LER-1981-008, /03L-0:on 810127,345 Kv Switchyard Bus K Tripped & Locked out,de-energizing Startup Transformer 02.Caused by Action from Directional Ground Current Relay & Charred Phase Lightning Arrestor C on Startup Transformer |
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60 E% ENT DATE 74 7b HEPoH T DAT E BJ EVENT DESCRIPTION AND PROB ADLE CONSEQUENCES h c l 2 l l(NP-33-81-08) On 1/27/81 at 2222 hours0.0257 days <br />0.617 hours <br />0.00367 weeks <br />8.45471e-4 months <br />, the 345 KV switchyard bus "K" tripped and
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TOLEDO EDISON COMPANY j
DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-81-08 DATE OF EVENT: January 27, 1981 and February 1, 1981 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE:
Loss of Startup Transformer #02 in Mode 5 and Loss of Startup Transformer #01 in Mode 3 Conditiona Prior to Occurrence: The unit was in Mc3e 5 with Power (MRT) = 0 and Load (Gross MWC) = 0.
Description of Occurrence: On January 27, 1981 at 2222 hours0.0257 days <br />0.617 hours <br />0.00367 weeks <br />8.45471e-4 months <br />, 345 KV switchyard bus K tripped and Jocked out, de-energizing Startup Transforer 02 and causing the station 13.8 KV bus being powered by Startup Transformer 02 to fast transfer to Startup Transformer C10 Being in Mode 5 the station did not enter the action statement of Technical Speci-fication 3.8.1.2 which requires the operability of only one circuit between the of fsite transmission network and the onsite Class lE distribution system. These requirements were being met.
On February 1, 1981 at 0620 hours0.00718 days <br />0.172 hours <br />0.00103 weeks <br />2.3591e-4 months <br />, a very similar instance occurred in which "J" bus tripped and locked out, de-energizing Startup Transformer 01 and causing the station
- 1. O KV bus A to fast transfer to Startup Transformer 02.
Being in Mode 3, the station entered the action statement of Technical Specification 3.8.1.1 which requires the opera-bility of two independent circuits between the offsite transmission network and the onsite Class lE distribution system. The action statement requires that within one hour the correct breaker alignments and indicated power availability be verified. This must be re-verified every eight hours thereafter until both circuits are restored to operable status. These requirements were met.
Designation of Apparent Cause of Occurrence:
Investigation by maintenance personnel revealed that the K bus trip had occurred due to action from a directional ground currnnt relay and that the "C" phase lightning arrester on Startup Transformer 02 appeared charred.
Subsequent testing verified that the lightning arrester was in fact damaged and shorted.
This could have been caused by an internal failure or from being struck by a bolt of lightning or electrical surge.
In the cause of the Startup Transformer 01 trip, testing determined that the "B" phase lightning arrester had faulted. There was no visible evidence of the fault.
It should be noted here that the weather was similar at the time of both occurrences.
In both instances the weather was snowy and wet.
Analysis of Occurrence: There was no danger to the health and safety of the public or to station personnel.
In both cases there was an automatic transfer of loads to the operabic startup transformer.
LER #81-008
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r TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-81-08 PACE 2
Corrective Action
Under Maintenance Work Order (IMO) 81-1400 the failed lightning arrester on Startup Transformer 02 was removed. The 02 Transformer was returned to service at 2331 hours0.027 days <br />0.648 hours <br />0.00385 weeks <br />8.869455e-4 months <br /> on January 28, 1981 without the lightning arrester.
Under MWO 81-1426, the failed lightning arrester on Transformer 01 was removed, and the transformer was returned to service at 1920 hours0.0222 days <br />0.533 hours <br />0.00317 weeks <br />7.3056e-4 months <br /> on February 1, 1981.
These actions were taken pending receipt of replacement parts.
Installation of new lightning arresters was done under Facility Change Request 81-050.
On February 7, 1981 the 02 Transformer was removed from service to install new lightning arresters. The work was completed and 02 again returned to service at 1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br /> on February 7, 1981. On February 8, 1981, the 01 Transformer was removed from service to install new lightning arresters.
The work was completed and 01 again i
returned to service at 1540 hours0.0178 days <br />0.428 hours <br />0.00255 weeks <br />5.8597e-4 months <br /> on February 8, 1981.
Failure Data: There have been no previous similar occurrences.
