ML19332D190

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Requests Response to Encl Concerns from Special Team Insp Rept 50-445/89-200 on 891016-27.Const & Testing of Plant Not Sufficiently Complete to Make Determination Re Operational Readiness
ML19332D190
Person / Time
Site: Comanche Peak Luminant icon.png
Issue date: 11/16/1989
From: Crutchfield D
Office of Nuclear Reactor Regulation
To: William Cahill
TEXAS UTILITIES ELECTRIC CO. (TU ELECTRIC)
References
50-445-89-200, NUDOCS 8911300131
Download: ML19332D190 (8)


See also: IR 05000445/1989200

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UMTED STATES -

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' NUCLEAR REGULATORY COMMISSION

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' November.16, 1989

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Docket: No.: 50-445:

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.Mr. W.- 1 Cahill, Jr.

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Executive Vice' President-

-Texas Utilities: Electric

1.400 North Olive Street, Lock Box 81

Dallas, Texas 75201;

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Dear Mr. Cahill:

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SUBJECT: NRC: INSPECTION REPORT 50-445/89-200

COMANCHE PEAK OPERATIONAL

READINESS ASSESSMENT TEAM INSPECTION-

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' An announced special' team inspection' of the Comanche Peak Steam Electric

. Station was. conducted by the NRC Headquarters staff during the' period of

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0ctober 16-27,c1989.' The purpose of this inspection.was to provide the-

. Director of the Office of Nuclear Reactor Regulation.with an independent-

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assessment of the construction and operational status of your facility.

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The'0perational-Readiness Assessment Team (ORAT) inspection concluded that

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the construction and testing lof the plant was not sufficiently complete to make

La determination withl respect to operational readiness.

Consequently, the team

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held an' interim-~ exit with you and members of your staff on October 27, 1989,

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-and will-schedule a follow-up inspection visit in the future. This: letter

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. documents the team's-. conclusions,-and'the1 concerns identified during the interim

exit that require your: attention before the follow-up. inspection.

This letter

~does not detaillany of.the strengths identified by the inspection team. A

discussion of the inspection findings will be provided in Inspection Report

50-445/89-200,- which will be issued following the completion of the remainder

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of the inspection.

The inspection team concluded that an insufficient number of systems were in

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the ' direct operational control of the operators to support a valid assessment

of operational readiness.

In addition, the team concluded that the plant

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staff had not adequately assumed responsibility for the systems and areas under

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operational control, and had not fully implemented operational programs.and

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= procedures as a direct result of the large amount of remaining construction and

maintenance work.. Finally, the team concluded that the operations and

operations support programmatic readiness were not adequate because several

operational programs had not been implemented or had weaknesses which precluded

their effective implementation.

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8911300131 891116

PDR

ADOCK 05000445

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Mr. W. - J.' Cahill, ' Jr.

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Novamber 16, 1989

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- As we discussed with you and your staff, our inspection activities resulted in

a clearer definition of the expectations regarding the level of construction

completion required for issuance of the operating license and a more detailed

assessment of the progress of your remaining work activities.

In addition,

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Lthe meaning and purpose of the operational readiness period was clarified.

As discussed during the interim exit, several actions must be taken before the

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remainder of the inspection can be completed.

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Evaluate and resolve the specific concerns identified by the inspection

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team and listed in Enclosure 1.

In addition, perform a broad-based

assessment of the~ adequacy and implementation of all of your programs

to identify and resolve any similar deficiencies.

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Based on the minimal previous comercial experience levels of your

'mid-level managers and. licensed operating staff, take steps to:

a.

Reduce the maintenance backlog and ensure that all systems are

functional for power operations.

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b.

Evaluate augmentation of the management staff with experienced

personnel,

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Focus attention on plant-labeling adequacy by examining the status of

the present plant labeling and evaluating the need for immediate

corrective actions, and by committing to implementing labeling

upgrades before the completion of the first refueling outage.

3.

The remainder of the ORAT inspection will be performed after you have:

a.

