ML19338D496
| ML19338D496 | |
| Person / Time | |
|---|---|
| Site: | Fort Calhoun |
| Issue date: | 09/08/1980 |
| From: | Hickle B OMAHA PUBLIC POWER DISTRICT |
| To: | |
| Shared Package | |
| ML19338D495 | List: |
| References | |
| NUDOCS 8009230351 | |
| Download: ML19338D496 (9) | |
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AVERAGE DAILY UNIT POWER LEVEL 50-285
. DOCKET NO.
Fort Calhoun #1
. 3.iT DATE September-8,~1980 CONSPI.ETED BY
~B. J. Hickle TELEPIIONE _(402)536-4413 MONE August, 1980
' DAY AVERAGE DAILY POWER LEVEL DAY.
AVER AGE DAILY POWER LEVEL t-
. (MWe-Net)
(MWe-Net) 434 435 37 2
433 435 is 3
433 432 39 4
434 432 20 3
434 431 21 6
434 431 22 7A.
433 434 23 s.
431-435 24 9
431 435 25 to
'432 26 433
.ti 433 434 27 L12.
433~
28 437 13
'433 436-29 14-434-435 30 i'
-- 15 ;
434 435 a
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'434
. INS 1 RUCTIONS O, this format, list the aserage daily unit power level in MWe Net for each day in the reporting nonth. Compute io
. the nearest whole megawatt.
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.8009230'351 I
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OPERATING DATA REPORT
- DOCKET NO; 50-285-
' DATE Septemoer 8,' 1980 '
~
COMPLETED BY-B. J. Hickle.
- TELEPilONE (402)53T-4413
> OPERITING STATU}
FortiCalhoun #1 Notes I. Unit Name:
- 2. Reporting Period:. -August, 1980-1420 2 3. Licensed Thermal Power (MWt):
- 4. Namepu.. ;.ing (Gross MWe):-
502-457
- 5. Design Electrical Rating (Net MWe):.
- 6. Maximum Dependable Capacity (Gross MWe)': 401 7/ Maximum Dependable Capacity (Net MWe):
'457
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
N/A
- 9. Power LevelTo Which Restricted,1f An Net' MWe):
N/A
~
- 10. Reasons For Restrictions.lf Any:
2.
This Month Yr. to-Date Cumulative
.744.0 5,855.0 60,792.0
- 11. Ilours in Reporting Period
- 12. Number Of flours Reactor Was Crit' cal 744'.0 2,449.1--
46,850.7
- 13. Reactor Reserve Shutdown flours 0.0 0.0 1,30925
- 14. Ilours Generator On-Line 744.0 2.387.3-45;838.4
- 15. Unit Resene Shutdown Hours.-
0.0 0.0-0.0-
- 16. Gross Thermal Energy Generated (MWH) 1,049,152.6 3,166,746.3:
56,401,725.6-
- 17. Gross Electrical Energy Generated (MWH) 339.426.0 1.027,932.0
_18,688,161.6 18.- Net Electrical Energy Generated (MWH) 322,571.2 974,199.0 17,661,718.8
- 19.. Unit Senice Factor 100.0-40.8 75.4-20." Unit A'vailability Factor ;
100.0 40.8-
- 75.4.
. 21. Unit Capacity Factor (Using MDC Net). -
94.9__
36.4 64.0-g 22.' Unit Capacity Factor (Using DER N' t).
94.9-36.4 63.6 e
23.' Unit Forced Outage Rate 0.0 0.4 4.3
- 24. Shutdowns Schedu?ed Over Next 6 Months (Type. Date,and Duration of Eacht
Nnno -
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? 25. If Shut'Down At End Of Report Period. Estimated Da' te of Startup:
N/A
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- 26. Units in Test Status (Prior to Commercial Operation):
Forecast Achieved INITIAL CRITICALITY.
INITIAL ELECTRICITY
~, COMMERCI L OPERATION -
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f Refuclingilnihr.etition =
- Fort ^Calhoun?--Unit No. 1
- Reportifor1thenonth' ending August 31,l1980.-
September-15,-1981 1.J Scheduled <date for nes:t' refueling. shutdown.