LER #81-008 t
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| 05000346/LER-1981-001, Forwards LER 81-001/01X-1 | Forwards LER 81-001/01X-1 | | | 05000346/LER-1981-001-01, /01X-1:on 810107,discovered Contractor Personnel on 801204 Disassembled Restraints Other than Those Requested & Failed to Perform Reassembly in Timely Manner. Caused by Inadequate Procedural Control | /01X-1:on 810107,discovered Contractor Personnel on 801204 Disassembled Restraints Other than Those Requested & Failed to Perform Reassembly in Timely Manner. Caused by Inadequate Procedural Control | | | 05000346/LER-1981-002-03, /03L-0:on 810102,reactor Coolant Pump 1-2 Was Shutdown Due to High Seal Return Temp & Deteriorating Seal Staging & on 810106,pump 2-1 Was Shutdown for Deteriorating Seal Staging.Caused by Seal Degradation.Seals Replaced | /03L-0:on 810102,reactor Coolant Pump 1-2 Was Shutdown Due to High Seal Return Temp & Deteriorating Seal Staging & on 810106,pump 2-1 Was Shutdown for Deteriorating Seal Staging.Caused by Seal Degradation.Seals Replaced | | | 05000346/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000346/LER-1981-003-03, /03L-0:on 810106,breaker HX02B Tripped, de-energizing Bus B Which Reduced Electrical Distribution Less than Tech Specs Required.Caused by Personnel Error. Breakers Restored.Operators Counselled Re Attentiveness | /03L-0:on 810106,breaker HX02B Tripped, de-energizing Bus B Which Reduced Electrical Distribution Less than Tech Specs Required.Caused by Personnel Error. Breakers Restored.Operators Counselled Re Attentiveness | | | 05000346/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000346/LER-1981-004, Forwards LER 81-004/03X-1 | Forwards LER 81-004/03X-1 | | | 05000346/LER-1981-005-03, /03L-0:on 810114,RCS Chloride Concentration Exceeded Tech Spec Limit.Caused by Use of Spotcheck in Cleaning Reactor Coolant Pump Seal Cavities.Instructions Issued for Use of Solvents in RCS | /03L-0:on 810114,RCS Chloride Concentration Exceeded Tech Spec Limit.Caused by Use of Spotcheck in Cleaning Reactor Coolant Pump Seal Cavities.Instructions Issued for Use of Solvents in RCS | | | 05000346/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000346/LER-1981-006-03, /03L-0:on 810119,power Lost to Safety Features Actuation Sys Channel 1 Cabinet.Caused by Blown Supply Fuse from Panel Y-1 Due to Procedure Deficiency.Fuse Replaced & Procedure Modified | /03L-0:on 810119,power Lost to Safety Features Actuation Sys Channel 1 Cabinet.Caused by Blown Supply Fuse from Panel Y-1 Due to Procedure Deficiency.Fuse Replaced & Procedure Modified | | | 05000346/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000346/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000346/LER-1981-007-03, /03L-0:on 810122,door 306 Found Partially Open,So That Spent Fuel Pool Emergency Ventilation Sys Could Not Have Maintained Area at Correct Pressure.Caused by Maladjusted Door Closure.Maint Work Order Issued | /03L-0:on 810122,door 306 Found Partially Open,So That Spent Fuel Pool Emergency Ventilation Sys Could Not Have Maintained Area at Correct Pressure.Caused by Maladjusted Door Closure.Maint Work Order Issued | | | 05000346/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000346/LER-1981-008-03, /03L-0:on 810127,345 Kv Switchyard Bus K Tripped & Locked out,de-energizing Startup Transformer 02.Caused by Action from Directional Ground Current Relay & Charred Phase Lightning Arrestor C on Startup Transformer | /03L-0:on 810127,345 Kv Switchyard Bus K Tripped & Locked out,de-energizing Startup Transformer 02.Caused by Action from Directional Ground Current Relay & Charred Phase Lightning Arrestor C on Startup Transformer | | | 05000346/LER-1981-009-03, /03L-0:on 810128,diesel Generator 1-2 Could Not Be Started W/Left Side Set of Air Start Motors During Diesel Generator Surveillance Test 5081.01.Caused by Failure of One Air Start Motor Due to Broken Solenoid Drive Shaft | /03L-0:on 810128,diesel Generator 1-2 Could Not Be Started W/Left Side Set of Air Start Motors During Diesel Generator Surveillance Test 5081.01.Caused by Failure of One Air Start Motor Due to Broken Solenoid Drive Shaft | | | 05000346/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000346/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000346/LER-1981-010-03, /03L-0:on 