ML19337A602

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Monthly Operating Repts for Aug 1980
ML19337A602
Person / Time
Site: North Anna  Dominion icon.png
Issue date: 09/09/1980
From: Neufer A, Woodsmall W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
Shared Package
ML19337A600 List:
References
NUDOCS 8009290321
Download: ML19337A602 (9)


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1 i i VIRGIrlIA ELECTRIC Afl0 POWER COMPANY i

NORTH ANNA POWER STATI0ft i
MONTHLY OPERATIf;G REPORT 1

) MONTH 4,,n,,e t YEAR m i >

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APPROVED:

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thV 4 l STATION MANAGER U 8009290 32.)

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r AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-338 UNIT t1A 1 DATE 9-9-80 COMPLETED BY W. A. Woodsmall, III TELEPHONE (703) 894-5151 MONTH August DAY AVERAGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL (MWe-Net) (MWe Net) 1 809 37 f>31 2 810 is 833 3 808 39 838 4 808 838 20 5 808 21 838 6 807 22 838 7 807 23 836 8 807 24 828 9 809 25 820 to 744 26 810 II 83? 27 835 12 831 g4j 33 13 830 29 835 la 809 30 829 15 834 837 3

16 830 INSTRUCTIONS On this format. list the average daily unit power levelin MWe Net for each day in the reporting month. Compute to the nearest whole megawatt.

(9/77) 1

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OPERATING DATA REPORT DOCKET NO. 50-333 DATE 09-09-80 COMPLETEU llY W.A.Woodp all,III TELEPilONE 701/R04-6151 OPERATING STATUS N"

I. Unit Name: North Anna 1

2. Reporting Period: A urrust 1980
3. Licensed Thermal Power (MW ): 2775
4. Nameplate Rating (Gross MWe): 947
5. Design Electrical Rating (Net MWe): 907
6. Maximum Dependable Capacity (Gross MWe): 880
7. Maximum Dependable Capacity (Net MWe): 850
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Gise Reasons:

N/A

9. Power Lesel To Which Restricted,If Any (Net MWe): N/A
10. Reasons For Restrictions.lf A.ny: N/A This Month Yr..to.Dat e Cumulatise iI. Ilours in Reporting Period 744 5,855 19,632
12. Number Of flours Reactor Was Critical 744 4.979.B Z5.145.0
13. Reactor Reserve Shutdown flours 'O 55J 203.9
14. Ilours Generator On.Line 744 4,780.7 14,833.9
15. Unit Reserse Shutdown floun 0 0 0
16. Grow Thermal Energy Generated (MWH) 2,037,456 12.15B 0B1 38.437.994
17. Gross Electrical Energy Generated (MWH) 6 J R . J2.9_ . _. 1 #06. 70R 7? 797.747
18. Net Electrical Energy Generated (MWH) 611.343 3.577.404 11.430,gs0
19. Unit Service Factor 700 B7.6 75.5
20. Unit Asailability Factor 100 BZ.6 75.5
21. Unit Capacity Factor IUsing MDC Net) 96.7 71.9 69.5
22. Unit Capacity FactorIUsing DER Net) 90.6 67.4 64.2
23. Unit Forced Outage Rate o 11.3 6.B
24. Shutdowns Scheduled Oser Next 6 Months ITy pe. Date,and Duration of Each):

Refuelina-six weeks t Deceml>er 1980 and Jangqru 1991

25. If Shut Down At End Of Report Period. Estimated Date of Startup: N/A
26. Unit > In Test Status Irrior to Commercial Operation): Forecast Achiesed INITIA L CRITICALITY INITI AL ELFCTRICITY CO\1M ERCI A L OPER ATION 10/77)

b DOCKEI NO. _8_0-338 UNITSilUIDOWNS AND PODER REDUCllONS ' rth Anna 1 UNil N AME DAIE _-9-80 COMPLETED ny Neuter Ittp0R1 hl0 Nill Auoust 1980 irt.ErilONE TT03) 894-5151 ext. 22' h.