- 2. i Scheduled date for restart follwing refueling.
November 15, 1981
- 3., 'Will; refuelingfor resumption of operation thereafter
- require altechnical specification change or other No
-licenseJanendment?
, ' a.: ; If' answer is yes, what, ~in general,;will
.these be?'
- b. 'If answer is no, has the reload fuel design and core configuration been reviewed by your Plant Safety Review Comnittee to deter-mine whether any unreviewed safety. questions NO are associated withLthe core reload.
If no such review has.taken place, when is
- c.
September 1,'1981 it scheduled?
4.
Scheduled-date(s)" for submitting proposed licensing :
action ~and support information.
~5.
Important licensing considerations associated with refueling, e.g., inew or different fuel design or supplier, unroviewed design or performance analysis nethods, significant changes in fuel design, new
- operating procedures.
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133 assemblics
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We ntmber of fuel assenblies: a) in the core 6.
b) in the spent-fuel pool 197 c): spent' fuel pool'
. storage capacity 483 r
d)-planned spent fuel' pool storage capacity 483 7.' l'Ihe projected ~datefof: the. last refueling that can be discharged'to ;thejspentifuel pool'asstnting the present 1985 Llicensed capacityn
<? Prepared'by EMM
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. September 5,E1980 Datc~
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OMAHA-PUBLIC POWER DISTRICT.
Fort:Calhoun. Station Unit'No.'1
' August 1980 J
Monthly Operations Report I.
OPERATIONS'SUMARY Fort Calhoun Station' received a license amendment during the month-Lof August which: allowed an. increase 1:s power level'to 1500 MWth. The operations department participated in the review of the operational-readiness of Fort-Calhoun~ Station to increase power-level. Plant
. specific: training was given the Fort Calhoun staff on the expected
. s,r.. tem parameter: and procedure changes which vere required to implement
'tbe-increased power level.
Normal surveillance tests and operational tests were completed with no abnormal results reported.
The unit operated at a nominal 1h20 MWth during the month of August.
Normal six shift training continued during August.
A.
. PERFORMANCE CHARACTERISTICS LER Number Deficiency LER 80-012:
During performance of ST-RPS-3, F.2, it was discovered that Trip Unit #3 (Reactor Coolant Flow) trip setpoints had drifted,out of specifi-cation in the nonconservative direction. Main-tenance: order #6405 was written to investigate the drift.
The R.P.S. was immediately placed in a two-out-of-three logic to trip mode.
Technical Specification 1 3(2) applies.
LER-80-013 During normal power' operation it-vas noted that
-Channel AJDC. sequencer SI-1 had a de-energized "on-auto" light associated with AC-3A, or the i
safeguards equipment supplied 1from Bus 133B.
.The'AC sequencer.for. channel A relatra safeguards
. equipment remained-operable throughout the event as were the. channel B AC and'DC sequencers..The safeguards loads from all h80 volt equipment, except 1B3B associated equirment (which is AC-3A
.only) remained operable from the DC channel A sequencer SI-1.
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LMonthly< Operations (Report-IAugust.1980' i
iPage Two I
' A.'
PERFORMANCE CHARACTERISTICS (Continued)
-LER Number ~
. _ Deficiency.
'LER 80-01h
- Transformer -(Th) of DG-r failed. This transformer fed power ;to.the diesel's oil' immersion heater as ell as.; alarm circuitry; corresponding to _the v
following items: lLov. lube oil; pressure, lov lube oil level,2and.High orJLov lube oil' temperature.
During the time of the transformer. (Th) failure,-
DG-2 as(vell, the 161KV 'and: 3h5KV systems were available:and. operable and would have been more than capable of mitigating the _ circumstances of '
an accident should the need arise. :In addition, DG-1 wasEconsidered~ inoperable only during'the-time-that the transformer was being changed out, i.e. only while DG-1 was in " local maintenance."