810202,MSIV Bypass Valve Ms 100 a Failed to Close.Probably Caused by Component Failure.Actuator Spring Adjusted to Increase Tension Until Valve Would Close | /03L-0:on 810202,MSIV Bypass Valve Ms 100 a Failed to Close.Probably Caused by Component Failure.Actuator Spring Adjusted to Increase Tension Until Valve Would Close | | | 05000346/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000346/LER-1981-011-03, /03L-0:on 810205,post-accident Monitoring Instrument HPI Flow 1-2 Was Declared Inoperable.Caused by Bad Current Buffer.Current Buffer Was Repaired,Recalibr & Reinstalled.Hpi Flow 1-2 Was Returned to Operable Status | /03L-0:on 810205,post-accident Monitoring Instrument HPI Flow 1-2 Was Declared Inoperable.Caused by Bad Current Buffer.Current Buffer Was Repaired,Recalibr & Reinstalled.Hpi Flow 1-2 Was Returned to Operable Status | | | 05000346/LER-1981-012-03, /03L-0:on 810212,control Rod 1-3 Absolute Position Indication Declared Inoperable Due to Fluctuating Signals Causing Asymmetric Rod Alarms.Exact Cause Undetermined,But Absolute Position Indication Leads Picking Up Noise | /03L-0:on 810212,control Rod 1-3 Absolute Position Indication Declared Inoperable Due to Fluctuating Signals Causing Asymmetric Rod Alarms.Exact Cause Undetermined,But Absolute Position Indication Leads Picking Up Noise | | | 05000346/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000346/LER-1981-013-03, /03L-0:on 810218,control Room Normal Ventilation Dampers Tripped Shut Resulting in No Power Available to Chlorine Detector 1 Above Control Room or in Block House. Caused by Failure of 10 Amp Fuse of Circuit Y111 | /03L-0:on 810218,control Room Normal Ventilation Dampers Tripped Shut Resulting in No Power Available to Chlorine Detector 1 Above Control Room or in Block House. Caused by Failure of 10 Amp Fuse of Circuit Y111 | | | 05000346/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000346/LER-1981-014-03, /03X-1:on 810226,decay Heat Valve 64 Would Not Open During Testable ECCS Valves Quarterly Test.Caused by Loose Set Rod Bushing,Allowing Gear Box Set Rod to Move Which Unlocked Limit Switches from Adjusted Position | /03X-1:on 810226,decay Heat Valve 64 Would Not Open During Testable ECCS Valves Quarterly Test.Caused by Loose Set Rod Bushing,Allowing Gear Box Set Rod to Move Which Unlocked Limit Switches from Adjusted Position | | | 05000346/LER-1981-014, Forwards LER 81-014/03X-1 | Forwards LER 81-014/03X-1 | | | 05000346/LER-1981-015-03, /03L-0:on 810227,access Door 107 Found Propped Open from ECCS 2 Pump Room 115 to Miscellaneous Waste Monitor Tank & Pump Room 114.Caused by Failure to Follow Posted Signs While Clearing Odor from Room | /03L-0:on 810227,access Door 107 Found Propped Open from ECCS 2 Pump Room 115 to Miscellaneous Waste Monitor Tank & Pump Room 114.Caused by Failure to Follow Posted Signs While Clearing Odor from Room | | | 05000346/LER-1981-015, Forwards LER 81-015/03L-0 | Forwards LER 81-015/03L-0 | | | 05000346/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000346/LER-1981-016-03, /03L-0:on 810308,dose Equivalent I-131 Level Exceeded Tech Spec Limit.Caused by Gas Leakage Through Fuel Cladding.Levels Monitored | /03L-0:on 810308,dose Equivalent I-131 Level Exceeded Tech Spec Limit.Caused by Gas Leakage Through Fuel Cladding.Levels Monitored | | | 05000346/LER-1981-017-03, /03L-0:on 810309,train 2 Hpi/Low Pressure Injection cross-connect Isolation Valve Dh 63 Would Not Open from Control Room During Quarterly Valve Surveillance Test 5051.13.Caused by Faulty Torque Switch in Valve Operator | /03L-0:on 810309,train 2 Hpi/Low Pressure Injection cross-connect Isolation Valve Dh 63 Would Not Open from Control Room During Quarterly Valve Surveillance Test 5051.13.Caused by Faulty Torque Switch in Valve Operator | | | 05000346/LER-1981-017, Forwards LER 81-017/03L-0 | Forwards LER 81-017/03L-0 | | | 05000346/LER-1981-018-03, /03L-0:on 810322 & 0401,chlorine Detector Ae 5358B Tripped.First Trip Probably Caused by Fouled Detector. Detector Cleaned.Detector & Circuit Board Replaced After Second Failure | /03L-0:on 810322 & 0401,chlorine Detector Ae 5358B Tripped.First Trip Probably Caused by Fouled Detector. Detector Cleaned.Detector & Circuit Board Replaced