05000271/LER-1980-042-03, /03L-0:on 801211,control Rod Block Was Not Received as Required Per Tech Spec.Caused by Arm on GE Limit Switch Model CR-1156 Working Loose & Being Bent by Platform.Arm Straightened & Tightened

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/03L-0:on 801211,control Rod Block Was Not Received as Required Per Tech Spec.Caused by Arm on GE Limit Switch Model CR-1156 Working Loose & Being Bent by Platform.Arm Straightened & Tightened
ML19340E789
Person / Time
Site: Vermont Yankee File:NorthStar Vermont Yankee icon.png
Issue date: 01/12/1981
From: Murphy W
VERMONT YANKEE NUCLEAR POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19340E787 List:
References
LER-80-042-03L, LER-80-42-3L, NUDOCS 8101150685
Download: ML19340E789 (1)


LER-1980-042, /03L-0:on 801211,control Rod Block Was Not Received as Required Per Tech Spec.Caused by Arm on GE Limit Switch Model CR-1156 Working Loose & Being Bent by Platform.Arm Straightened & Tightened
Event date:
Report date:
2711980042R03 - NRC Website

text

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s aeCaTOArs ao E3caipr:CN ANO 8ACSASLE 00NSECUENCE3 h EvENr Ia+:I l Durine refueline coerations when the refueline clatform was moved ever the core withi laia!I a fuel assembiv en the hoist, a control red block was not received as reOutred bv la!Ai !T S.

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l,alI repair, the refueline interlocks were tested satisfactorilv. The limit switch is I

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