05000334/LER-1980-065-01, /01T-0: on 800912,determined That Both River Water Supply Lines Will Be Subj to Overstress During Seismic Event.Caused by Dead Weight & DBE Loading Factors.Corrective Actions Underway

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/01T-0: on 800912,determined That Both River Water Supply Lines Will Be Subj to Overstress During Seismic Event.Caused by Dead Weight & DBE Loading Factors.Corrective Actions Underway
ML19338E068
Person / Time
Site: Beaver Valley
Issue date: 09/17/1980
From: Lacey W
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19338E067 List:
References
LER-80-065-01T, LER-80-65-1T, NUDOCS 8009240456
Download: ML19338E068 (2)


LER-1980-065, /01T-0: on 800912,determined That Both River Water Supply Lines Will Be Subj to Overstress During Seismic Event.Caused by Dead Weight & DBE Loading Factors.Corrective Actions Underway
Event date:
Report date:
3341980065R01 - NRC Website

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[ o_[.2,j lIt has been determined that an overstress condition exists ar one location on each I

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Attachment To LER 80-65 /01T Beaver Valley Power Stat ion Duquesne Light Company Docket No. 50-334 No furthur information is available or needed tra sati'.fy the reporting requirement.

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