05000219/LER-1980-036-03, /03L-0:on 800815 & 16,stack Releases Were Not Continuously Monitored Due to Failure of Stack Gas Sample Sys.Caused by Loose Motor Cooling Fan on Sample Pump B. Sample Pump Filter Replaced & Motor Cooling Fan Tightened

From kanterella
(Redirected from ML19338D580)
Jump to navigation Jump to search
/03L-0:on 800815 & 16,stack Releases Were Not Continuously Monitored Due to Failure of Stack Gas Sample Sys.Caused by Loose Motor Cooling Fan on Sample Pump B. Sample Pump Filter Replaced & Motor Cooling Fan Tightened
ML19338D580
Person / Time
Site: Oyster Creek
Issue date: 09/15/1980
From: Ross D
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19338D578 List:
References
LER-80-036-03L, LER-80-36-3L, NUDOCS 8009230488
Download: ML19338D580 (3)


LER-1980-036, /03L-0:on 800815 & 16,stack Releases Were Not Continuously Monitored Due to Failure of Stack Gas Sample Sys.Caused by Loose Motor Cooling Fan on Sample Pump B. Sample Pump Filter Replaced & Motor Cooling Fan Tightened
Event date:
Report date:
2191980036R03 - NRC Website

text

NMC FGHM 066 U.3. NUCLEAR REGULATORY COMMISSt%N '

i c:m i

,' LICENSEE EVENT REPORT

- O co~'=o' 'oc = i i

i i

i,io

~

'~' c,'v

> " c ="

='~ = >" :~'

Io ! t l lN IJ l0 lC lP l1 l@l 0 l 0 l -} O l 0 l 0 l 0 l 0 l - l 0 I O (@ 4 l 1 l 1 I 1 l 1 (@l l

l

$7 CAT 54@

7 8 9 UCEf43EE CODE 14 13 UCENSENUMSER 25 26 UCENSE TYPE JO CONT Iol8I l L @l Ol S l 0 l 01 O l 2 l -1 l 9 @l 0 l 8 l 1 l 5 l 8 l 0 l@l 0 l 9 l I ! S I 8 l O l@

seuRC I

tiQ 61 COCXET NUMS E A as 69 EVENT CATE 74 75 REPCRT C ATE 80 EVEN T CESCRIPTION AND PRCSA8LE CONSEQUENCES h t o I:l l On August 15, 1980 and again on August 16, 1980, a limitine condition l

t o tal l for operation as per T.S.3.6.A.3 was exceeded when stack releases were l

?

g o i4; ;

not continuously monitored due to failure of the stack gas sample system.

I c,

lo 1s1 ;

'In both incidents, stack gas sample pump "B" tripped on thermal overload.

I t C r,7 i Sample pump "B" was returned to service af ter the first trio but af ter I

+

i gg ;_ the second trip, system operation was restored bv olacine oumo "A" in I

i06aii service. Gaseous releases to the stack were normal durine the event.

I si sc

$YsTEW

CAUsE

CAusE CCMP.

VALVE 0002 COCE susCO 2 CO*.tPONE!;T OCDE sus:005 sus::. E

!aisi i Bi B l@ I x f@ I z l@ la 10 lT l0 la lx l@ I z i@ L;Ll@

J 3

10 11 12 IJ 18 79 20 sEOUENTIAL CCCURRENCE ME*CRT 95Vis3CN

_ EVENT YEAR

@ ;gga aC I 81 of L-h!

I o l 31 61 1-1 I ol 3I LLI l-1 L2J

.EP.g R EPCRT NQ.

COCE TYPE NO.

_ 21 22 23 24 26 27 28

.7 20 at 32 Ahc Hourts h s e tN 7

N C P T

M sC S.

sVP L MA UA PER

}Bl@lFl@

l B l@

lAl@

l 01 Ol 0l 1l l Yl@

l N I@

l Nl@

lGl0l4l6l(

22 24 2s se 33 40 4i 42 42 u

47 CAUSE DESCRl8TICN AND CORRECTIVE ACTIONS @

litol l The cause of this event was a loose motor cooling fnn nn enm1, m - un" l

Ii t i i l The stack eas samole eumo filter was ren1ntnd nnd cha m em-re n1 %.

cm I

Thie installation of a new Radioactive Caseous Effluents gl was tightened.

I i,i3i l Monitoring System, to be comoleted bv January 1981 is expected to sub-I ii i4 3 l-stantially improve the raliability of the Stack Gas Monitorine Svs tem.

