05000334/LER-1980-067-01, /01T-0:on 800912, Determined That Branch Line of 24-inch Reactor Plant Component Cooling Water Header Will Be Subj to Overstress During Seismic Event.Caused by Dead Weight & DBE Loading Factors

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/01T-0:on 800912, Determined That Branch Line of 24-inch Reactor Plant Component Cooling Water Header Will Be Subj to Overstress During Seismic Event.Caused by Dead Weight & DBE Loading Factors
ML19338E070
Person / Time
Site: Beaver Valley
Issue date: 09/17/1980
From: Lacey W
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19338E067 List:
References
LER-80-067-01T, LER-80-67-1T, NUDOCS 8009240461
Download: ML19338E070 (2)


LER-1980-067, /01T-0:on 800912, Determined That Branch Line of 24-inch Reactor Plant Component Cooling Water Header Will Be Subj to Overstress During Seismic Event.Caused by Dead Weight & DBE Loading Factors
Event date:
Report date:
3341980067R01 - NRC Website

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'N NRC FORM 384 U. S. NUCLEAA REGULATORY COMMISSION i

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,. Io12l l It has been determined that an overs' tress condition exists'at a two (2) inch

__j c o ;3l l branch line off the 24 inch reactor plant component cooling water header during a l

lo#Ai l design basis earthquake. Consequences of the loss of this line would lead to a l

L i o, s 1 l los's of Residu:rl Heat Removal (RHR) because of the need to isolate the whole l

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Attachment To LER 80-67/01T-Beaver Valley Power Station Duquesre Light Company Docket No. 50-334 No further information is available or needed*to satisfy the reporting requirement.

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