LER 80-015 During routine' inspection, it was noted that trip unit setpoints on "C" channel, trip unit.hl(Steam
~
Generator Level) had become positive rather than negative. Maintenance' order 6430 was written to investigate and repair the problem. The RPS was immediately placed in a'two-out-of-three logic to trip mode. ' Technical Specification 1.3(5)' applies.
B.
CHANGES IN OPERATING METh0DS-None C.-
RESULTS OF SURVEILLANCE TESTS AND INSPECTIONS None
'D.
- CHANGES', TESTS AND _ EXPERIMENTS CARRIED OUT WITHOUT COLMISSION
. APPROVAL i
Procedure Description SP-RPS-5 Excore Detector Symmetric Offset recalibration/
no adjustment required.
'SP-FAUD-l '
Fuel Assembly Uplift Condition Detection /all results normal.
SPA RC-3' Reactivity Computer and Beactor Physics Content P
adjustment /results are normal.
EEAR(FC-79-166-LCV-2 Replacement / completed per procedure.
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~ Monthly Operations Report August 1980.
Page Three D.
LCHANGES, TESTS AND EXPERIMENTS CARRIED OUT WITHOUT COMMISSION APPROVAL'(Continued)
- Procedure Description-DCR 743-33
-Replacement of. Component Cooling Heat Exchanger Rav Water Inlet Valve / completed per design.
EEAR FC-79-7 Seismic Supports for Reactor Missle' Shields /
-completed as designed.
DCR 76-30 Containment Decon and Cleanup / completed as designed.
EEAR FC-79-108 Diaphram Modification (WD-9h5 and WD-9h6)/
completed as-designed.
E.
RESULTS OF LEAK RATE TESTS
'There were no leak rate tests performed during August except ST-CONT-2 by operators on PAL door.
F.
CHANGES IN PLANT OPERATING STAFF Miss Elizabeth Goebel started with H.P. group 8-18-80, f-G.
TRAINING Training for August included the following:
- EDO Training for plant supervisors.
- System Training for operations.on HVAC, Halon and Fire Detection.
Fire brigade training for plant personnel.
- Radioactive material handling for CARP personnel.
Stretch power for all staff and operations personnel.
Driver training ~for plant personnel.
'- Emergency sampling.
- OIE notices and bulletin review.
- Cycle 6 Tech. Spec.'for operations.
~
- Safety. meeting for operations,' maintenance and
.teehnicali groups.
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?Monthli. Operations.Repdrt Augast 19801 PagelFour
.H.
- CHANGES, TESTS AND EXPERIMENTS REQUIRING. NUCLEAR REGULATORY-.
COMMISSION AUTHORIZATION PURSUANT TO 10CFR50 59..
Chan6ei; To Facility OperatingL License DPR-40s
.. Amendment No. 50,~ dated August 15,'1980... This amendment.
changed License Co'ndition 3.A'.'
and.the Technical Speci-fications to authorize operation-at 1500.MWt.
Amendment No.,51,: dated August 28,.1980. This amendment-deleted certain' environmental monitoring and reporting
- requirements and increased the maximum and. differential condenser cooling vater discharge temperature limits.
h.
tb-Approved By
' Manager-Foft Calhoun Station-h
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Monthly. Operations, Report.-
~ August,1980.
~ Page' = Five
'II.
MAINTENANCE (Significant Safety Related)
M- 0. #
Oate Description-Corrective Acticn
.6h72 T-16-80:
.HCV-1108A vill not shut.
Replaced solenoid valve 6h90 7-18-80:
CH-13 leak.
Replaced valve CH-258.
Tightened intake and-discharge
'6568
~ 7-21-80 RMO-55 leak..
6832 8-20-80 D-2 Fuel'oi1Ltransfer pumps vill Changed out 0-ring in foot valve.
-not pick up suction.
I665h 8-7-80 RM-055 flange leak.
Install new gasket.
6579 8 h-80 CH-1B has internal leak.
Replaced gaskets and 3 discharge-valves.
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