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!! ., jg 'h Y f, Licensee E*, k Cause & Corrective N. . Date y H, gx 3g @

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)s5 Eveni y un u At tl"" 8" jgg Itepost a g Pievent Itecurience 6 b I .

j No si';nificant pcwer eductic nS or plant Shutdown'S.

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, I: Forced Iteason: Metintil: Exhibit G . Instructions S: Stlieduled A Lpeipment Failnre(Explain), I Manual for Picparation of Dana D Mainte sance niTest 2-Manual Sciarn. Entry Sheels for 1.icensee C.itefueling 3 Automatic Sesam. Event !tepost (l.I'1111 !c (Ntilti G-D.Itegulatory itest Iction 4-Olher (Explain) 0161)

E Operator Training & IJcense Examination i F Adndnistrative 5 ti Operational 1
ssos (Emplain) thhibit I- Same Source p:/77) ll Other (Earlain)

OPERATING DATA REPORT DOCKET NO. 50-339 DATE 9-9-W COMPLETED BY W. A. Woodsmall, IIK TELEPHONE (/U3) W4-5151 OPERATLNG STATUS N

1. Urdt Name: Nnrth Ann 3 9
2. Reporting Period: Auonst 1990
3. Licensed Thermal Power (MWt): 277G .
4. Nameplate Rating (Gross MWe): 947
5. Design Electrical Rating (Net MWe): 907
6. Maximum Dependable Capacity (Gross MWe): 429
7. Maximurn Dependable Capacity (Net MWe): 898 8' If Changes Occur in Capacity Ratings (1tems Number 3 nrough 7) Since Last Report. Give Reasons:

Item 1 channart frnm 170 en 977c h;, r,.11 tw ..g r i 4,gmc7 a3+na p_71_on

9. Power Level To Which Restricted,if Any (Net MWe): N/A ,
10. Reasons For Restrictions,if Any: N/A l

his Month Yr to-Date Cumulative

11. Hours in Reporting Period 744 1 9nq 1 9no
12. Number Of Hours Reactor Was Critical  ??G P 7'4 A 4 776 4
13. Reactor Reserve Shutdown Hours 0 0 0
14. Hours Generator On-Line 55 s; RR
15. Unit Reserve Shutdown Hours 0 0 0
16. Gross Thermal Energy Generated (MWH) 39.455 4 4 R17 a1 917
17. Gross Electrical Energy Generated (MWH) 8.174 _ _ ,

8.174 8.174

18. Net Electrical EnerEy Generated (MWH) 6,562 _

6.56? 6.562

19. Unit Service Factor _ N/A N/A N/A
20. Unit Availability Factor N/A M/A M/A
21. Unit Capacity Factor (Using MDC Net) N/A N/A tDA .

I

22. Unit Capacity Factor (Using DER Net) N/A _

N/A N/A

23. Unit Forced Outage Rate N/A N/A N/A l
24. Shutdowns Scheduled Over Next 6 Months (Type. Date,and Duration of Eacht: ,

TMI 'A d i f f r n + 1 n n e - Mnunn,hnr 1 1000 11 Asur l Maintenance: April 1. 1981- 11 d5vs

25. If Shut Down At End Of Report Period. Estimated Date of Startup: 09-4-80
26. Units In Test Status (Prior to Commercial Operationi: Forecast Achieved INITIA L CRITICALITY -6/12/80 INITIAL ELECTRICITY 8/P5/80 COMMERCIAL OPERATION 11/15/80 1o/77) l 1

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.

50-339 UNIT NA 2 DATE 9-9-80 COMPLETED BY kl. A. Woodsmall, III TELEPHONE - (703) 894-5151 MONTH Aunust DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1 0 17 n

. 2 0 18 0 3 0 _

19 0 4 0 20 0 5 0 21 0 6 0 22 0 7 0 23 0 _

8 0 24 0 9 0 25 28 10 0 26 la l1 0 27 102 12 0 28 128 13 0 29 0 14 0 30 0 15 0 3, 0 16 0 INSTRUCTIONS On this format, list the average daily unit power levelin MWe Net for each day in the reporting month. Compute to the nearest whole megawatt.

