01, /01T-0:on 800908,overstress Condition Found to Exist on 1C Charging Pump Discharge Line During Seismic Event.Cause Unknown.Pipe Support Mods Will Be Completed Before Startup

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/01T-0:on 800908,overstress Condition Found to Exist on 1C Charging Pump Discharge Line During Seismic Event.Cause Unknown.Pipe Support Mods Will Be Completed Before Startup
ML19343A165
Person / Time
Site: Beaver Valley
Issue date: 09/09/1980
From: Lacey W
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19343A163 List:
References
LER-80-063-01T, LER-80-63-1T, NUDOCS 8009160313
Download: ML19343A165 (2)


LER-1980-063, /01T-0:on 800908,overstress Condition Found to Exist on 1C Charging Pump Discharge Line During Seismic Event.Cause Unknown.Pipe Support Mods Will Be Completed Before Startup
Event date:
Report date:
3341980063R01 - NRC Website

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Attachment To LER 80-63/01T Beaver Valley Power Station Duquesne Light Company Docket No. 50-334 No further information is available or needed to satisfy the reporting requirements.