05000334/LER-1980-114-03, /03L-0:on 801215,during Shift Channel Check of Refueling Water Storage Tank,Channel C Level Indicator Found Reading High.Caused by Transmitter Zero Drift. Transmitter Recalibr & Returned to Svc

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/03L-0:on 801215,during Shift Channel Check of Refueling Water Storage Tank,Channel C Level Indicator Found Reading High.Caused by Transmitter Zero Drift. Transmitter Recalibr & Returned to Svc
ML19341A208
Person / Time
Site: Beaver Valley
Issue date: 01/14/1981
From: Lacey W
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19341A205 List:
References
LER-80-114-03L, LER-80-114-3L, NUDOCS 8101220387
Download: ML19341A208 (2)


LER-1980-114, /03L-0:on 801215,during Shift Channel Check of Refueling Water Storage Tank,Channel C Level Indicator Found Reading High.Caused by Transmitter Zero Drift. Transmitter Recalibr & Returned to Svc
Event date:
Report date:
3341980114R03 - NRC Website

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CON'T 40 el DOCKET NVueER nd 69 EN ENT DATE 34 PS REPORT DATE 80 EVENT DESCRtPTION ANO PROe AOLE CONSEQUENCES h Q l At 0730 hours0.00845 days <br />0.203 hours <br />0.00121 weeks <br />2.77765e-4 months <br /> during the scheduled shif t channel check of the Refueling Water l

g l Storane Tank (RWST) Icvel indicators, the channel C level indicator was found

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It was declared inoperable and power operation continued in l

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The health and s,1fety of the

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Attachment To I.ER 80-114/03L Beaver Valley Power Station Duquesne Light Company Docket No. 50-334 I

No further information is available or needed to satisfy the reporting requirement.

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