ML19337A602
| ML19337A602 | |
| Person / Time | |
|---|---|
| Site: | North Anna |
| Issue date: | 09/09/1980 |
| From: | Neufer A, Woodsmall W VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.) |
| To: | |
| Shared Package | |
| ML19337A600 | List: |
| References | |
| NUDOCS 8009290321 | |
| Download: ML19337A602 (9) | |
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i VIRGIrlIA ELECTRIC Afl0 POWER COMPANY i
NORTH ANNA POWER STATI0ft i
MONTHLY OPERATIf;G REPORT 1
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MONTH 4,,n,,e t YEAR m i
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i APPROVED:
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STATION MANAGER U
8009290 32.)
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r AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.
50-338 UNIT t1A 1 DATE 9-9-80 COMPLETED BY W. A. Woodsmall, III TELEPHONE (703) 894-5151 MONTH August DAY AVERAGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL (MWe-Net)
(MWe Net) 1 809 37 f>31 2
810 is 833 3
808 39 838 808 4
20 838 5
808 21 838 6
807 22 838 7
807 836 23 8
807 24 828 9
809 25 820 to 744 26 810 II 83?
27 835 831 12 33 g4j 13 830 835 29 la 809 30 829 15 834 3
837 16 830 INSTRUCTIONS On this format. list the average daily unit power levelin MWe Net for each day in the reporting month. Compute to the nearest whole megawatt.
(9/77) 1
r OPERATING DATA REPORT DOCKET NO. 50-333 DATE 09-09-80 COMPLETEU llY W.A.Woodp all,III TELEPilONE 701/R04-6151 OPERATING STATUS N"
I. Unit Name:
North Anna 1
- 2. Reporting Period:
A urrust 1980
- 3. Licensed Thermal Power (MW ):
2775
- 4. Nameplate Rating (Gross MWe):
947
- 5. Design Electrical Rating (Net MWe): 907 880
- 6. Maximum Dependable Capacity (Gross MWe):
- 7. Maximum Dependable Capacity (Net MWe):
850
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Gise Reasons:
N/A
- 9. Power Lesel To Which Restricted,If Any (Net MWe):
N/A
- 10. Reasons For Restrictions.lf A.ny:
N/A This Month Yr..to.Dat e Cumulatise 744 5,855 19,632 iI. Ilours in Reporting Period
- 12. Number Of flours Reactor Was Critical 744 4.979.B Z5.145.0
- 13. Reactor Reserve Shutdown flours
'O 55J 203.9
- 14. Ilours Generator On.Line 744 4,780.7 14,833.9
- 15. Unit Reserse Shutdown floun 0
0 0
- 16. Grow Thermal Energy Generated (MWH) 2,037,456 12.15B 0B1 38.437.994
- 17. Gross Electrical Energy Generated (MWH) 6 J R. J2.9_. _.
1 #06. 70R 7? 797.747
- 18. Net Electrical Energy Generated (MWH) 611.343 3.577.404 11.430,gs0
- 19. Unit Service Factor 700 B7.6 75.5
- 20. Unit Asailability Factor 100 BZ.6 75.5
- 21. Unit Capacity Factor IUsing MDC Net) 96.7 71.9 69.5
- 22. Unit Capacity FactorIUsing DER Net) 90.6 67.4 64.2
- 23. Unit Forced Outage Rate o
11.3 6.B
- 24. Shutdowns Scheduled Oser Next 6 Months ITy pe. Date,and Duration of Each):
Refuelina-six weeks t Deceml>er 1980 and Jangqru 1991
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
N/A
- 26. Unit > In Test Status Irrior to Commercial Operation):
Forecast Achiesed INITIA L CRITICALITY INITI AL ELFCTRICITY CO\\1M ERCI A L OPER ATION 10/77)
b DOCKEI NO. _8_0-338 UNITSilUIDOWNS AND PODER REDUCllONS UNil N AME
' rth Anna 1 DAIE
_-9-80 COMPLETED ny Neuter Ittp0R1 hl0 Nill Auoust 1980 irt.ErilONE TT03) 894-5151 ext. 22' h.
- f 8
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'h Y f, k
Licensee E*
Cause & Corrective N..