Demonstrated that all systems can function by the successful

performance of all technical specification surveillance tests that

are required for 5 percent power operations--to the extent they

can be performeo before fuel load,

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Decided that the facility is operationally ready for low power

operation, including completion of the items above, and advised the

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NRC that the facility is ready for the team to return and confirm

your operational readiness assessment.

Sincerely,

77/. W L /

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DennisM.Crutchfield, Ass 7cIitteDirector

for Special Projects

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Office of Nuclear Reactor Regulation

Enclosure:

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Identified Concerns

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'M . W. J. Cahill

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November 16, 1989

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cc w/ enclosure:

Mr. Robert F. Warnick.

Jack R. Newman, Esq.

Assistant Director

Newmr.n & Holtzinger

- for Inspection Programs

1615 L Street, NW

Comanche Peak Project Division

Suite 1000

.U. S. Nuclear Regulatory Connission

Washington, D.C.

20036

P. 0, Box 1029

Granbury, Texas 76048

Chief, Texas Bureau of Radiation Control

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Texas Department of Health

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Regional Administrator, Region IV

1100 West 49th Street

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U. S. Nuclear Regulatory Commission

Austin, Texas 78756

611 Ryan Plaza Drive, Suite 1000

Arlington, Texas 76011

Honorable George Crump

County Judge

Ms. Billie Pirner Garde', Esq.

Glen Rose, Texas 76043

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Robinson, Robinson, et al.

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103 East College Avenue

Appleton, Wisconsin 54911

Mrs. Juanita Ellis, President -

Citizens Association for S'ound Energy

1426. South Polk

Dallas, Texas: 75224

E. F. Ottney

P. O. Box 1777

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Glen Rose, Texas 76043

Mr. Roger.D. Walker

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Manager, Nuclear Licensing

Texas Utilities Electric Company

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400 North Olive Street, L. B. 81

Dallas, Texas 75201

Texas Utilities Electric Company

-c/o Bethesda Licensing

3 Metro Center, Suite 610

Bethesda, Maryland 20814

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William A. Burchette, Esq.

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Counsel for Tex-La Electric

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Cooperative of Texas

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Heron, Burchette, Ruckert & Rothwell

1025 Thomas Jefferson Street, NW

Washington, D.C. 20007

GDS Associates, Inc.

Suite 720

1850 Parkway Place

Marietta, Georgia 30067-8237

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ENCLOSURE 1

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CONCERNS. IDENTIFIED DURING INTERIM INSPECTION EXIT OF OCTOBER 27, 1989

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Unidentified hardware deficiencies

Numerous hardware deficiencies were

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1 dent 171ed in systems and rooms which had been turned over to operational

control. These deficiencies had not been i nntified during the room and

. system turnovers, and had not been identified by the operators or system

_ engineers during routine tours and surveillances.

For example, the _ inspection team identified (1) leakage of the IB Diesel

Generator (DG) jacket water and service water piping joints, and

_(2)' standing water, loose relay label plates, and broken terminal board

wire retainers in DG. control cabinets. The IE battery cells had

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electrolyte levels above high level marks and showed evidence of

overfilling. - There were-invalid Quality Control Nonconformance report

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waiver tags. posted on equipment which had not been removed nor identified

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during(CS) service water relief valve, tapt

room and area turnovers. The team Ound a leaking Containment

Spray

blockage of the CS flow

transmitter drain line, a disconnected limit switch on valve HCV-0606,

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and removed safety injection accumulator spool pieces without procedural

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guidance.

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Throughouttheplant,theteamnotedthat(1)theelectricaldistribution

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and process-instrumentation doors under operational control were not

routinely secured by(3)perations, (2) the vent and drain valve caps were

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not installed, and

several rising stem valves had water and debris in

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the top of the actuator which could adversely affect the operation and

reliability of the valves.

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Operational Responsibility - The actions of a licensed operator inoicated

a _ lack of " ownership" for the operational consequences of conflicting

testing requirements, in that the operator was persuaded by maintenance

technicians to simultaneously perform two surveillances which he believed

conflicted.

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Shift Communications - The team observed a lack of effective comunication

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between operating shifts concerning the corrective and troubleshooting

actions following problems encountered turning the main generator.

4.