(9/77)

50-339 DOCKET NO.

UNIT SHU1 DOWNS AND POWER REDUCTIONS Noreh Anna 2 UNIT N AME DATE no-no an COMPLETED BY A.G- Neufer August REPORT MONTH T ELEPHONE 703/894-5151 5g 3 y Licensee ,E r, Cause & Corrective No. Date g 3g i js5 Event p h'8 gu Action to H

f: 5 jgg Report # mV g Presen Recurrence 6 .

Initic 1 Power Gene ratic1 begins 08-2 i-80 at 0547. (Not ccmmerci al) 80-01 80-08-26 F 18.1 H+ 3 Turbine trip / Reactor trip when genera-tor breaker was openec'. Placed recor-ders on Ibactor Protection Circuits to tra.m cause.

80-02 80-08-27 F 2.4 H* 3 Turbine Trip /Roactor Trip when Oversped Protection Controller was activated during test.

80-03 80-08-28 F 2.0 A* 3 Steam Gcnerator Lo Level Reactor Trip caused by loss of Feedwater Flow when Condensate Pump Suction Straincts were l

clogged up. C1 caned straincts.

80-04 80-08-23 F 79.5 D 1 280-051/037,0 W VALygg Unit Shutdown to comply with Technical Spccifications TS. 3.6.3.1 Fcedwater/

Containment Penetration Tsolation.

I 2 3 4 F: Forced Reason: Method: Exhibit G. instructions S: Scheduled A Equipment Failure (Explain) 1-Manual for Preparation of Data B. Maintenance of Test 2-Manual Scram. Entry Sheets for Licensee C. Refueling 3 Automatic Scram. Event Report (LER) File (NUREG.

D-Regulatcry Restriction 4-Other (Explain) 0161)

E-Operator Training & License Examination F-Administrative 5 G-Operational Error (Explain) Exhibit I- Same Source (9/77) li Other (Explain)

-sco Attached Sheet

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DOCKE1NO.

UNil SIIUIDOWNS AND POWI:R REDUCI10NS UNIINAML DATE 00-09-90

,1.G.Neufer

, COMPLElED BY REPORT MONIll ,,ugust TELEPItONE 703/S94-5151 C

- !g 3 $

j~[y 5 Licensee E-t, {q Cause & Corrective No. DJte g 3g  % Event gy ]

O Action to H yE $ ygc e

Report */ to U o u

Present Recurrence 6

80-04 F Conti tues chrough end of . month.

Shut Down I 2 3 4 F: Forced Reason: Method: Exhibit G -Instructions S: Schedu ed A. Equipment Failure (Explain) 1 Manual for Preparation of Data B. Maintenance of Test 2-Manual Scram. Entry Sheets for Licensee C-Refueling 3-Automatic Scram. Event ReporI (1.ER) hie (NURI G-D Regulatory Restriction 4-Other (Explain) 0161)

E-Operator Training & License Examination F Administrative 5 G-Operational Erroi (Explain) Exhibit ! - Same Source (9/77) Il Other (Explain)

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UNIT SilUTDOWN AND POWER REDUCTIONS EXPL C'sTION SilEET DOCKET NO. 50-339 REPORT MONTH August UNIT NNIE North Anna 2 YEAR 1980 DATE 09-09-80 r

COMPLETED BY A. G. Neufer l

80-01 Unit was being removed f rom service for a scheduled turbine overspeed test.

!, When the last generater output breaker was opened, the turbine and reactor

. tripped. An improperly set transmitter PT-MS-232 caused turbine valves to j pulse open raising the 1st stage press to greater than 10% (turbine power

greater than 10% with generator output breakers open causes a turbine trip) j' resulting in a turbine trip and reactor trip.

l 80-02 When the Overspeed Protection Controller pulsed during the planned overspeed

test it caused First Stage Impulse Pressure to go greater than 10% inducing
a signal te reinstate the at-power trips.

! t I 80-03 Condensate Pump Suction Strainers clogged up causing a loss of Feedwater

! Flow. i 1

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