I 7

ss so T

sPowEm oTMR sTA EsEc7EEY

's^f2'E oiscovtaY mEsCn PTroN l1 l5 I [ E l@ l 0l 9l 4l@l NA l

l A l@l Ooerator observation l

7

.,g,, y u

n s

=

4

.o l i 1 s 1 l z l @e l zl@lAucuNTe, ACTiviTv @ l LcCATicN cP uuA E @

nuAst P nuAst NA l

NA I

7 3 3 to 3

44 45

  • ERSCNNEL EXPosumEs 30 NUMBER TY8E CEsCMIPTTON lt l 71 l 0 l 0 l 0 l@l z l@l NA l

PE#sCMNE L INJU Es NUMstm ESCRIPTICN 11 141l0l0l0l@l NA l

7 8 9 11 32 i LCss C8 Om OAV4CE To AAcal.:TY 80 Tw*t CEsC9t*Tso% \\

y LLL*Jl l@l

'i NA I

7 e-9 10 80 l

.gsu g 3E CAlpTION s'

iILI_l61 i:

e NA I

IfIll'ill'li 1

8.9 to 65 69 EG. ;

NAME OF *CE8ARER Donald A. Ross

~0 S.

~

PwcNE:

8009230 M

o.

o dOOkb EO0 Jersey Central Power & Ught Company Madison Avenue at Punch Bowl Road Momstown, New Jersey 07960 (201)455-8200 OYSTER CREEK NUCLEAR GENERATING STATION Forked River, New Jersey 08731 Licensee Event Report Reportable Occurrence No. 50-219/80-36/3L p ort Date Septed er 15, 1980 Occurrence Date August 15, 1980 Identification of Occurrence Exceeding a limiting condition for operations as per the Technical Specifications, paragraph 3.6.A.3, failure of the stack gas sample system to continuously monitor stack releases.

This event is considered to be a reportable occurrence as defined in the Technical Specifications, paragraph 6.9.2.b. (2).

Conditions Prior to Occurrence The plant was operating at steady state power.

Plant parameters at the time of occurrence were:

Power:

Reactor,1820 Wt Electrical, 590 W e Flow:

Recirculation 15.1 x 10" gpm 6.64 x 106 lb/hr Stack Gas Activity: 696 pCi/sec Description of Occurrence On Friday, August 15, 1980, at approximately 1730 hours0.02 days <br />0.481 hours <br />0.00286 weeks <br />6.58265e-4 months <br /> a Stack Gas Sample Line Low Flow alarm was received in the control room. An operator was sent to investi-gate the problem.

Subsequently, the "B" stack gas sample pump tripped at which time a reactor shutdown was commenced. The pump thermal overload protection was reset but the sample flow was still low. At 1834 hours0.0212 days <br />0.509 hours <br />0.00303 weeks <br />6.97837e-4 months <br />, the pump filter was changed and the "B" pump returned to service at which time the sample flow returned to normal. At that time the reactor shutdown was terminated. At 0030 on August 16, the "B" stack gas sample pump tripped again on thermal overload.

Upon investigation the "B" pump motor was found to be very hot.

Subsequently, "A" stack gas sample pump was placed in service and system operation returned to normal.

Jersey Central Power & Ught Company is a Member of the General Public Utihties System

~ '.

1

.i.

Repo'rtable Occurrence 18o.! 50-219/80-36/3L -

Page 2 s>

y -4 september 15, 1980 i

fif Subsequent investigation revealed that the "B" pump motor cooling fan had become t

i loose which was causing the motor to overheat due to insufficient cooling air flow..

Apparent Cause of Occurrence The appahent hause o'f this occurrence was a' loose cooling fan on the motor of sample pump "B'.'.

Overheating caused the pump to trip on thermal overload.

s Analysis of Occurrence.

n A review of the stack gas radiation monitor recorder. traces showed the levels in both monitor channels to be constant (at 200 cys) befora and after this event.

In a further effort to determine if excessive ' stack releases might have occurred during the time that both ' stack gas sample pumps were not operating, recorder traces of radiation monitoring systems associated with two gaseous streams released through the stack were reviewed. The. reactor building ventilation exhaust radiation monitor recorder traces showed that the levels in both channels were relatively constaat,with no spiking during the time of this event. Also, the recorder trac 6 for the Augmented Off Gas System effluent monitor showed that radiation. levels were' constant during the period involved. Based on these con-siderations,f the safety significance of this event is considered minimal.

Corrective Action

The stack gas sample pump filter was replaced and the motor cooling fan was retightened. The installation of a new Radioactive Gaseaus Effluents Monitor-ing System, to be complete by January 1981, is expected to substantially improve the accuracy and reliability of the Stack Gas Monitoring System.

Failure Data i

. Gast Manufacturing Company Model 2-065-V2 Serial (167-154906 i

y e

+

t b

.b

)

s.

8

" -.g N'

j