System Status Control - ODA-410. " System Status Control," provided a

method for recording the current system valve alignments and maintaining

configuration control of all operational systems. A review of the DG

system identified that the valve status file was not being updated as

required, in that the position of DG starting air isolation valves was not

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correctly updated on the drawing. Although the use of marked-up drawinct

is a difficult method to implement, the valve alignments of only four

systems were being controlled by the procedure.

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LCO Tracking and Control - ODA-308, "LC0 Tracking Log," provided a method

for tracking and control of LC0 action requirements. The procedural

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requirements were not correctly implemented in that the entry and exit of

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LCOs were not logged, and the shift technical advisor reviews of recent

LCO action. requirements were not performed.

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Plant Investigation Reports - STA-503, " Plant Investigation Report,"'

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provided for identification.and tracking of PIRs in order to obtain timely

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and effective implementation of corrective actions for plant events.- This

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program was not properly implemented and-the corrective actions were not

~ timely or effective because (1) immediate corrective actions were not

being recorded, (2) PIRs were not initi.ated for problessiconcerning the

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main generator turning problems as indicated by the shift log, (3) the

operations department believed that PIR closure could occur when correc--

tive actions.were identified vice implemented, and most importantly (4) 23

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outstanding PIRs were overdue on October 20, 1989, by as much as

1-4= months and 4 PIRs on inadequate clearances as!early as April 1989 had

not been evaluated.

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7.

Corrective Actions for NRC Inspections - There were several' corrective

actions which remained to be completed for previous NRC inspection find-

ings. For example, the team noted that 159 of the original 238 discrep-

ancies between the emergency response guidelines and the facility's design

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basis remain to be resolved prior to fuel load.

in addition, the team

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noted that the corrective actions to resolve the accessibility and opera-

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bility of equipment in the AFW turbine feedwater pump. room'had nct identi-

fied or resolved concerns involving (1) inadequate grating installed to

access pquipment, (2) excessive turns required to operate valves,-and (3)

inadequate-room ventilation.

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Confined S) ace Entries - STA-606, " Work Requests and Work Orders,"

' requireo t1at a confined space work permit be issued prior to beginning

work in any confined space.

The team noted that work was secured on the

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outboard containment isolation valve for the containment spray system;

however, the confined space was-not secured (i.e., closed or posted)

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following the completion of this work.

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Design Modifications - STA-205, " Changes to Procedures," and STA-717,

. Design Modification Review Group," procedurally allowed modifications to

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be performed without a safety evaluation if the modification was performed

prior to fuel load. The applicant had performed safety evaluations for

all modifications and intended to incorporate all modifications as a final

safety-analysis change prior to fuel load; however, the potential existed

to miss evaluating a change to the facility.

In addition, STA-205 did act

require a safety evaluation or screening for typographical errors or for

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non-significant changes of intent. This ambiguous requirement had the

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potential to miss safety evaluation for omitted symbols such as +/- signs

and required individual interpretation as to the intent of the procedure.

10. Limiting Conditions for Operation Tracking - ODA-308, "LC0 Tracking Log,"

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did not require document #. tion of management authorization for voluntary

LC0 entries, verification of the required periodic management reviews, and

docunentation and retention of the rationale for LCO exits.

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. Root Cause Analysis and Trending - The system engineers minually performed

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data reduction and-trending-of component root ~cause failure. This method

-was time consuming and difficult to perfom because the nuclear plant

reliability data system (NPRDS) was not fully implemented and had numerous

component identification differences with the master equipment list.

12.

Inter-system Actuations - STA-606, " Work Control Procedure," did not

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require notes or precautions to specifically identify to the operators

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anticipated ' inter-system actuations such as alarms or trips which may

occur during planned work activities.

13. Timely Incident Investinations'- STA-422 " Processing of One Forms," did

not: support an expeditious initiation of incident investigations because

the one form must be processed through the work control center and plan of

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the day meetings before the. incident team is formed.

14.

Post-Trip Reviews - ODA-108, " Post-Trip Review," assumed that all trips

nad a cettnitive cause and did not provide for additional evaluations of

those. trips which cannot be definitively identified prior to restart of

the facility.- In addition, the procedure did not require timely. written

statements of the principals involved in a trip in order to document the

circumstances before memories fade.