Date y
3g
)s5 Eveni y
At tl"" 8" H,
gx y
jgg Itepost a un u Pievent Itecurience g
6 b
I j
No si';nificant pcwer eductic nS or plant Shutdown'S.
}
d b,.
1 t
- t i
2 3
4 I: Forced Iteason:
Metintil:
Exhibit G. Instructions S: Stlieduled A Lpeipment Failnre(Explain),
I Manual for Picparation of Dana D Mainte sance niTest 2-Manual Sciarn.
Entry Sheels for 1.icensee C.itefueling 3 Automatic Sesam.
Event !tepost (l.I'1111 !c (Ntilti G-D.Itegulatory itest Iction 4-Olher (Explain) 0161)
E Operator Training & IJcense Examination i
F Adndnistrative 5
ti Operational 1:ssos (Emplain) thhibit I-Same Source p:/77) ll Other (Earlain)
OPERATING DATA REPORT DOCKET NO.
50-339 DATE 9-9-W COMPLETED BY W. A. Woodsmall, IIK TELEPHONE
(/U3) W4-5151 OPERATLNG STATUS N
- 1. Urdt Name:
Nnrth Ann 3 9
- 2. Reporting Period:
Auonst 1990
- 3. Licensed Thermal Power (MWt):
277G
- 4. Nameplate Rating (Gross MWe):
947
- 5. Design Electrical Rating (Net MWe):
907 429
- 6. Maximum Dependable Capacity (Gross MWe):
898
- 7. Maximurn Dependable Capacity (Net MWe):
8' If Changes Occur in Capacity Ratings (1tems Number 3 nrough 7) Since Last Report. Give Reasons:
Item 1 channart frnm 170 en 977c h;, r,.11 tw..g r i 4,gmc7 a3+na p_71_on
- 9. Power Level To Which Restricted,if Any (Net MWe):
N/A
- 10. Reasons For Restrictions,if Any:
N/A l
his Month Yr to-Date Cumulative
- 11. Hours in Reporting Period 744 1 9nq 1 9no
- 12. Number Of Hours Reactor Was Critical
??G P 7'4 A 4 776 4
- 13. Reactor Reserve Shutdown Hours 0
0 0
- 14. Hours Generator On-Line 55 s;
RR 0
0 0
- 15. Unit Reserve Shutdown Hours
- 16. Gross Thermal Energy Generated (MWH) 39.455 4 4 R17 a1 917 8.174 8.174 8.174
- 17. Gross Electrical Energy Generated (MWH)
- 18. Net Electrical EnerEy Generated (MWH) 6,562 6.56?
6.562
- 19. Unit Service Factor
_ N/A N/A N/A
- 20. Unit Availability Factor N/A M/A M/A
- 21. Unit Capacity Factor (Using MDC Net)
N/A N/A tDA
- 22. Unit Capacity Factor (Using DER Net)
N/A N/A N/A
- 23. Unit Forced Outage Rate N/A N/A N/A
- 24. Shutdowns Scheduled Over Next 6 Months (Type. Date,and Duration of Eacht:
'A d i f f r n + 1 n n e -
Mnunn,hnr 1 1000 11 Asur Maintenance: April 1. 1981-11 d5vs 09-4-80
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
- 26. Units In Test Status (Prior to Commercial Operationi:
Forecast Achieved INITIA L CRITICALITY
-6/12/80 INITIAL ELECTRICITY 8/P5/80 COMMERCIAL OPERATION 11/15/80 1o/77)
AVERAGE DAILY UNIT POWER LEVEL 50-339 DOCKET NO.
UNIT NA 2 DATE 9-9-80 COMPLETED BY kl. A. Woodsmall, III TELEPHONE - (703) 894-5151 MONTH Aunust DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 1 0
17 n
2 0
18 0
3 0
19 0
4 0
20 0
5 0
21 0
6 0
22 0
7 0
23 0
8 0
24 0
9 0
28 25 10 0
26 la l1 0
27 102 12 0
28 128 13 0
29 0
14 0
30 0
0 0
15 3,
16 0
INSTRUCTIONS On this format, list the average daily unit power levelin MWe Net for each day in the reporting month. Compute to the nearest whole megawatt.
