LER-1980-059, /03L-0:on 801215,discovered That Main Station & Diesel Generator Monthly Battery Surveillance Tests Not Performed as Scheduled on 800801 & 1121.Caused by Personnel Error.Administrative Controls Implemented |
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l NRC FCCM 364 U. S. NUCLEAR RE%UI.ATORY COMMISSION
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NAME OF *aE8ARER PMCNE:
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7 OYSTER CREEK NUCLEAR GDERATING STATICN Forked River, New Jersey 08731 Licensee Event Beport Reportable Occurrence No. 50-219/80-59/3L Report Date January 15, 1981 occu&io ce Date December 15, 1980 Identification of ner,ui=ce Violation of the Technical SF fications, sections 4.7.A.5 and 4.7.B.2 when the monthly surv=ilianca tests for the Main Statico and Diesel Generator starting batteries were not pe&fmoi for the month of Novencer.
Durire the investigaticn it m also ecnfim=ri that the monthly survaillance tests for the Diesel Generator and Main Station batteries were also not peformed on August 1, 1980 as required.
This event is considered to be a t e si.able occurrence as defined in the Tachnical F4 F4 cations, paragraph 6.9.2.b. (3).
Conditions Prior to Occi.u.i=ce 21e plant was operating at steady state power until about 2200 hours0.0255 days <br />0.611 hours <br />0.00364 weeks <br />8.371e-4 months <br /> on Novenber 21, 1980 at which time a reactor shutdown was ccmnenced for reasons unrelated to this event. Major plant pat==i.crs for that day were:
Power:
Core 1930 MM:
Electrical 630 MWe 4
Flow:
Recirculation 15.3 x 10 p Faarkater 7.07 x 106 lb/hr Da= -intion of occurrence
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On Monday, nacs=hal 15, 1980, during a review of the Master Survai11anca Schedule it was discovered that the Diesel Generator Ltnthly Bat 9_ry Survaillanca (Plant Procedure 636.2.006) and Main Statica Mcnthly Battery Survaillanca (Plant Procedure 634.2.003) were not performed as scheduled for the ucnth of Novenber.
The tests were scheduled to be pe&f-=d en Neverber 21, 1980. Die ::enthly battery checks were previously Muu=1 on Cui.ei.+c 24, 1980 but not done again until Decenber 19, 1980. During a review of the recards it was also ennfim=ri that the ucnthly battery checks were also not pm.few =1 within the required interval in Aucust 1980.
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Reportable Occurrenm Page 2 Report No. 50-219/80-59/3L Apparent Cause of Occw.4=s The cause of the occurrence is attributed to pw.muual er:or. The tests were inadvertently overlooked by the pa m nnal r w sible for performing the tests and the supervisor did not have a positive means of ensuring that all survai11ance
.t tests were performed when dar%1ed.
j Analysis of occuti= s
'Ihe manufacturer's instructions for battery care rm-4 that written records be kept to follow the performance of batteries. 'Ihis type of survaillance has been dennstrated through avnariance to provide an indication of a cell hamming irregular or unserviceable long before it t+2 - em a failure. The batteries will deteriorate with time, but precipitous failure is unlikely. 'Ihe Tec.5u'ical Apaci*ications required that the voltage of each battery cell be measured nonthly. 'Ibe weekly battery tests, which were peifw.u=:d as scheduled, require the measurement of the pilot cell voltage and total battery voltage. A review of the data recorded on the weekly tests indicated no obvious dam =dation in the overall condition of the batteries. In addition, the monthly battery checks performed in the follow 2ng acnths indicated all the individual cell voltages were within acceptable limits.
Corrective Action
'Ihe electrical department reviewed the bidant with their personnel and stressed the importance of pm.fw.uu.ng all - W survaillanca testing within the Tari#ied intervals. In addition, the department has inplemented practices to ensure the situation does not recur. 'Ihese practices include:
1.
A copy of the survaillanca schadnla will be maintained and signed cff by the aes w. late supervisor when receiving the a:npleted documenc.
c 2.
The appropriate supervisor will review the survaillanca testing require-ments due for the week in advance with the person responsible to perform the test.
3.
An end of the week verification by the appuriate supervisor will be pw1&asizi to assure c:Epletion of all scheduled surveillance tests.
Failure Data Not applicable.
Previous Similar Events
LER 50-219/80-012 l
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