ML19332E997

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Monthly Operating Rept for Nov 1989 for Trojan Nuclear Plant
ML19332E997
Person / Time
Site: Trojan File:Portland General Electric icon.png
Issue date: 11/30/1989
From: Ulmer F, Yundt C
PORTLAND GENERAL ELECTRIC CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
CPY-325-89, NUDOCS 8912130251
Download: ML19332E997 (6)


Text

1" NW P rtland General Electric Company Tr:jan Nuclear Plant 71760 Columbia River liwy

' Rainier, Oregon 97048 (503)$563713 December 6, 1989 CPY-325-89 US Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:

Monthly Operating Report in accordance with the Trojan Nuclear Plant Technical Specifications reporting requirements, the Monthly Operating Data Report is submitted for November, 1989.

Sincerely, 0

C.

, Yundt General Manager CPY:sp Attachment c:

Mr. John B. Martin Regional Administrator, Region V US Nuclear Regulatory Commission Mr. David Stewart Smith Department of Energy State of Oregon Resident Inspector MOR Distribution

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j TROJAN NUCLEAR PLANT 1

Trojan Operating Report November 1989 OPERATIONS l

The plant began the month in Mode 1, at 97% power.

The Plant i

reached 97% power on October 4th.

The plant is presently being maintained at 97% power as a result of an administrative reduction in Reactor Coolant System average temperature (Tgg ).

This resulted from changes to the Over Temperature Delta Temperature setpoints to reflect the plants safety analysis l

assumptions.

The plant will remain at this power level until an engineering analysis is completed and changes accomplished to allow us to increase our output.

On November 1",

a series of short duration alarms of Main Generator field grounds were received.

Various attempts were made to locate the source of the grounds with no success.

Monitoring equipment has been installed to monitor for grounds.

On November 8*,

a spurious high alarm on the Containment radiation monitor (PRM-1D), caused an automatic closure of the hydrogen vent Containment isolation valves.

The source of the spurious signal has not been determined.

The effected PRM and the other associated PRMs were satisfactorily retested.

PRM-1D was restored to service.

A noise suppression circuit is being installed to reduce spurious signals.

On November 13*,

the

'C' Main Steam Isolation Valve Bypass failed to close during the performance of testing.

The valve was isolated in accordance with the Trojan Technical Specifications.

On November 20*,

several problems were identified with the performance of fire protection surveillances.

All work on fie detectors and alarm supervision systems was stopped until a review of fire barrier inspections was completed.

A special task force has been formed to review past and scheduled surveillances in other areas to assure that none are missed, and to develope a program to schedule all surveillances under one program with the responsibility residing with Plant Planning and Scheduling.

On November 30", the number 1 seal water leak off flow indicator for Reactor Coolant Pump number 2 failed.

The failure was identified as a loose fuse clip.

The problem was fixed and verified not to exist on any other seal water leak off flow indicators.

The plant ended the month in Mode 1, at 97% power.

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MAINTENANCE Significant maintenance completed during this period includes:

Repaired the

'A' SO Detector.

p Repaired the Su11 air Air Compressor.

APPROVED Plant C p h1 Manager l

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AVERAGE DAILY UNIT P0k'ER LEVEL i

DOCKET NO: 50-344 UNIT: Trojan DATE: December, 19_89l COMPLETED BY:_F.

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Ulmer TELEPHONE: so3 s%6-1711 ext 4495 MONTH ' November, 1989 DAY AVERAGE DAILY P0k'ER LEVEL DAY AVERAGE DAILY P0k'ER LEVEL (HWe-Net)

(MWe-Net) 1 1069 17 1066 2

1069 18 1071 3

1067 19 1070 4

1070 20 1069 5

1069 21 1069 6

1071 22 1070 7

1071 23 1068 8

1070 24 1071 9

1068 25 1072 10 1066 26 1072 11 1066 27 1071 12 1069 28 1071 13 1069 29 1071 14 1069 30 1073 15 1069 31 NA 16 1069 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting month.

Compute to the nearest whole megawatt.

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l OPERATLNG DATA REPORT 50-344

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DOCKET NO.

DATE.lkccattacr, 1989 -

COMPLETED Y A J.

Ulmer TELEPHONE 5 0 3 - s u-3 713 Ext. 495 OPERATING STATUS Trojan Nuclear Plant Notes

1. Unit Nonw:

Novanhar. 14n0 t

. 2. Reporting Period:

3411

3. Lleensed Thermel Power (MWt):

1216

4. Namepiste Rating (Gross MWe):

1I30

5. Design Electrical Rating (Not MWe):

1153

6. Masimum Dependable Capacity (Grom MWe):

1095

7. Maximum Dependable Capacity (Net MWe):
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report.Give Reasons:

No chanoe.

Administrative 1v restricted to 97% of

9. Power level To Which Restricted,1f Any (Net MWe):

rated power.

10. Reseems For Restrictions. lf Any:

RCS temocrature instrumant inaccuracy Annn=ntinna and 4-nad nn avarage temocrature limit (589'P) and ovnr-tnmnaratura/nunennwar entnn4nt m i a rms -

management hold.

This Meath Yr. te.Dete Cumulative 720 8016 116136 i1. Hours la Reporting Periog 720 4679.2 71osa_2

12. Number Of Hours Rosetor was Critieel 0

0 3 tn7

13. Rosetor Reserve Sheldown Hours 720 4540 a 71nna 7
14. Hours Generator On4.4me
15. Unit Reserve Shutdown Hours 0

3249 o

2381756 150234s5 22662aaas

16. Gross Thermal Energy Genersted (MWM) 804585 sn61627 7anoin7o
17. Geen Elmetrieel Energy Genereted (MWH) 770073 4784471 70652541
18. Not Electrical Energy Generated (MWM) 1oo s6.8 61.2
19. Unit Service Factor

_ 100 56.B 64.0

20. Unit Aveitability Eseto, 97 7 5a %

66 R

21. Unit Capacity Feeter (Using MDC Net) 94.7 52.8 53.8
22. Unit Capecity Factor (Using DER Ne )

0 2.8 13.2

23. Unit Forced Outage Rate
24. Shutdowns Scheduled Over Next 6 Months (Type.Dete and Duration of Eacht:

Annual Refuelina Outaae, March 21, 1990 (78 days)

N/A

25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units in Test Status IPrior io Commercial Operstlos):

Foreenet Achieved N/A N/A INITIA L CRITICALITY N/A N/A INITIAL ELECTRICITY N/A N/A COMMERCIAL OPER ATION (0/77)

DOEMETNO. 50-344 UNITSHUTDOWNS ANDFOWER REDUCTIONS INGT MABIE Trnian DATE Decanhar-19A9 NIIO 8T E-1-

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REPDRT MON 118 Novesuber, 1989 TELEF990ME 503-556-3713 ext 495 i

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