(9/77)
50-339 DOCKET NO.
UNIT SHU1 DOWNS AND POWER REDUCTIONS Noreh Anna 2 UNIT N AME DATE no-no an A.G-Neufer COMPLETED BY REPORT MONTH August T ELEPHONE 703/894-5151 h'8 5g 3
y Licensee
,E r, Cause & Corrective No.
Date g
3g i
js5 Event p
Action to gu Presen Recurrence f:
5 jgg Report #
mV H
g 6
Initic 1 Power Gene ratic1 begins 08-2 i-80 at 0547.
(Not ccmmerci al) 80-01 80-08-26 F
18.1 H+
3 Turbine trip / Reactor trip when genera-tor breaker was openec'. Placed recor-ders on Ibactor Protection Circuits to tra.m cause.
80-02 80-08-27 F
2.4 H*
3 Turbine Trip /Roactor Trip when Oversped Protection Controller was activated during test.
80-03 80-08-28 F
2.0 A*
3 Steam Gcnerator Lo Level Reactor Trip caused by loss of Feedwater Flow when Condensate Pump Suction Straincts were l
clogged up.
C1 caned straincts.
W 80-04 80-08-23 F
79.5 D
1 280-051/037,0 VALygg Unit Shutdown to comply with Technical Spccifications TS. 3.6.3.1 Fcedwater/
Containment Penetration Tsolation.
I 2
3 4
F: Forced Reason:
Method:
Exhibit G. instructions S: Scheduled A Equipment Failure (Explain) 1-Manual for Preparation of Data B. Maintenance of Test 2-Manual Scram.
Entry Sheets for Licensee C. Refueling 3 Automatic Scram.
Event Report (LER) File (NUREG.
D-Regulatcry Restriction 4-Other (Explain) 0161)
E-Operator Training & License Examination F-Administrative 5
G-Operational Error (Explain)
Exhibit I-Same Source (9/77) li Other (Explain)
-sco Attached Sheet
(2)
DOCKE1NO.
UNil SIIUIDOWNS AND POWI:R REDUCI10NS UNIINAML DATE 00-09-90 COMPLElED BY
,1.G.Neufer REPORT MONIll,,ugust TELEPItONE 703/S94-5151 C
5 Licensee E-t,
{q Cause & Corrective
!g 3
$ [y j~
Event gy
]
Action to No.
DJte g
3g yE ygc Report */
to U O
Present Recurrence H
o u
e 6
80-04 F
Conti tues chrough end of. month.
Shut Down I
2 3
4 F: Forced Reason:
Method:
Exhibit G -Instructions S: Schedu ed A. Equipment Failure (Explain) 1 Manual for Preparation of Data B. Maintenance of Test 2-Manual Scram.
Entry Sheets for Licensee C-Refueling 3-Automatic Scram.
Event ReporI (1.ER) hie (NURI G-D Regulatory Restriction 4-Other (Explain) 0161)
E-Operator Training & License Examination F Administrative 5
G-Operational Erroi (Explain)
Exhibit ! - Same Source (9/77)
Il Other (Explain)
Page 1 of 1 4
UNIT SilUTDOWN AND POWER REDUCTIONS EXPL C'sTION SilEET DOCKET NO.
50-339 REPORT MONTH August UNIT NNIE North Anna 2 YEAR 1980 DATE 09-09-80 r
COMPLETED BY A. G. Neufer l
80-01 Unit was being removed f rom service for a scheduled turbine overspeed test.
When the last generater output breaker was opened, the turbine and reactor tripped. An improperly set transmitter PT-MS-232 caused turbine valves to j
pulse open raising the 1st stage press to greater than 10% (turbine power greater than 10% with generator output breakers open causes a turbine trip) j' resulting in a turbine trip and reactor trip.
l 80-02 When the Overspeed Protection Controller pulsed during the planned overspeed test it caused First Stage Impulse Pressure to go greater than 10% inducing a signal te reinstate the at-power trips.
t I
80-03 Condensate Pump Suction Strainers clogged up causing a loss of Feedwater Flow.
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