After Second Failure | | | 05000346/LER-1981-018, Forwards LER 81-018/03L-0 | Forwards LER 81-018/03L-0 | | | 05000346/LER-1981-019-03, /03L-0:on 810323,fluctuating Signals W/Numerous Asymmetric Rod Alarms Received,Resulting in Control Rod 4-7 Absolute Position Indication Inoperability.Probably Caused by Electrical Penetration Module Deficiency | /03L-0:on 810323,fluctuating Signals W/Numerous Asymmetric Rod Alarms Received,Resulting in Control Rod 4-7 Absolute Position Indication Inoperability.Probably Caused by Electrical Penetration Module Deficiency | | | 05000346/LER-1981-019, Forwards LER 81-019/03L-0 | Forwards LER 81-019/03L-0 | | | 05000346/LER-1981-020-03, /03L-0:on 810324,valve CV5011A,on Containment Air Sample Inlet Line to Hydrogen Analyzer,Would Not Stroke Closed W/Monitor Operator.Caused by Badly Worn Tripper in Motor Operator.Tripper Levers Replaced | /03L-0:on 810324,valve CV5011A,on Containment Air Sample Inlet Line to Hydrogen Analyzer,Would Not Stroke Closed W/Monitor Operator.Caused by Badly Worn Tripper in Motor Operator.Tripper Levers Replaced | | | 05000346/LER-1981-020, Forwards LER 81-020/03L-0 | Forwards LER 81-020/03L-0 | | | 05000346/LER-1981-021-03, /03L-0:on 810401,half Trip Occurred from Steam & Feedwater Rupture Control Sys Channel 1 Low Steam Generator Level Trip.Caused by Power Supply Failure.Power Supply Replaced Per Work Order on 810402 | /03L-0:on 810401,half Trip Occurred from Steam & Feedwater Rupture Control Sys Channel 1 Low Steam Generator Level Trip.Caused by Power Supply Failure.Power Supply Replaced Per Work Order on 810402 | | | 05000346/LER-1981-021, Forwards LER 81-021/03L-0 | Forwards LER 81-021/03L-0 | | | 05000346/LER-1981-022, Forwards LER 81-022/03L-0 | Forwards LER 81-022/03L-0 | | | 05000346/LER-1981-022-03, /03L-0:on 810316,NRC Site Inspector Reported Finding Four 0.5-inch Holes Through Control Room Equipment Room East Fire Wall.On 810403,two Holes Found in Wall of Room 427B.Caused by Personnel Error | /03L-0:on 810316,NRC Site Inspector Reported Finding Four 0.5-inch Holes Through Control Room Equipment Room East Fire Wall.On 810403,two Holes Found in Wall of Room 427B.Caused by Personnel Error | | | 05000346/LER-1981-023-03, /03L-1:on 810403,decay Heat Cooler Outlet Valve CC1467 Stroked Closed During Component Cooling Water Monthly Test & Would Not Reopen.Caused by Excessive Wear on Actuator Due to Design Deficiency.Actuator Rebuilt | /03L-1:on 810403,decay Heat Cooler Outlet Valve CC1467 Stroked Closed During Component Cooling Water Monthly Test & Would Not Reopen.Caused by Excessive Wear on Actuator Due to Design Deficiency.Actuator Rebuilt | | | 05000346/LER-1981-023, Forwards LER 81-023/03L-1 | Forwards LER 81-023/03L-1 | | | 05000346/LER-1981-024, Forwards LER 81-024/03L-0 | Forwards LER 81-024/03L-0 | | | 05000346/LER-1981-024-03, /03L-0:on 810418,bus J Was Rapidly Taken Out of Svc W/O Providing for Alternate Power Supply for Decay Heat Pump 1-1.Caused by Personnel Error.Procedure Modified & Operator Informed of Mods | /03L-0:on 810418,bus J Was Rapidly Taken Out of Svc W/O Providing for Alternate Power Supply for Decay Heat Pump 1-1.Caused by Personnel Error.Procedure Modified & Operator Informed of Mods | | | 05000346/LER-1981-025, Forwards LER 81-025/03L-0 | Forwards LER 81-025/03L-0 | | | 05000346/LER-1981-025-03, /03L-0:on 810423,during Review of Safety Tagging Log,Unit Entered Mode 4 W/O Required Two Makeup Pumps Operable.Caused by Personnel Error.Pumps Restored to Operation.Personnel Reinstructed in Procedures | /03L-0:on 810423,during Review of Safety Tagging Log,Unit Entered Mode 4 W/O Required Two Makeup Pumps Operable.Caused by Personnel Error.Pumps Restored to Operation.Personnel Reinstructed in Procedures | | | 05000346/LER-1981-026-03, /03L-0:on 810428,reactor Protection Sys Channel 1 Tripped on Flux/Delta Flux/Flow.Caused by Failure of Flow Differential Pressure Transmitter Primary Power Transformer Shorting to Ground.New Amplifier Installed & Calibr | /03L-0:on 810428,reactor Protection Sys Channel 1 Tripped on Flux/Delta Flux/Flow.Caused by Failure of Flow Differential Pressure Transmitter Primary Power Transformer Shorting to Ground.New Amplifier Installed & Calibr | |
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