15. . Plant Labelino - An upgrade program to improve the useability of the plant

labelingthroughouttheplanthadnotbeen'inglemented. The valves and

components were currently labeled with metai dog tags" which were very

difficult to locate and use.

In addition, rooms and commodities (i.e.,

trays, conduits, and piping)-were not currently labeled throughout the

plant. The implementation of this upgrade program had been delayed until

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completion of the'first refueling outage (and may not be finished by

then).

Because of the difficulty in finding and reading the present

labels, a potential exists for operator errors.

16. One Forms - STA-421, "One Form Evaluation," provided a new method for

identification and resolution of plant deficiencies and had not been

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_ implemented.

This program was intended to consolidate and simplify th

several problem identification methods.

17.

Safety Evaluations - STA-602, "Temporar,y Modifications," did not require a

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safety evaluation of~ temporary modifications which were performed before

fuel load. The applicant was performing temporary modifications without

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safety' evaluations and intended to reduce the number of outstanding

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temporary modifications, and perform safety evaluations of the remainder

-at th4 time of fuel load. Although acceptable, this method had the

potential to miss performing the required safety evaluations.

18.

Preventive Maintenance Programs - All of the periodic preventive mainte-

nance requirements were not being performed due to the large construction

and maintenance work load. As a result, the PM backlog was increasing.

19. Scaffolding - CMP-CV-1014, " Scaffold Erection and Control," which con-

trolled scaffolding erection over safety-related and seismic equipment

.during the operations phase, had not been implemented.

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" * 20. frevious Coasnercial Experience - Although the licensed operators met the

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minimum expertence requirements of the applicent's program for hot partic-

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1pation experience, the operators had minimal previous commercial operat-

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ing experience.

In addition, the mid. level managers in the areas of

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operations, technical support, plant evaluations, radiation protection,

and fire protection, also had minimal previous comercial operating

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experience. Although the ANSI 3.1 requirements for minimal experience

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levels had been met, the lack of depth of commercial operating experience

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in sanapers and operators will make a smooth initial startup wore

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difficu.t.

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21. Procedural Inadecuacies - ABN-710A, "SG Water Level Instrument Malfunction

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Chect," had referencing inadequacies which had the potential to confuse

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the operators and result in a trip of the reactor. All of the operators

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questioned incorrectly identified the steam generator protection bistables

due to confusing references in the procedure.

In addition, there were

unauthorized and unreviewed temporary markings on the instrument cards

which incorrectly identified the level switch numbers. Although correc-

tive actions for previously-identified procedure problems had been imple-

mented for this procedure, this potential e-ror was not identified.

22. Cualit.y Assurance involvement in 0)erations - Discussions with the

Operations Manager indicate that tte Quality Assurance Department had not

been used for the identification and resolution of operations problems.

In addition, the Quality Assurance Department had_not performed an audit

of the technical specification (TS) surveillance scheduling program, but

did intend to review this master schedule of the TS required testing prior

to fuel load. During a limited review, the inspection team identified

four errors in the master schedule where required TS surveillances were

not scheduled. The lack of Qus11ty Assurance Department involvement in

the support of management overview of the operations department and

-operational programs was not indicative of a pro-active approach to

quality involvement in the support of operational rndiness.

23. Technical Specification Surveillance Procedures - The trigger procedures

(i.e., shift logs) fcr conditional T5 surveillance requirem a ts allowed

missing hourly primary and secondary temperature and pressure readings due

to the longer frequency of the trigger procedures.

In addition, the TS

surveillance requirements for localized containment temperatures were not

specifically obtained by the surveillance procedure.

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Clearance Procedures - STA-605, " Clearance and Safety Tagging," allowed the

shift supervisor to remove a danger tag and reposition or operate equip-

ment on a temporary basis in nonemergency conditions without sufficient

controls to ensure the adequacy of the remaining clearance.

This is

particularly safety significant at this f acility due to the extensive use

of master clearances and tiered clearances.

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